55 resultados para MP3 (Audio coding standard)


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In this paper, a low-power, highly linear, integrated, active-RC filter exhibiting a multi-standard (IEEE 802.11a/b/g and DVB-H) application and bandwidth (3MHz, 4MHz, 9.5MHz) is present. The filter exploits digitally-controlled polysilicon resister banks and an accurate automatic tuning scheme to account for process and temperature variations. The automatic frequency calibration scheme provides better than 3% corner frequency accuracy. The Butterworth filter is design for receiver (WLAN and DVB-H mode) and transmitter (WLAN mode). The filter dissipation is 3.4 mA in RX mode and 2.3 mA (only for one path) in TX mode from 2.85-V supply. The dissipation of calibration consumes 2mA. The circuit has been fabricated in a 0.35um 47-GHz SiGe BiCMOS technology, the receiver and transmitter occupy 0.28-mm(2) and 0.16-mm(2) (calibration circuit excluded), respectively.

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This paper proposes an embedded ultra low power nonvolatile memory in a standard CMOS logic process. The memory adopts a bit cell based on the differential floating gate PMOS structure and a novel operating scheme. It can greatly improve the endurance and retention characteristic and make the area/bit smaller. A new high efficiency all-PMOS charge pump is designed to reduce the power consumption and to increase the power efficiency. It eliminates the body effect and can generate higher output voltage than conventional structures for a same stage number. A 32-bit prototype chip is fabricated in a 0.18 mu m 1P4M standard CMOS logic process and the core area is 0.06 mm(2). The measured results indicate that the typical write/erase time is 10ms. With a 700 kHz clock frequency, power consumption of the whole memory is 2.3 mu A for program and 1.2 mu A for read at a 1.6V power supply.

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A monolithic silicon CMOS optoelectronic integrated circuit (OEIC) was designed and fabricated with standard 0.6 mu m CMOS technology. This OEIC circuit consisted of an integrated double photodiode detector (DPD) and a preamplifier. The DPD detector exhibited high bandwidth by screening the bulk-generated diffusion carriers and suppressing the slow diffusion tail effect. The preamplifier exploited the regulated cascode (RGC) configuration as the input stage of receiver, thus isolating the influence of photodiode capacitance and input parasitic capacitance on bandwidth. Testing results showed that the bandwidth of OEIC was 700MHz, indicating the bit rate of 1Gb/s was achieved.

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A 1GHz monolithic photo-detector (PD) and trans-impedance amplifier (TIA) is designed with the standard 0.35 mu m CMOS technique. The design of the photo-detector is analyzed and the CMOS trans-impedance amplifier is also analyzed in the paper. The integrating method is described too. The die photograph is also showed in the paper.

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A silicon light emitting device is designed and simulated. It is fabricated in 0.6 mum standard CMOS technology. The device can give more than 1 muW optical power of visible light under reverse breakdown. The device can be turned on at a bias of 0.88 V and work in a large range of voltage: 1.0-6.0 V The external electrical-optical conversion efficiency is more than 10(-6). The optical spectrum of the device is between 540-650 nm, which have a clear peak near 580 nm. The emission mechanism can be explained by a hot carrier direct recombination model.

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An ultra low power non-volatile memory is designed in a standard CMOS process for passive RFID tags. The memory can operate in a new low power operating scheme under a wide supply voltage and clock frequency range. In the charge pump circuit the threshold voltage effect of the switch transistor is almost eliminated and the pumping efficiency of the circuit is improved. An ultra low power 192-bit memory with a register array is implemented in a 0.18 mu M standard CMOS process. The measured results indicate that, for the supply voltage of 1.2 volts and the clock frequency of 780KHz, the current consumption of the memory is 1.8 mu A (3.6 mu A) at the read (write) rate of 1.3Mb/s (0.8Kb/s).

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A low-power, highly linear, multi-standard, active-RC filter with an accurate and novel tuning architec-ture is presented. It exhibits 1EEE 802. 11a/b/g (9.5 MHz) and DVB-H (3 MHz, 4 MHz) application. The filter exploits digitally-controlled polysilicon resistor banks and a phase lock loop type automatic tuning system. The novel and complex automatic frequency calibration scheme provides better than 4 comer frequency accuracy, and it can be powered down after calibration to save power and avoid digital signal interference. The filter achieves OIP3 of 26 dBm and the measured group delay variation of the receiver filter is 50 ns (WLAN mode). Its dissipation is 3.4 mA in RX mode and 2.3 mA (only for one path) in TX mode from a 2.85 V supply. The dissipation of calibration consumes 2 mA. The circuit has been fabricated in a 0.35μm 47 GHz SiGe BiCMOS technology; the receiver and transmitter filter occupy 0.21 mm~2 and 0.11 mm~2 (calibration circuit excluded), respectively.

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A compact direct digital frequency synthesizer (DDFS) for system-on-chip implementation of the high precision rubidium atomic frequency standard is developed. For small chip size and low power consumption, the phase to sine mapping data is compressed using sine symmetry technique, sine-phase difference technique, quad line approximation technique,and quantization and error read only memory (QE-ROM) technique. The ROM size is reduced by 98% using these techniques. A compact DDFS chip with 32bit phase storage depth and a 10bit on-chip digital to analog converter has been successfully implemented using a standard 0.35μm CMOS process. The core area of the DDFS is 1.6mm^2. It consumes 167mW at 3.3V,and its spurious free dynamic range is 61dB.

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Scan test can be inserted around hard IP cores that have not been designed with DFT approaches. An 18x18 bits Booth Coding-Wallace Tree multiplier has been designed with full custom approach with 0.61 m CMOS technology. When we reuse the multiplier in another chip, scan chain has been inserted around it to increase the fault coverage. After scan insertion, the multiplier needs 4.7% more areas and 24.4% more delay time, while the fault coverage reaches to 95%.

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基于量化调制的音频水印方案以其原理简单、操纵灵活等特点,已引起人们广泛关注,但现有方案不同程度地存在鲁棒性较差等不足之处.结合音频统计均值稳定特性及同步码技术,提出了一种新的数字音频水印嵌入算法,该算法选取稳健的16位巴克码作为同步标记,通过量化音频样本统计均值嵌入同步码,同时结合听觉掩蔽特性量化低频小波系数平均值嵌入数字水印.仿真实验结果表明,本算法不仅具有较好的不可感知性,而且对常规信号处理(MP3压缩、低通滤波、添加噪声、均衡化等)和去同步攻击(随机剪切、幅度缩放、抖动等)均具有较好的鲁棒性.

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In a previous Letter [Opt. Lett. 33, 1171 (2008)], we proposed an improved logarithmic phase mask by making modifications to the original one designed by Sherif. However, further studies in another paper [Appl. Opt. 49, 229 (2010)] show that even when the Sherif mask and the improved one are optimized, their corresponding defocused modulation transfer functions (MTFs) are still not stable with respect to focus errors. So, by further modifying their phase profiles, we design another two logarithmic phase masks that exhibit more stable defocused MTF. However, with the defocus-induced phase effect considered, we find that the performance of the two masks proposed in this Letter is better than the Sherif mask, but worse than our previously proposed phase mask, according to the Hilbert space angle. (C) 2010 Optical Society of America

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In two papers [Proc. SPIE 4471, 272-280 (2001) and Appl. Opt. 43, 2709-2721 (2004)], a logarithmic phase mask was proposed and proved to be effective in extending the depth of field; however, according to our research, this mask is not that perfect because the corresponding defocused modulation transfer function has large oscillations in the low-frequency region, even when the mask is optimized. So, in a previously published paper [Opt. Lett. 33, 1171-1173 (2008)], we proposed an improved logarithmic phase mask by making a small modification. The new mask can not only eliminate the drawbacks to a certain extent but can also be even less sensitive to focus errors according to Fisher information criteria. However, the performance comparison was carried out with the modified mask not being optimized, which was not reasonable. In this manuscript, we optimize the modified logarithmic phase mask first before analyzing its performance and more convincing results have been obtained based on the analysis of several frequently used metrics. (C) 2010 Optical Society of America