958 resultados para wear-resistant steel


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Recent reports have indicated that 23.5% of the nation's highway bridges are structurally deficient and 17.7% are functionally obsolete. A significant number of these bridges are on the Iowa secondary road system where over 86% of the rural bridge management responsibilities are assigned to the counties. Some of the bridges can be strengthened or otherwise rehabilitated, but many more are in need of immediate replacement. In a recent investigation (HR-365 "Evaluation of Bridge Replacement Alternatives for the County Bridge System") several types of replacement bridges that are currently being used on low volume roads were identified. It was also determined that a large number of counties (69%) have the ability and are interested in utilizing their own forces to design and construct short span bridges. In reviewing the results from HR-365, the research team developed one "new" bridge replacement concept and a modification of a replacement system currently being used. Both of these bridge replacement alternatives were investigated in this study, the results of which are presented in two volumes. This volume (Volume 1) presents the results of Concept 1 - Steel Beam Precast Units. Concept 2 - Modification of the Beam-in-Slab Bridge is presented in Volume 2. Concept 1, involves the fabrication of precast units (two steel beams connected by a concrete slab) by county work forces. Deck thickness is limited so that the units can be fabricated at one site and then transported to the bridge site where they are connected and the remaining portion of the deck placed. Since Concept 1 bridge is primarily intended for use on low-volume roads, the precast units can be constructed with new or used beams. In the experimental part of the investigation, there were three types of static load tests: small scale connector tests, "handling strength" tests, and service and overload tests of a model bridge. Three finite element models for analyzing the bridge in various states of construction were also developed. Small scale connector tests were completed to determine the best method of connecting the precast double-T (PCDT) units. "Handling strength" tests on an individual PCDT unit were performed to determine the strength and behavior of the precast unit in this configuration. The majority of the testing was completed on the model bridge [L=9,750 mm (32 ft), W=6,400 mm (21 ft)] which was fabricated using the precast units developed. Some of the variables investigated in the model bridge tests were number of connectors required to connect adjacent precast units, contribution of diaphragms to load distribution, influence of position of diaphragms on bridge strength and load distribution, and effect of cast-in-place portion of deck on load distribution. In addition to the service load tests, the bridge was also subjected to overload conditions. Using the finite element models developed, one can predict the behavior and strength of bridges similar to the laboratory model as well as design them. Concept 1 has successfully passed all laboratory testing; the next step is to field test it.

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This project continues the research which addresses the numerous bridge problems on the Iowa secondary road system. It is a continuation (Phase 2) of Project HR-382, in which two replacement alternatives (Concept 1: Steel Beam Precast Units and Concept 2: Modification of the Benton County Beam-in-Slab Bridge) were investigated. In previous research for concept 1, a precast unit bridge was developed through laboratory testing. The steel-beam precast unit bridge requires the fabrication of precast double-tee (PCDT) units, each consisting of two steel beams connected by a reinforced concrete deck. The weight of each PCDT unit is minimized by limiting the deck thickness to 4 in., which permits the units to be constructed off-site and then transported to the bridge site. The number of units required is a function of the width of bridge desired. Once the PCDT units are connected, a cast-in-place reinforced concrete deck is cast over the PCDT units and the bridge railing attached. Since the steel beam PCDT unit bridge design is intended primarily for use on low-volume roads, used steel beams can be utilized for a significant cost savings. In previous research for concept 2, an alternate shear connector (ASC) was developed and subjected to static loading. In this investigation, the ASC was subjected to cyclic loading in both pushout specimens and composite beam tests. Based on these tests, the fatigue strength of the ASC was determined to be significantly greater than that required in typical low volume road single span bridges. Based upon the construction and service load testing, the steel-beam precast unit bridge was successfully shown to be a viable low volume road bridge alternative. The construction process utilized standard methods resulting in a simple system that can be completed with a limited staff. Results from the service load tests indicated adequate strength for all legal loads. An inspection of the bridge one year after its construction revealed no change in the bridge's performance. Each of the systems previously described are relatively easy to construct. Use of the ASC rather than the welded studs significantly simplified the work, equipment, and materials required to develop composite action between the steel beams and the concrete deck.

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This report presents the results of surveys to determine studded tire usage in Iowa. Also reported are the results of measurements of transverse pavement profiles at selected locations where the pavement is subjected to a high volume of traffic. The surveys were made in January of each of the years 1969 through 1978 and in each of 27 areas into which the state was divided. Estimates of studded tire usage were also made at various locations on Interstate highways in Iowa. The lowest percentage of studded tires was observed in the initial count during the winter of 1968-69. Two years later the percentage had increased to the maximum (22.6%) and then began a gradual decline. The latest count in January of 1978 indicated 8.5% of the cars had studded tires. The decline in the use of studded tires is attributed to the efforts of the Iowa DOT and others to obtain a ban on studded tires and a continual increase in the use of radial tires with claims of improved traction. The wear measurements were recorded by camera. It was found that studded tires have worn ruts in Iowa pavements as deep as 5/16 inch. The ruts lead to water on the pavement and this causes hydroplaning, as well as splash and spray. The conclusion of the study was that studded tires should be banned in Iowa.

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The need to upgrade a large number of understrength and obsolete bridges in the U.S. has been well documented in the literature. Through several Iowa DOT projects, the concept of strengthening simple-span bridges by post-tensioning has been developed. The purpose of the project described in this report was to investigate the use of post-tensioning for strengthening continuous composite bridges. In a previous, successfully completed investigation, the feasibility of strengthening continuous, composite bridges by post-tensioning was demonstrated on a laboratory 1/3-scale-model bridge (3 spans: 41 ft 11 in. x 8 ft 8 in.). This project can thus be considered the implementation phase. The bridge selected for strengthening was in Pocahontas County near Fonda, Iowa, on County Road N28. With finite element analysis, a post-tensioning system was developed that required post-tensioning of the positive moment regions of both the interior and exterior beams. During the summer of 1988, the strengthening system was installed along with instrumentation to determine the bridge's response and behavior. Before and after post-tensioning, the bridge was subjected to truck loading (1 or 2 trucks at various predetermined critical locations) to determine the effectiveness of the strengthening system. The bridge, with the strengthening system in place, was inspected approximately every three months to determine any changes in its appearance or behavior. In 1989, approximately one year after the initial strengthening, the bridge was retested to identify any changes in its behavior. Post-tensioning forces were removed to reveal any losses over the one-year period. Post-tensioning was reapplied to the bridge, and the bridge was tested using the same loading program used in 1988. Except for at a few locations, stresses were reduced in the bridge the desired amount. At a few locations flexural stresses in the steel beams are still above 18 ksi, the allowable inventory stress for A7 steel. Although maximum stresses are above the inventory stress by about 2 ksi, they are about 5 ksi below the allowable operating stress; therefore, the bridge no longer needs to be load-posted.

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The Phase I research, Iowa Department of Transportation (IDOT) Project HR-214, "Feasibility Study of Strengthening Existing Single Span Steel Beam Concrete Deck Bridges," verified that post-tensioning can be used to provide strengthening of the composite bridges under investigation. Phase II research, reported here, involved the strengthening of two full-scale prototype bridges - one a prototype of the model bridge tested during Phase I and the other larger and skewed. In addition to the field work, Phase II also involved a considerable amount of laboratory work. A literature search revealed that only minimal data existed on the angle-plus-bar shear connectors. Thus, several specimens utilizing angle-plus-bar, as well as channels, studs and high strength bolts as shear connectors were fabricated and tested. To obtain additional shear connector information, the bridge model of Phase I was sawed into four composite concrete slab and steel beam specimens. Two of the resulting specimens were tested with the original shear connection, while the other two specimens had additional shear connectors added before testing. Although orthotropic plate theory was shown in Phase I to predict vertical load distribution in bridge decks and to predict approximate distribution of post-tensioning for right-angle bridges, it was questioned whether the theory could also be used on skewed bridges. Thus, a small plexiglas model was constructed and used in vertical load distribution tests and post-tensioning force distribution tests for verification of the theory. Conclusions of this research are as follows: (1) The capacity of existing shear connectors must be checked as part of a bridge strengthening program. Determination of the concrete deck strength in advance of bridge strengthening is also recommended. (2) The ultimate capacity of angle-plus-bar shear connectors can be computed on the basis of a modified AASHTO channel connector formula and an angle-to-beam weld capacity check. (3) Existing shear connector capacity can be augmented by means of double-nut high strength bolt connectors. (4) Post-tensioning did not significantly affect truck load distribution for right angle or skewed bridges. (5) Approximate post-tensioning and truck load distribution for actual bridges can be predicted by orthotropic plate theory for vertical load; however, the agreement between actual distribution and theoretical distribution is not as close as that measured for the laboratory model in Phase I. (6) The right angle bridge exhibited considerable end restraint at what would be assumed to be simple support. The construction details at bridge abutments seem to be the reason for the restraint. (7) The skewed bridge exhibited more end restraint than the right angle bridge. Both skew effects and construction details at the abutments accounted for the restraint. (8) End restraint in the right angle and skewed bridges reduced tension strains in the steel bridge beams due to truck loading, but also reduced the compression strains caused by post-tensioning.

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The unifying objective of Phases I and II of this study was to determine the feasibility of the post-tensioning strengthening method and to implement the technique on two composite bridges in Iowa. Following completion of these two phases, Phase III was undertaken and is documented in this report. The basic objectives of Phase III were further monitoring bridge behavior (both during and after post-tensioning) and developing a practical design methodology for designing the strengthening system under investigation. Specific objectives were: to develop strain and force transducers to facilitate the collection of field data; to investigate further the existence and effects of the end restraint on the post-tensioning process; to determine the amount of post-tensioning force loss that occurred during the time between the initial testing and the retesting of the existing bridges; to determine the significance of any temporary temperature-induced post-tensioning force change; and to develop a simplified design methodology that would incorporate various variables such as span length, angle-of-skew, beam spacing, and concrete strength. Experimental field results obtained during Phases II and III were compared to the theoretical results and to each other. Conclusions from this research are as follows: (1) Strengthening single-span composite bridges by post-tensioning is a viable, economical strengthening technique. (2) Behavior of both bridges was similar to the behavior observed from the bridges during field tests conducted under Phase II. (3) The strain transducers were very accurate at measuring mid-span strain. (4) The force transducers gave excellent results under laboratory conditions, but were found to be less effective when used in actual bridge tests. (5) Loss of post-tensioning force due to temperature effects in any particular steel beam post-tensioning tendon system were found to be small. (6) Loss of post-tensioning force over a two-year period was minimal. (7) Significant end restraint was measured in both bridges, caused primarily by reinforcing steel being continuous from the deck into the abutments. This end restraint reduced the effectiveness of the post-tensioning but also reduced midspan strains due to truck loadings. (8) The SAP IV finite element model is capable of accurately modeling the behavior of a post-tensioned bridge, if guardrails and end restraints are included in the model. (9) Post-tensioning distribution should be separated into distributions for the axial force and moment components of an eccentric post-tensioning force. (10) Skews of 45 deg or less have a minor influence on post-tensioning distribution. (11) For typical Iowa three-beam and four-beam composite bridges, simple regression-derived formulas for force and moment fractions can be used to estimate post-tensioning distribution at midspan. At other locations, a simple linear interpolation gives approximately correct results. (12) A simple analytical model can accurately estimate the flexural strength of an isolated post-tensioned composite beam.

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The need to upgrade understrength bridges in the United States has been well documented in the literature. The concept of strengthening steel stringer bridges in Iowa has been developed through several Iowa DOT projects. The objective of the project described in this report was to investigate the use of one such strengthening system on a three-span continuous steel stringer bridge in the field. In addition, a design methodology was developed to assist bridge engineers with designing a strengthening system to obtain the desired stress reductions. The bridge selected for strengthening was in Cerro Gordo County near Mason City, Iowa on County Road B65. The strengthening system was designed to remove overstresses that occurred when the bridge was subjected to Iowa legal loads. A two part strengthening system was used: post-tensioning the positive moment regions of all the stringers and superimposed trusses in the negative moment regions of the two exterior stringers at the two piers. The strengthening system was installed in the summers of 1992 and 1993. In the summer of 1993, the bridge was load tested before and after the strengthening system was activated. The load test results indicate that the strengthening system was effective in reducing the overstress in both the negative and positive regions of the stringers. The design methodology that was developed includes a procedure for determining the magnitude of post-tensioning and truss forces required to strengthen a given bridge. This method utilizes moment and force fractions to determine the distribution of strengthening axial forces and moments throughout the bridge. Finite element analysis and experimental results were used in the formulation and calibration of the methodology. A spreadsheet was developed to facilitate the calculation of these required strengthening forces.

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Some of the Iowa Department of Transportation (Iowa DOT) continuous, steel, welded plate girder bridges have developed web cracking in the negative moment regions at the diaphragm connection plates. The cracks are due to out-of-plane bending of the web near the top flange of the girder. The out-of-plane bending occurs in the "web-gap", which is the portion of the girder web between (1) the top of the fillet welds attaching the diaphragm connection plate to the web and (2) the fillet welds attaching the flange to the web. A literature search indicated that four retrofit techniques have been suggested by other researchers to prevent or control this type of cracking. To eliminate the problem in new bridges, AASHTO specifications require a positive attachment between the connection plate and the top (tension) flange. Applying this requirement to existing bridges is expensive and difficult. The Iowa DOT has relied primarily on the hole-drilling technique to prevent crack extension once cracking has occurred; however, the literature indicates that hole-drilling alone may not be entirely effective in preventing crack extension. The objective of this research was to investigate experimentally a method proposed by the Iowa DOT to prevent cracking at the diaphragm/plate girder connection in steel bridges with X-type or K-type diaphragms. The method consists of loosening the bolts at some connections between the diaphragm diagonals and the connection plates. The investigation included selecting and testing five bridges: three with X-type diaphragms and two with K-type diaphragms. During 1996 and 1997, these bridges were instrumented using strain gages and displacement transducers to obtain the response at various locations before and after implementing the method. Bridges were subjected to loaded test trucks traveling in different lanes with speeds varying from crawl speed to 65 mph (104 km/h) to determine the effectiveness of the proposed method. The results of the study show that the effect of out-of-plane loading was confined to widths of approximately 4 in. (100 mm) on either side of the connection plates. Further, they demonstrate that the stresses in gaps with drilled holes were higher than those in gaps without cracks, implying that the drilling hole technique is not sufficient to prevent crack extension. The behavior of the web gaps in X-type diaphragm bridges was greatly enhanced by the proposed method as the stress range and out-of-plane distortion were reduced by at least 42% at the exterior girders. For bridges with K-type diaphragms, a similar trend was obtained. However, the stress range increased in one of the web gaps after implementing the proposed method. Other design aspects (wind, stability of compression flange, and lateral distribution of loads) must be considered when deciding whether to adopt the proposed method. Considering the results of this investigation, the proposed method can be implemented for X-type diaphragm bridges. Further research is recommended for K-type diaphragm bridges.

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Glucagon-like peptide-1(7-37) (GLP-1) is the most potent insulinotropic hormone characterized thus far. Because its activity is preserved in non-insulin-dependent diabetes mellitus (NIDDM) patients, it is considered a potential new drug for the treatment of this disease. One limitation in its therapeutic use is a short half-life in vivo (5 minutes), due in part to a fast degradation by the endoprotease dipeptidylpeptidase IV (DPPIV). Recently, it was reported that GLP-1 became resistant to DPPIV when the alanine residue at position 8 was replaced by a glycine (GLP-1-Gly8). We report here that this change slightly decreased the affinity of the peptide for its receptor (IC50, 0.41 +/- 0.14 and 1.39 +/- 0.61 nmol/L for GLP-1 and GLP-1-Gly8, respectively) but did not change the efficiency to stimulate accumulation of intracellular cyclic adenosine monophosphate (cAMP) (EC50, 0.25 +/- 0.05 and 0.36 +/- 0.06 nmol/L for GLP-1 and GLP-1-Gly8, respectively). Second, we demonstrate for the first time that this mutant has an improved insulinotropic activity compared with the wild-type peptide when tested in vivo in an animal model of diabetes. A single injection of 0.1 nmol GLP-1-Gly8 in diabetic mice fed a high-fat diet can correct fasting hyperglycemia and glucose intolerance for several hours, whereas the activity of 1 nmol GLP-1 vanishes a few minutes after injection. These actions were correlated with increased insulin and decreased glucagon levels. Interestingly, normoglycemia was maintained over a period that was longer than the predicted peptide half-life, suggesting a yet undescribed long-term effect of GLP-1-Gly8. GLP-1-Gly8 thus has a markedly improved therapeutic potential compared with GLP-1, since it can be used at much lower doses and with a more flexible schedule of administration.

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Rapid production of IL-4 by Leishmania homolog of mammalian RACK1 (LACK)-reactive CD4(+) T cells expressing the V beta 4-V alpha 8 TCR chains has been shown to drive aberrant Th2 cell development and susceptibility to Leishmania major in BALB/c mice. In contrast, mice from resistant strains fail to express this early IL-4 response. However, administration of either anti-IL-12 or -IFN-gamma at the initiation of infection allows the expression of this early IL-4 response in resistant mice. In this work we show that Leishmania homolog of mammalian RACK1-reactive CD4(+) T cells also expressing the V beta 4-V alpha 8 TCR chains are the source of the early IL-4 response to L. major in resistant mice given anti-IL-12 or -IFN-gamma Abs only at the onset of infection. Strikingly, these cells were found to be required for the reversal of the natural resistance of C57BL/6 mice following a single administration of anti-IL-12 or -IFN-gamma Abs. Together these results suggest that a deficiency in mechanisms capable of down-regulating the early IL-4 response to L. major contributes to the exquisite susceptibility of BALB/c mice to L. major.

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The degree of blast resistance of upland rice (Oryza sativa L.) cultivar Araguaia has decreased over time causing significant yield losses. The major objective of this study was to obtain blast (Pyricularia grisea) resistant somaclones, adapting greenhouse and field selection procedures. Rice blast resistance and agronomic traits were assessed in R2 to R6 generations derived from regenerant plants (R1) from immature panicles of Araguaia. The evaluation and selection procedures include testing of early segregating populations and fixed lines in the advanced generations, under natural field conditions, and artificial inoculations in the greenhouse, with prevalent races IB-1 and IB-9 of P. grisea. Somaclones with both vertical resistance and slow blasting resistance were obtained. Twenty of 31 somaclones developed with a high degree of vertical resistance and fan shaped plant type maintained resistance in field and blast nursery tests in the R6 generation. Greenhouse selection with two specific physiologic races yielded 44 somaclones with slow blasting resistance, similar plant type and yield potential as that of Araguaia.

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The nose is the anatomical site usually recommended for methicillin-resistant Staphylococcus aureus (MRSA) screening. Other sites are also recommended, but are more controversial. We showed that the sensitivities of MRSA detection from nasal swabs alone were 48% and 62% by culture or by rapid PCR test, respectively. These percentages increased to 79% and 92% with the addition of groin swabs, and to 96% and 99% with the addition of groin and throat swabs. In conclusion, neither by culture nor by rapid PCR test is nose sampling alone sufficient for MRSA detection. Additional anatomical sites should include at least the groin and throat.

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Two composite, prestressed, steel beams, fabricated by slightly different methods, were fatigue tested to destruction. Stresses and deflections were measured at regular intervals, and the behavior of each beam as failure progressed was recorded. Residual stresses were then evaluated by testing segments of each beam. An attempt was made to assess the effects of the residual stresses on fatigue strength.

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The penetration of chloride ions from deicing salts into the portland cement concrete of bridge decks can cause corrosion and serious damage to the reinforcing steel. Concrete properties which prevent chloride penetration into the bridge deck and provide a good structural and economic wearing surface are desirable. A variety of mix designs have been tried in the past in search of improved performance and lower costs for bridge deck overlay concrete. A group of mixes with various designs have been tested in this project and results are being compared to determine which concrete mix appears to be the most cost effective and resistant to chloride penetration for bridge deck overlay use.

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Purpose: Polyethylene wear is a recurrent problem in joint arthroplasty. Small debris particles are also associated to inflammation reaction of the surrounding bone, eventually leading to the failure of the bound between the implant and the host bone, and implant loosening. The goal of this study was thus to estimate the volume of polyethylene wear of a reversed prosthesis, and compare it to an anatomic prosthesis, during one year of activities of daily living. Material and Methods: A numerical musculoskeletal model of the glenohumeral joint was used for this comparative study. The reversed (RP) and anatomic (AP) Aequalis prostheses were positioned in the numerical model. Eight levels of abduction were considered. Their daily frequency was estimated from in-vivo recorded data on healthy volunteers during activities of daily living. One year of use was simulated to predict the linear and volumetric wear. The volumetric wear was the difference of volume between the original and worn component. Results: With the AP, the contact pattern on the glenoid surface moved rapidly from the inferior to the superior side during the first 30 degrees of abduction, and then went back to the inferior side. With the RP, the contact pattern on the humeral cup surface remained at the inferior side. Contact pressure was 20 times lower with the RP than with the AP. One year of use produced a maximum linear wear of 0.2 mm with the AP, and 0.13 mm with the RP. However, the volumetric wear was 8.4 mm3 with the AP, but reached 44.6 mm3 with the RP. Conclusion: Polyethylene particles are a matter of concern with AP. Infiltration of these particles within the bone-implant interface can induce a implant loosening. This problem should not be underestimated with RP. It might be associated to a higher level of humeral stem loosening reported with RP. The long term survival of RP might be improved by using a highly cross-linked polyethylene, which has a better abrasion resistance but lower plastic resistance.