941 resultados para Pork processing industry
Resumo:
This chapter attempts to identify whether product differentiation or geographical differentiation is the main source of profit for firms in developing economies by employing a simple idea from the recently developed method of empirical industrial organization. Theoretically, location choice and product choice have been considered as analogues in differentiation, but in the real world, which of these strategies is chosen will result in an immense difference in firm behavior and in the development process of the industry. Development of the technique of empirical industrial organization enabled us to identify market outcomes with endogeneity. A typical case is the market outcome with differentiation, where price or product choice is endogenously determined. Our original survey contains data on market location, differences in product types, and price. The results show that product differentiation rather than geographical differentiation mitigates pressure on price competition, but 70 per cent secures geographical monopoly.
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This study tested whether contract farming or farmers professional cooperatives (FPCs) improved the social benefit of pork production and income of breeding farmers in China. The main concern of this study is whether institutional arrangement like contract farming or FPCs actually improved the welfare of farmers as expected. To answer this question accurately, we estimated the differentiated market demand of pork products in order to quantify the benefit by transaction types. Our study finds that contract farming or FPCs improved the benefits of pork products, but farmer's income remained lower than that of traditional transaction types. This finding is new in terms of quantifying distribution of the economic values among sales outlets, agro-firms and farmers. It is more reliable because it explicitly captures impacts from both demand side and supply side by structural estimation. In practice, we need to keep it mind the bargaining power of small farmers will not improve instantly even when the contract farming or FPCs are introduced.
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This thesis is a documented energy audit and long term study of energy and water reduction in a ghee factory. Global production of ghee exceeds 4 million tonnes annually. The factory in this study refines dairy products by non-traditional centrifugal separation and produces 99.9% pure, canned, crystallised Anhydrous Milk Fat (Ghee). Ghee is traditionally made by batch processing methods. The traditional method is less efficient, than centrifugal separation. An in depth systematic investigation was conducted of each item of major equipment including; ammonia refrigeration, a steam boiler, canning equipment, pumps, heat exchangers and compressed air were all fine-tuned. Continuous monitoring of electrical usage showed that not every initiative worked, others had pay back periods of less than a year. In 1994-95 energy consumption was 6,582GJ and in 2003-04 it was 5,552GJ down 16% for a similar output. A significant reduction in water usage was achieved by reducing the airflow in the refrigeration evaporative condensers to match the refrigeration load. Water usage has fallen 68% from18ML in 1994-95 to 5.78ML in 2003-04. The methods reported in this thesis could be applied to other industries, which have similar equipment, and other ghee manufacturers.
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Over the last 20 years, environmental management in Queensland has moved from the policy backwaters of government to the front line of operations by way of regulatory enforcement, industry programs and incentives. When the new Queensland Environmental Protection Act 1994 (EPA) came into effect, the business of environmental management has become a central feature of urban and rural development activity. The concept of environmentally sustainable development (ESD), has given life to the precautionary principle as a way for planners and regulators to place relevant controls on development. The planning, development and operation of pig farming systems has been effected by the new regulatory framework. Ever more definitive standards and approval permits have emerged which endeavour to achieve ESD. With these modern planning instruments in place, rural industry sectors have become, quite legitimately, concerned about future opportunities for research and innovation. This paper asserts that the capacity to engage in research and to achieve innovation in the pork producing industry is not hindered by Queensland environmental regulation frameworks. However, in order for research and innovation to prosper within these frameworks, some protocols need to be followed by the industry. What is at stake is community confidence.
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The future of the shrimp industry in India depends entirely on our export markets. Therefore the future of the industry must be related to the demand for shrimps in foreign markets. The most important market today for India is the United States. In the United States the domestic production of shrimps which was about 112 million pounds in 1950 has increased only slightly to 139.6 million pounds in 1965. However the consumption during the same period increased from 119.5 million pounds to 274.2 million pounds - the gap between home production and consumption is made up by imports.
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The wastage of prawns due to spoilage in processing factories accounted to about 0-12% in 1974, 0-35% in 1975, 0-3% in 1976 and 0-4% in 1977. Spoilage increases with the time lag between catching and processing and also due to defective icing. The paper discusses the counts of whole prawns required for obtaining meat of specified size grades.
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Quality control is defined as the continuing assessment of a current operation. It is usually the responsibility of an individual or a department directly responsible to the management. In the case of fish and fishery products, quality control includes all the steps taken to protect the quality of the material since catch until it reaches the consumer.
Resumo:
In this study, an attempt was made in order to measure and evaluate the eco-efficiency performance of a pultruded composite processing company. For this purpose the recommendations of World Business Council for Sustainable Development (WCSD) and the directives of ISO 14301 standard were followed and applied. The main general indicators of eco-efficiency, as well as the specific indicators, were defined and determined. With basis on indicators’ figures, the value profile, the environmental profile, and the pertinent eco-efficiency ratios were established and analyzed. In order to evaluate potential improvements on company eco-performance, new indicators values and eco-efficiency ratios were estimated taking into account the implementation of new proceedings and procedures, at both upstream and downstream of the production process, namely: i) Adoption of a new heating system for pultrusion die-tool in the manufacturing process, more effective and with minor heat losses; ii) Recycling approach, with partial waste reuse of scrap material derived from manufacturing, cutting and assembly processes of GFRP profiles. These features lead to significant improvements on the sequent assessed eco-efficiency ratios of the present case study, yielding to a more sustainable product and manufacturing process of pultruded GFRP profiles.
Resumo:
In this study, an attempt was made in order to measure and evaluate the eco-efficiency performance of a pultruded composite processing company. For this purpose the recommendations of World Business Council for Sustainable Development (WCSD) and the directives of ISO 14301 standard were followed and applied. The main general indicators of eco-efficiency, as well as the specific indicators, were defined and determined. With basis on indicators’ figures, the value profile, the environmental profile, and the pertinent ecoefficiency’s ratios were established and analyzed. In order to evaluate potential improvements on company eco-performance, new indicators values and eco-efficiency ratios were estimated taking into account the implementation of new proceedings and procedures, both in upstream and downstream of the production process, namely: a) Adoption of new heating system for pultrusion die in the manufacturing process, more effective and with minor heat losses; c) Recycling approach, with partial waste reuse of scrap material derived from manufacturing, cutting and assembly processes of GFRP profiles. These features lead to significant improvements on the sequent assessed eco-efficiency ratios of the present case study, yielding to a more sustainable product and manufacturing process of pultruded GFRP profiles.
Resumo:
The World Business Council for Sustainable Development (WBCSD) defines Eco-Efficiency as follows: ‘Eco- Efficiency is achieved by the delivery of competitively priced-goods and services that satisfy human needs and bring quality of life, while progressively reducing ecological impacts and resource intensity throughout the life-cycle to a level at least in line with the earth’s estimated carrying capacity’. Eco-Efficiency is under this point of view a key concept for sustainable development, bringing together economic and ecological progress. Measuring the Eco-Efficiency of a company, factory or business, is a complex process that involves the measurement and control of several and relevant parameters or indicators, globally applied to all companies in general, or specific according to the nature and specificities of the business itself. In this study, an attempt was made in order to measure and evaluate the eco-efficiency of a pultruded composite processing company. For this purpose the recommendations of WBCSD [1] and the directives of ISO 14301 standard [2] were followed and applied. The analysis was restricted to the main business branch of the company: the production and sale of standard GFRP pultrusion profiles. The main general indicators of eco-efficiency, as well as the specific indicators, were defined and determined according to ISO 14031 recommendations. With basis on indicators’ figures, the value profile, the environmental profile, and the pertinent eco-efficiency’s ratios were established and analyzed. In order to evaluate potential improvements on company eco-performance, new indicators values and ecoefficiency ratios were estimated taking into account the implementation of new proceedings and procedures, both in upstream and downstream of the production process, namely: a) Adoption of new heating system for pultrusion die in the manufacturing process, more effective and with minor heat losses; b) Implementation of new software for stock management (raw materials and final products) that minimize production failures and delivery delays to final consumer; c) Recycling approach, with partial waste reuse of scrap material derived from manufacturing, cutting and assembly processes of GFRP profiles. In particular, the last approach seems to significantly improve the eco-efficient performance of the company. Currently, by-products and wastes generated in the manufacturing process of GFRP profiles are landfilled, with supplementary added costs to this company traduced by transport of scrap, landfill taxes and required test analysis to waste materials. However, mechanical recycling of GFRP waste materials, with reduction to powdered and fibrous particulates, constitutes a recycling process that can be easily attained on heavy-duty cutting mills. The posterior reuse of obtained recyclates, either into a close-looping process, as filler replacement of resin matrix of GFRP profiles, or as reinforcement of other composite materials produced by the company, will drive to both costs reduction in raw materials and landfill process, and minimization of waste landfill. These features lead to significant improvements on the sequent assessed eco-efficiency ratios of the present case study, yielding to a more sustainable product and manufacturing process of pultruded GFRP profiles.
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Kerala was the pioneer in modern seafood processing and exporting. But now the industry is Iacingalot of problems due to low productivity and deterioration in the quality of the products. only about 17% of the installed freezing capacity in sea food processing industry was reported to be utilised during 1979-80. The price of the export commodities its decided by the buyers based on international supply and demand pattern and based on the strength and weakness of dollar/yen. The only way to increase the profitability of the processors is to reduce the cost of production to the possible extent. The individual processors find it difficult to continue in this field due to low productivity and quality problems. The main objectives of the research are to find out how the production is being managed in the seafood processing(freezing) 17industry in Kerala and the reasons for low productivity and poor quality of the products. The study includes a detailed analysis of Location of the factories. Layout Purchase, production and storage patterns. Production planning and scheduling. Work Measurement of the processing of important products. Quality Control and Inspection. Management Information System