996 resultados para regular replacement


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Dissertação de mestrado, Educação Especial - Domínios Cognitivo e Motor, Escola Superior de Educação e Comunicação, Universidade do Algarve, 2015

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The sum of wheat flour and corn starch was replaced by 10, 20, or 30% whole amaranth flour in both conventional (C) and reduced fat (RF) pound cakes. and the effects on physical and sensory properties of the cakes were investigated. RF presented 33% fat reduction. The increasing amaranth levels darkened crust and crumb of cakes, which decreased color acceptability. Fresh amaranth-containing cakes had similar texture characteristics to (he controls, evaluated both instrumentally and sensorially. Sensory evaluation revealed that replacement by 30% amaranth flour decreased C cakes overall acceptability scores, clue to its lower specific volume and darker color. Amaranth flour levels had no significant effect on overall acceptability of RF cakes. Hence, the sum of wheat flour and corn starch could be successfully replaced by up to 20% amaranth flour in C and up to 30% in RF pound cakes without negatively affecting sensory quality in fresh cakes. Moisture losses for all the cakes were similar, approximate to 1% per day during storage. After six days of storage, both C and RF amaranth-containing cakes had higher hardness and chewiness values than control cakes. Further experiments involving sensory evaluation during storage are necessary to determine the exact limit of amaranth flour replacement.

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Purpose: To evaluate the influence of sex, implant characteristics, and bone grafting on the survival rate of dual acid-etched (DAE) implants. Materials and Methods: Patients treated with internal-hex DAE implants for single-tooth replacement in a military dental clinic between January 2005 and December 2010 were included in this study. Clinical data related to implant characteristics, implant location, presence of grafted bone, and implant failures were collected. The primary outcome was implant loss. The survival rate was analyzed using the Kaplan-Meier method. Cox regression modeling was used to determine which factors would predict implant failure. Results: DAE implants were evaluated in a total of 988 patients (80.3% men). Twenty-four (2.4%) implants failed, most were cylindric (54.2%) with regular platforms (70.8%) and were 10 mm long (58.3%). The failure rate was 2.4% for the anterior maxilla, 3.3% for the posterior maxilla, 1.6% for the anterior mandible, and 2.0% for posterior mandible. The cumulative survival rate was 97.6%. The failure rate was 8.8% in implants placed after sinus augmentation, 7.3% in bone block-grafted areas, and 1.6% in native bone. Based on multivariable analysis (Cox regression), sinus augmentation and bone block grafting had a statistically significant effect on implant failure; the hazard ratios were 5.5 and 4.6, respectively. Conclusion: The results revealed that DAE implants had high survival rates, and no influence of sex, location, shape, diameter, or length on failure rates could be observed. However, a significant association was observed between failure and presence of bone graft in the implant area. Int J Oral Maxillofac Implants 2012;27:1243-1248

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Background Centers for Disease Control Guidelines recommend replacement of peripheral intravenous (IV) catheters every 72 to 96 hours. Routine replacement is thought to reduce the risk of phlebitis and bacteraemia. Catheter insertion is an unpleasant experience for patients and replacement may be unnecessary if the catheter remains functional and there are no signs of inflammation. Costs associated with routine replacement may be considerable. Objectives To assess the effects of removing peripheral IV catheters when clinically indicated compared with removing and re-siting the catheter routinely.

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Computer aided joint replacement surgery has become very popular during recent years and is being done in increasing numbers all over the world. The accuracy of the system depends to a major extent, on accurate registration and immobility of the tracker attachment devices to the bone. This study was designed to asses the forces needed to displace the tracker attachment devices in the bone simulators. Bone simulators were used to maintain the uniformity of the bone structure during the study. The fixation devices tested were 3mm diameter self drilling, self tapping threaded pin, 4mm diameter self tapping cortical threaded pin, 5mm diameter self tapping cancellous threaded pin and a triplanar fixation device ‘ortholock’ used with three 3mm pins. All the devices were tested for pull out, translational and rotational forces in unicortical and bicortical fixation modes. Also tested was the normal bang strength and forces generated by leaning on the devices. The forces required to produce translation increased with the increasing diameter of the pins. These were 105N, 185N, and 225N for the unicortical fixations and 130N, 200N, 225N for the bicortical fixations for 3mm, 4mm and 5mm diameter pins respectively. The forces required to pull out the pins were 1475N, 1650N, 2050N for the unicortical, 1020N, 3044N and 3042N for the bicortical fixated 3mm, 4mm and 5mm diameter pins. The ortholock translational and pull out strength was tested to 900N and 920N respectively and still it did not fail. Rotatory forces required to displace the tracker on pins was to the magnitude of 30N before failure. The ortholock device had rotational forces applied up to 135N and still did not fail. The manual leaning forces and the sudden bang forces generated were of the magnitude of 210N and 150N respectively. The strength of the fixation pins increases with increasing diameter from three to five mm for the translational forces. There is no significant difference in pull out forces of four mm and five mm diameter pins though it is more that the three mm diameter pins. This is because of the failure of material at that stage rather than the fixation device. The rotatory forces required to displace the tracker are very small and much less that that can be produced by the surgeon or assistants in single pins. Although the ortholock device was tested to 135N in rotation without failing, one has to be very careful not to put any forces during the operation on the tracker devices to ensure the accuracy of the procedure.