997 resultados para LEG POWER


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Artioli, GG, Gualano, B, Franchini, E, Batista, RN, Polacow, VO, and Lancha, AH Jr. Physiological, performance, and nutritional profile of the Brazilian Olympic Wushu (kung-fu) team. J Strength Cond Res 23(1): 20-25, 2009-The purpose of the present study was to determine physiological, nutritional, and performance profiles of elite Olympic Wushu (kung-fu) athletes. Ten men and four women elite athletes took part in the study. They completed the following tests: body composition, nutritional assessment, upper-body Wingate Test, vertical jump, lumbar isometric strength, and flexibility. Blood lactate was determined at rest and after the Wingate Test. Blood lactate was also determined during a training session (combat and Taolu training). We found low body fat (men: 9.5 +/- 6.3%; women: 18.0 +/- 4.8%), high flexibility (sit-and-reach-men: 45.5 +/- 6.1 cm; women: 44.0 +/- 6.3 cm), high leg power (vertical jump-men: 37.7 +/- 8.4 cm; women: 32.3 +/- 1.1 cm), high lumbar isometric strength (men: 159 6 13 cm; women: 94 6 6 cm), moderate arm mean and peak power (Wingate Test-men: 4.1 +/- 0.4 and 5.8 +/- 0.5 W.kg(-1), respectively; women: 2.5 +/- 0.3 and 3.4 +/- 0.3 W.kg(-1), respectively), and elevated blood lactate after the Wingate Test (men: 10.8 +/- 2.0 mmol.L(-1); women: 10.2 +/- 2.0 mmol.L(-1)) and during training (combat: 12.0 +/- 1.8 mmol.L(-1); Taolu: 7.7 +/- 3.3 mmol.L(-1)). Men athletes consume a high-fat, low-carbohydrate diet, whereas women consume a moderate, high-carbohydrate diet. Energy consumption was markedly variable. In conclusion, Olympic Wushu seems to be a highly anaerobic-dependent combat sport. Low body fat, high flexibility, leg anaerobic power, isometric strength, and moderately high arm anaerobic power seem to be important for successful competitive performance.

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The aim of this study was to examine the reliability and validity of field tests for assessing physical function in mid-aged and young-old people (55–70 y). Tests were selected that required minimal space and equipment and could be implemented in multiple field settings such as a general practitioner's office. Nineteen participants completed 2 field and 1 laboratory testing sessions. Intra-class correlations showed good reliability for the tests of upper body strength (lift and reach, R= .66), lower body strength (sit to stand, R= .80) and functional capacity (Canadian Step Test, R= .92), but not for leg power (single timed chair rise, R= .28). There was also good reliability for the balance test during 3 stances: parallel (94.7% agreement), semi-tandem (73.7%), and tandem (52.6%). Comparison of field test results with objective laboratory measures found good validity for the sit to stand (cf 1RM leg press, Pearson r= .68, p< .05), and for the step test (cf PWC140, r= −.60, p< .001), but not for the lift and reach (cf 1RM bench press, r= .43, p> .05), balance (r= −.13, −.18, .23) and rate of force development tests (r= −.28). It was concluded that the lower body strength and cardiovascular function tests were appropriate for use in field settings with mid-aged and young-old adults.

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To evaluate whether a history of falls is directly related to the quadriceps muscular function and body sway, 26 elderly women were divided on the basis of the presence or absence of a history of falls. Evaluation of muscular power and anteroposterior and mediolateral displacements of center of pressure during consecutive stand and sit 5 times were performed. Fallers exhibited higher mediolateral displacement than nonfallers. No differences were observed for quadriceps power and for sit-to-stand time between groups (P<.05). The fall history was not related to the quadriceps muscular function or to the anteroposterior displacement during sit to stand.

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PURPOSE: Alpine ski performance relates closely to both anaerobic and aerobic capacities. During their competitive season, skiers greatly reduce endurance and weight training, and on-snow training becomes predominant. To typify this shift, we compared exhaustive ramp cycling and squat (SJ) and countermovement jumping (CMJ) performance in elite males before and after their competitive season. RESULTS: In postseason compared with preseason: 1) maximal oxygen uptake (VO 2 max) normalized to bodyweight was higher (55.2 +/- 5.2 vs 52.7 +/- 3.6 mL x kg(-1) x min(-1), P < 0.01), but corresponding work rate (W) was unchanged; 2) at ventilatory thresholds (VT), absolute and relative work rates were similar but heart rates were lower; 3) VO2/W slope was greater (9.59 +/- 0.6 vs 9.19 +/- 0.4 mL O2 x min(-1) x W(-1), P = 0.02), with similar flattening (P < 0.01) above V T1 at both time points; and 4) jump height was greater in SJ (47.4 +/- 4.4 vs 44.7 +/- 4.3 cm, P < 0.01) and CMJ (52.7 +/- 4.6 vs 50.4 +/- 5.0 cm, P < 0.01). DISCUSSION: We believe that aerobic capacity and leg power were constrained in preseason and that improvements primarily reflected an in-season recovery from a fatigued state, which was caused by incongruous preseason training. Residual adaptations to high-altitude exposure in preseason could have also affected the results. Nonetheless, modern alpine skiing seemingly provides an ample cardiovascular training stimulus for skiers to maintain their aerobic capacities during the racing season. CONCLUSIONS: We conclude that aerobic fitness and leg explosiveness can be maintained in-season but may be compromised by heavy or excessive preseason training. In addition, ramp test V O2/W slope analysis could be useful for monitoring both positive and negative responses to training.

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Objetivo: Determinar la distribución por percentiles de salto con contramovimiento (CMJ) en una población escolar de Bogotá, Colombia, perteneciente al estudio Fuprecol. Métodos: Estudio transversal realizado entre 2846 niños y 2754 adolescentes, entre 9 a 17 años de edad, pertenecientes a 18 instituciones educativas oficiales de Bogotá, Colombia. Se evaluó el CMJ, de acuerdo, con lo establecido por la batería de condición física, Fuprecol. Se calcularon, los percentiles (P3, P10, P25, P50, P75, P90 y P97), y curvas centiles por el método LMS, según su sexo y edad. Se realizó una comparación entre los valores de la CMJ observados con estándares internacionales. Resultados: La muestra estuvo constituida por 5.600 niños y adolescentes entre 9 y 17 años; el promedio de edad fue 12,6 ± 2,4 años. En el CMJ, los valores altos, los obtuvieron los niños, franja en la que la media osciló entre 25,1 cm a los 9 años, y 38,6 cm a los 17; para las niñas, la media fluctuó entre 23,2 cm a los 9 años, y 28,6 a los 17; en ambos sexos esos valores aumentan proporcional a la edad. Conclusiones: Se registran percentiles del CMJ de acuerdo con la edad y el sexo, que podrán ser usados como referencia en la evaluación del salto vertical desde edades tempranas.

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El propósito del presente estudio era generar los valores normativos de salto largo para niños de 9-17.9 años, e investigar las diferencias de sexo y grupo de edad

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Strength of leg peference and interlateral asymmetry in kinematics of kicking a ball for power were assessed in 6- to 10-year-old right-footed soccer player children. Leg preference was evaluated separately for three task categories: balance stabilization, soccer related mobilization, and general mobilization. The results showed that while both categories of mobilization tasks were featured by a consistent preference for the right leg, in stabilization tasks we observed lower scores and greater interindividual variability of leg preference. No effect of age was detected on leg preference. Analysis of peak foot velocity revealed similar increment of performance of the right and left legs from the ages 6-8 to 10 years. This finding supports the notion of stable Magnitude of interlateral asymmetries of performance during motor development. (C) 2008 Wiley Periodicals, Inc. Dev Psychobiol 50: 799-806, 2008.

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The aim of this study was to test if the critical power model can be used to determine the critical rest interval (CRI) between vertical jumps. Ten males performed intermittent countermovement jumps on a force platform with different resting periods (4.1 +/- 0.3 s, 5.0 +/- 0.4 s, 5.9 +/- 0.6 s). Jump trials were interrupted when participants could no longer maintain 95% of their maximal jump height. After interruption, number of jumps, total exercise duration and total external work were computed. Time to exhaustion (s) and total external work (J) were used to solve the equation Work = a + b . time. The CRI (corresponding to the shortest resting interval that allowed jump height to be maintained for a long time without fatigue) was determined dividing the average external work needed to jump at a fixed height (J) by b parameter (J/s). in the final session, participants jumped at their calculated CRI. A high coefficient of determination (0.995 +/- 0.007) and the CRI (7.5 +/- 1.6 s) were obtained. In addition, the longer the resting period, the greater the number of jumps (44 13, 71 28, 105 30, 169 53 jumps; p<0.0001), time to exhaustion (179 +/- 50, 351 +/- 120, 610 +/- 141, 1,282 +/- 417 s; p<0.0001) and total external work (28.0 +/- 8.3, 45.0 +/- 16.6, 67.6 +/- 17.8, 111.9 +/- 34.6 kJ; p<0.0001). Therefore, the critical power model may be an alternative approach to determine the CRI during intermittent vertical jumps.

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Ide, BN, Leme, TCF, Lopes, CR, Moreira, A, Dechechi, CJ, Sarraipa, MF, da Mota, GR, Brenzikofer, R, and Macedo, DV. Time course of strength and power recovery after resistance training with different movement velocities. J Strength Cond Res 25(7): 2025-2033, 2011-The purpose of this study was to evaluate the time course of strength and power recovery after a single bout of strength training designed with fast and slow contraction velocities. Nineteen male subjects were randomly divided into 2 groups: the slow-velocity contraction (SV) group and the fast velocity contraction (FV) group. Resistance training protocols consisted of 5 sets of 12 repetition maximum (5 x 12RM) with 50 seconds of rest between sets and 2 minutes between exercises. Contraction velocity was controlled by the execution time for each repetition (SV-6 seconds to complete concentric and eccentric phases and for FV-1.5 seconds). Leg Press 45 degrees 1RM (LP 1RM), horizontal countermovement jump (HCMJ), and right thigh circumference (TC) were accessed in 6 distinct moments: base (1 week before exercise), 0 (immediately after exercises), 24, 48, 72, and 96 hours after exercise protocol. The SV and FV presented significant LP 1RM decrements at 0, and these were still evident 24-48 hours postexercise. The magnitude of decline was significantly (p<0.05) higher for FV. The SV and FV presented significant HCMJ decrements at 0, but only for FV were these still evident 24-72 hours postexercise. The SV and FV presented significant TC increments at 0, and these were still evident 24-48 hours postexercise for SV but for FV it continued up to 96 hours. The magnitude of increase was significantly (p<0.05) higher for FV. In conclusion, the fast contraction velocity protocol resulted in greater decreases in LP 1RM and HCMJ performance, when compared with slow velocity. The results lead us to interpret that this variable may exert direct influence on acute muscle strength and power generation capacity.

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Abad, CCC, Prado, ML, Ugrinowitsch, C, Tricoli, V, and Barroso, R. Combination of general and specific warm-ups improves leg-press one repetition maximum compared with specific warm-up in trained individuals. J Strength Cond Res 25(8): 2242-2245, 2011-Accurate assessment of muscular strength is critical for exercise prescription and functional evaluation. The warm-up protocol may affect the precision of the 1 repetition maximum (1RM) test. Testing guidelines recommend performing both general and specific warm-ups before strength tests. The general warm-up intends to raise muscle temperature, whereas the specific warm-up aims to increase neuromuscular activation. Although there is scientific evidence for performing the specific warm-up, the effects of general warm-up on strength tests are still unclear. The purpose of this study was to investigate whether the combination of a general with a specific warm-up (G + SWU) protocol would improve leg press 1RM values compared with a specific warm-up (SWU) protocol. Thirteen participants were tested for leg-press 1RM under 2 warm-up conditions. In the first condition, participants performed the SWU only, which was composed of 1 set of 8 repetitions at approximately 50% of the estimated 1RM followed by another set of 3 repetitions at 70% of the estimated 1RM. In the second condition (G + SWU), participants performed the 1RM test after a 20-minute general warm-up on a stationary bicycle at 60% of HRmax and the same specific warm-up as in the SWU. Values of 1RM in SWU and in G + SWU were compared by a paired t-test, and significance level was set at p <= 0.05. Strength values were on average 8.4% (p = 0.002) higher in the G + SWU compared with the SWU. These results suggest that the G + SWU induced temperature-dependent neuromuscular adjustments that increased muscle force production capacity. Therefore, these results support the recommendations of the testing guidelines to perform a moderate intensity general warm-up in addition to the specific warm-up before maximum strength assessments.

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This doctoral thesis introduces an improved control principle for active du/dt output filtering in variable-speed AC drives, together with performance comparisons with previous filtering methods. The effects of power semiconductor nonlinearities on the output filtering performance are investigated. The nonlinearities include the timing deviation and the voltage pulse waveform distortion in the variable-speed AC drive output bridge. Active du/dt output filtering (ADUDT) is a method to mitigate motor overvoltages in variable-speed AC drives with long motor cables. It is a quite recent addition to the du/dt reduction methods available. This thesis improves on the existing control method for the filter, and concentrates on the lowvoltage (below 1 kV AC) two-level voltage-source inverter implementation of the method. The ADUDT uses narrow voltage pulses having a duration in the order of a microsecond from an IGBT (insulated gate bipolar transistor) inverter to control the output voltage of a tuned LC filter circuit. The filter output voltage has thus increased slope transition times at the rising and falling edges, with an opportunity of no overshoot. The effect of the longer slope transition times is a reduction in the du/dt of the voltage fed to the motor cable. Lower du/dt values result in a reduction in the overvoltage effects on the motor terminals. Compared with traditional output filtering methods to accomplish this task, the active du/dt filtering provides lower inductance values and a smaller physical size of the filter itself. The filter circuit weight can also be reduced. However, the power semiconductor nonlinearities skew the filter control pulse pattern, resulting in control deviation. This deviation introduces unwanted overshoot and resonance in the filter. The controlmethod proposed in this thesis is able to directly compensate for the dead time-induced zero-current clamping (ZCC) effect in the pulse pattern. It gives more flexibility to the pattern structure, which could help in the timing deviation compensation design. Previous studies have shown that when a motor load current flows in the filter circuit and the inverter, the phase leg blanking times distort the voltage pulse sequence fed to the filter input. These blanking times are caused by excessively large dead time values between the IGBT control pulses. Moreover, the various switching timing distortions, present in realworld electronics when operating with a microsecond timescale, bring additional skew to the control. Left uncompensated, this results in distortion of the filter input voltage and a filter self-induced overvoltage in the form of an overshoot. This overshoot adds to the voltage appearing at the motor terminals, thus increasing the transient voltage amplitude at the motor. This doctoral thesis investigates the magnitude of such timing deviation effects. If the motor load current is left uncompensated in the control, the filter output voltage can overshoot up to double the input voltage amplitude. IGBT nonlinearities were observed to cause a smaller overshoot, in the order of 30%. This thesis introduces an improved ADUDT control method that is able to compensate for phase leg blanking times, giving flexibility to the pulse pattern structure and dead times. The control method is still sensitive to timing deviations, and their effect is investigated. A simple approach of using a fixed delay compensation value was tried in the test setup measurements. The ADUDT method with the new control algorithm was found to work in an actual motor drive application. Judging by the simulation results, with the delay compensation, the method should ultimately enable an output voltage performance and a du/dt reduction that are free from residual overshoot effects. The proposed control algorithm is not strictly required for successful ADUDT operation: It is possible to precalculate the pulse patterns by iteration and then for instance store them into a look-up table inside the control electronics. Rather, the newly developed control method is a mathematical tool for solving the ADUDT control pulses. It does not contain the timing deviation compensation (from the logic-level command to the phase leg output voltage), and as such is not able to remove the timing deviation effects that cause error and overshoot in the filter. When the timing deviation compensation has to be tuned-in in the control pattern, the precalculated iteration method could prove simpler and equally good (or even better) compared with the mathematical solution with a separate timing compensation module. One of the key findings in this thesis is the conclusion that the correctness of the pulse pattern structure, in the sense of ZCC and predicted pulse timings, cannot be separated from the timing deviations. The usefulness of the correctly calculated pattern is reduced by the voltage edge timing errors. The doctoral thesis provides an introductory background chapter on variable-speed AC drives and the problem of motor overvoltages and takes a look at traditional solutions for overvoltage mitigation. Previous results related to the active du/dt filtering are discussed. The basic operation principle and design of the filter have been studied previously. The effect of load current in the filter and the basic idea of compensation have been presented in the past. However, there was no direct way of including the dead time in the control (except for solving the pulse pattern manually by iteration), and the magnitude of nonlinearity effects had not been investigated. The enhanced control principle with the dead time handling capability and a case study of the test setup timing deviations are the main contributions of this doctoral thesis. The simulation and experimental setup results show that the proposed control method can be used in an actual drive. Loss measurements and a comparison of active du/dt output filtering with traditional output filtering methods are also presented in the work. Two different ADUDT filter designs are included, with ferrite core and air core inductors. Other filters included in the tests were a passive du/dtfilter and a passive sine filter. The loss measurements incorporated a silicon carbide diode-equipped IGBT module, and the results show lower losses with these new device technologies. The new control principle was measured in a 43 A load current motor drive system and was able to bring the filter output peak voltage from 980 V (the previous control principle) down to 680 V in a 540 V average DC link voltage variable-speed drive. A 200 m motor cable was used, and the filter losses for the active du/dt methods were 111W–126 W versus 184 W for the passive du/dt. In terms of inverter and filter losses, the active du/dt filtering method had a 1.82-fold increase in losses compared with an all-passive traditional du/dt output filter. The filter mass with the active du/dt method was 17% (2.4 kg, air-core inductors) compared with 14 kg of the passive du/dt method filter. Silicon carbide freewheeling diodes were found to reduce the inverter losses in the active du/dt filtering by 18% compared with the same IGBT module with silicon diodes. For a 200 m cable length, the average peak voltage at the motor terminals was 1050 V with no filter, 960 V for the all-passive du/dt filter, and 700 V for the active du/dt filtering applying the new control principle.

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The aim of the present study was to verify the applicability of anaerobic work capacity (AWC) determined from the critical power model in elite table tennis players. Eight male international level table tennis players participated in the study. The tests undertaken were: 1) A critical frequency test used to determinate the anaerobic work capacity; 2) Wingate tests were performed using leg and arm ergometers. AWC corresponded to 99.5 +/- 29.1 table tennis balls. AWC was not related to peak (r = -0.25), mean (r = -0.02), relative peak (r = -0.49) or relative mean power (r = 0.01), nor fatigue index (r = -0.52) (Wingate leg ergometer). Similar correlations for peak (r = -0.34), mean (r = -0.04), relative peak (r = -0.49), relative mean power (r = -0.14) and peak blood lactate concentration (r = -0.08) were determined in the Wingate arm ergometer test. Based on these results the AWC determined by a modified critical power test was not a good index for measurement of anaerobic capacity in table tennis players.

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This paper presents an improved analysis of a novel Programmable Power-factor-corrected-Based Hybrid Multipulse Power Rectifier (PFC-HMPR) for utility interface of power electronic converters. The proposed hybrid multipulse rectifier is composed of an ordinary three-phase six-pulse diode-bridge rectifier (Graetz bridge) with a parallel connection of single-phase switched converters in each three-phase rectifier leg. In this paper, the authors present a complete discussion about the controlled rectifiers' power contribution and also a complete analysis concerning the total harmonic distortion of current that can be achieved when the proposed converter operates as a conventional 12-pulse rectifier. The mathematical analysis presented in this paper corroborate, with detailed equations, the experimental results of two 6-kW prototypes implemented in a laboratory.

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A novel hybrid three-phase rectifier is proposed. It is capable to achieve high input power factor (PF) and low total harmonic input currents distortion (THDI). The proposed hybrid high power rectifier is composed by a standard three-phase six-pulse diode rectifier (Graetz bridge) with a parallel connection of single-phase Sepic rectifiers in each three-phase rectifier leg. Such topology results in a structure capable of programming the input current waveform and providing conditions for obtaining high input power factor and low harmonic current distortion. In order to validate the proposed hybrid rectifier, this work describes its principles, with detailed operation, simulation, experimental results, and discussions on power rating of the required Sepic converters as related to the desired total harmonic current distortion. It is demonstrated that only a fraction of the output power is processed through the Sepic converters, making the proposed solution economically viable for very high power installations, with fast investment payback. Moreover, retrofitting to existing installations is also feasible since the parallel path can be easily controlled by integration with the existing dc-link. A prototype has been implemented in the laboratory and it was fully demonstrated to both operate with excellent performance and be feasibly implemented in higher power applications.

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A novel hybrid high power rectifier capable to achieve unity power factor is proposed in this paper. Single-phase SEPIC rectifiers are associated in parallel with each leg of three-phase 6-pulse diode rectifier resulting in a programmable input current waveform structure. In this paper it is described the principles of operation of the proposed converter with detailed simulation and experimental results. For a total harmonic distortion of the input line current (THDI) less than 2% the rated power of the SEPIC rectifiers is 33%. Therefore, power rating of the SEPIC parallel converters is a fraction of the output power, on the range of 20% to 33% of the nominal output power, making the proposed solution economically viable for high power installations, with fast pay back of the investment. Moreover, retrofits to existing installations are also possible with this proposed topology, since the parallel path can be easily controlled by integration with the already existing de-link. Experimental results are presented for a 3 kW implemented prototype, in order to verify the developed analysis.