968 resultados para Reduced common mode switching
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© IMechE 2014. Controlled auto-ignition, also known as homogeneous charge compression ignition, has been the subject of extensive research because of their ability to provide simultaneous reductions in fuel consumption and NOx emissions from a gasoline engine. However, due to its limited operation range, switching between controlled auto-ignition and spark ignition combustion is needed to cover the complete operating range of a gasoline engine for passenger car applications. Previous research has shown that the spark ignition -controlled auto-ignition hybrid combustion (SCHC) has the potential to control the ignition timing and heat release process during the mode transition operations. However, it was found that the SCHC is often characterized with large cycle-to-cycle variations. The cyclic variations in the in-cylinder pressure are particularly noticeable in terms of both their peak values and timings while the coefficient of variation in the indicated mean effective pressure is much less. In this work, the cyclic variations in SCHC operations were analyzed by means of in-cylinder pressure and heat release analysis in a single-cylinder gasoline engine equipped with Variable Valve Actuation (VVA) systems. First, characteristics of the in-cylinder pressure traces during the spark ignition-controlled auto-ignition hybrid combustion operation are presented and their heat release processes analyzed. In order to clarify the contribution to heat release and cyclic variation in SCHC, a new method is introduced to identify the occurrence of auto-ignition combustion and its subsequent heat release process. Based on the new method developed, the characteristics of cyclic variations in the maximum rate of pressure rise and different stages of heat release process have been analyzed and discussed.
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Common mode voltage (CMV) variations in PWM inverter-fed drives generate unwanted shaft and bearing current resulting in early motor failure. Multilevel inverters reduce this problem to some extent, with higher number of levels. But the complexity of the power circuit increases with an increase in the number of inverter voltage levels. In this paper a five-level inverter structure is proposed for open-end winding induction motor (IM) drives, by cascading only two conventional two-level and three-level inverters, with the elimination of the common mode voltage over the entire modulation range. The DC link power supply requirement is also optimized by means of DC link capacitor voltage balancing, with PWM control., using only inverter switching state redundancies. The proposed power circuit gives a simple power bits structure.
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Electromagnetic Interference (EMI) noise is one of the major issues during the design of the grid-tied power converters. Presence of high dv/dt in Common Mode (CM) voltage, excites the parasitic capacitances and causes injection of narrow peaky current to ground. This results in high EMI noise level. A topology consisting of a single phase PWM-rectifier with LCL filter, utilising bipolar PWM method is proposed which reduces the EMI noise level by more than 30dB. This filter topology is shown to be insensitive to the switching delays between the legs of the inverter. The proposed topology eliminates high dv/dt from the dc-bus CM voltage by making it sinusoidal. Hence, the high frequency CM current injection to ground is minimized.
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This paper develops a seven-level inverter structure for open-end winding induction motor drives. The inverter supply is realized by cascading four two-level and two three-level neutral-point-clamped inverters. The inverter control is designed in such a way that the common-mode voltage (CMV) is eliminated. DC-link capacitor voltage balancing is also achieved by using only the switching-state redundancies. The proposed power circuit structure is modular and therefore suitable for fault-tolerant applications. By appropriately isolating some of the inverters, the drive can be operated during fault conditions in a five-level or a three-level inverter mode, with preserved CMV elimination and DC-link capacitor voltage balancing, within a reduced modulation range.
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Electromagnetic interference (EMI) noise is one of the major issues during design of grid-tied power converters. A novel LCL filter topology for a single-phase pulsewidth modulation (PWM) rectifier that makes use of bipolar PWM method is proposed for a single-phase to three-phase motor drive power converter. The proposed topology eliminates high dv/dt from the dc-bus common-mode (CM) voltage by making it sinusoidal. Hence, the high-frequency CM current injection to the ground and the motor-side CM current are minimized. The proposed filter configuration makes the system insensitive to circuit non-idealities such as mismatch in inductors values, unequal turn-on and turn-off delays, and dead-time mismatch between the inverter legs. Different variants of the filter topology are compared to establish the effectiveness of the proposed circuit. Experimental results based on the EMI measurement on the grid side and the CM current measurement on the motor side are presented for a 5-kW motor drive. It is shown that the proposed filter topology reduces the EMI noise level by about 35 dB.
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In this paper, several aspects of high frequency related issues of modern AC motor drive systems, such as common mode voltage, shaft voltage and resultant bearing current and leakage currents, have been discussed. Conducted emission is a major problem in modern motor drives that produce undesirable effects on electronic devices. In modern power electronic systems, increasing power density and decreasing cost and size of system are market requirements. Switching losses, harmonics and EMI are the key factors which should be considered at the beginning stage of a design to optimise a drive system.
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Bearing damage in modern inverter-fed AC drive systems is more common than in motors working with 50 or 60 Hz power supply. Fast switching transients and common mode voltage generated by a PWM inverter cause unwanted shaft voltage and resultant bearing currents. Parasitic capacitive coupling creates a path to discharge current in rotors and bearings. In order to analyze bearing current discharges and their effect on bearing damage under different conditions, calculation of the capacitive coupling between the outer and inner races is needed. During motor operation, the distances between the balls and races may change the capacitance values. Due to changing of the thickness and spatial distribution of the lubricating grease, this capacitance does not have a constant value and is known to change with speed and load. Thus, the resultant electric field between the races and balls varies with motor speed. The lubricating grease in the ball bearing cannot withstand high voltages and a short circuit through the lubricated grease can occur. At low speeds, because of gravity, balls and shaft voltage may shift down and the system (ball positions and shaft) will be asymmetric. In this study, two different asymmetric cases (asymmetric ball position, asymmetric shaft position) are analyzed and the results are compared with the symmetric case. The objective of this paper is to calculate the capacitive coupling and electric fields between the outer and inner races and the balls at different motor speeds in symmetrical and asymmetrical shaft and balls positions. The analysis is carried out using finite element simulations to determine the conditions which will increase the probability of high rates of bearing failure due to current discharges through the balls and races.
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The global financial crisis (GFC) in 2008 rocked local, regional, and state economies throughout the world. Several intermediate outcomes of the GFC have been well documented in the literature including loss of jobs and reduced income. Relatively little research has, however, examined the impacts of the GFC on individual level travel behaviour change. To address this shortcoming, HABITAT panel data were employed to estimate a multinomial logit model to examine mode switching behaviour between 2007 (pre-GFC) and 2009 (post-GFC) of a baby boomers cohort in Brisbane, Australia—a city within a developed country that has been on many metrics the least affected by the GFC. In addition, a Poisson regression model was estimated to model the number of trips made by individuals in 2007, 2008, and 2009. The South East Queensland Travel Survey datasets were used to develop this model. Four linear regression models were estimated to assess the effects of the GFC on time allocated to travel during a day: one for each of the three travel modes including public transport, active transport, less environmentally friendly transport; and an overall travel time model irrespective of mode. The results reveal that individuals were more likely to switch to public transport who lost their job or whose income reduced between 2007 and 2009. Individuals also made significantly fewer trips in 2008 and 2009 compared to 2007. Individuals spent significantly less time using less environmentally friendly transport but more time using public transport in 2009. Baby boomers switched to more environmentally friendly travel modes during the GFC.
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This paper evaluates and proposes various compensation methods for three-level Z-source inverters under semiconductor-failure conditions. Unlike the fault-tolerant techniques used in traditional three-level inverters, where either an extra phase-leg or collective switching states are used, the proposed methods for three-level Z-source inverters simply reconfigure their relevant gating signals so as to ride-through the failed semiconductor conditions smoothly without any significant decrease in their ac-output quality and amplitude. These features are partly attributed to the inherent boost characteristics of a Z-source inverter, in addition to its usual voltage-buck operation. By focusing on specific types of three-level Z-source inverters, it can also be shown that, for the dual Z-source inverters, a unique feature accompanying it is its extra ability to force common-mode voltage to zero even under semiconductor-failure conditions. For verifying these described performance features, PLECS simulation and experimental testing were performed with some results captured and shown in a later section for visual confirmation.
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16-electrode phantoms are developed and studied with a simple instrumentation developed for Electrical Impedance Tomography. An analog instrumentation is developed with a sinusoidal current generator and signal conditioner circuit. Current generator is developed withmodified Howland constant current source fed by a voltage controlled oscillator and the signal conditioner circuit consisting of an instrumentation amplifier and a narrow band pass filter. Electronic hardware is connected to the electrodes through a DIP switch based multiplexer module. Phantoms with different electrode size and position are developed and the EIT forward problem is studied using the forward solver. A low frequency low magnitude sinusoidal current is injected to the surface electrodes surrounding the phantom boundary and the differential potential is measured by a digital multimeter. Comparing measured potential with the simulated data it is intended to reduce the measurement error and an optimum phantom geometry is suggested. Result shows that the common mode electrode reduces the common mode error of the EIT electronics and reduces the error potential in the measured data. Differential potential is reduced up to 67 mV at the voltage electrode pair opposite to the current electrodes. Offset potential is measured and subtracted from the measured data for further correction. It is noticed that the potential data pattern depends on the electrode width and the optimum electrode width is suggested. It is also observed that measured potential becomes acceptable with a 20 mm solution column above and below the electrode array level.
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Common mode voltage (CMV) variations in PWM inverter-fed drives generate unwanted shaft and bearing current resulting in early motor failure. Multilevel inverters reduce this problem to some extent, with higher number of levels. But the complexity of the power circuit increases with an increase in the number of inverter voltage levels. In this paper a five-level inverter structure is proposed for open-end winding induction motor (IM) drives, by cascading only two conventional two-level and three-level inverters, with the elimination of the common mode voltage over the entire modulation range. The DC link power supply requirement is also optimized by means of DC link capacitor voltage balancing, with PWM control, using only inverter switching state redundancies. The proposed power circuit gives a simple power bus structure.
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A multilevel inverter for generating 17 voltage levels using a three-level flying capacitor inverter and cascaded H-bridge modules with floating capacitors has been proposed. Various aspects of the proposed inverter like capacitor voltage balancing have been presented in the present paper. Experimental results are presented to study the performance of the proposed converter. The stability of the capacitor balancing algorithm has been verified both during transients and steady-state operation. All the capacitors in this circuit can be balanced instantaneously by using one of the pole voltage combinations. Another advantage of this topology is its ability to generate all the voltages from a single dc-link power supply which enables back-to-back operation of converter. Also, the proposed inverter can be operated at all load power factors and modulation indices. Additional advantage is, if one of the H-bridges fail, the inverter can still be operated at full load with reduced number of levels. This configuration has very low dv/dt and common-mode voltage variation.
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Stimulus artifacts inhibit reliable acquisition of biological evoked potentials for several milliseconds if an electrode contact is utilized for both electrical stimulation and recording purposes. This hinders the measurement of evoked short-latency biological responses, which is otherwise elicited by stimulation in implantable prosthetic devices. We present an improved stimulus artifact suppression scheme using two electrode simultaneous stimulation and differential readout using high-gain amplifiers. Substantial reduction of artifact duration has been shown possible through the common-mode rejection property of an instrumentation amplifier for electrode interfaces. The performance of this method depends on good matching of electrode-electrolyte interface properties of the chosen electrode pair. A novel calibration algorithm has been developed that helps in artificial matching of impedance and thereby achieves the required performance in artifact suppression. Stimulus artifact duration has been reduced down to 50 mu s from the stimulation-cum-recording electrodes, which is similar to 6x improvement over the present state of the art. The system is characterized with emulated resistor-capacitor loads and a variety of in-vitro metal electrodes dipped in saline environment. The proposed method is going to be useful for closed-loop electrical stimulation and recording studies, such as bidirectional neural prosthesis of retina, cochlea, brain, and spinal cord.
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We use vibration localization as a sensitive means of detecting small perturbations in stiffness in a pair of weakly coupled micromechanical resonators. For the first time, the variation in the eigenstates is studied by electrostatically coupling nearly identical resonators to allow for stronger localization of vibrational energy due to perturbations in stiffness. Eigenstate variations that are orders of magnitude greater than corresponding shifts in resonant frequency for an induced stiffness perturbation are experimentally demonstrated. Such high, voltagetunable parametric sensitivities together with the added advantage of intrinsic common mode rejection pave the way to a new paradigm of mechanical sensing. ©2009 IEEE.
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The most common mode of deactivation suffered by catalysts fitted to two-stroke engines has traditionally been thermal degradation, or even meltdown, of the washcoat and substrate. The high temperatures experienced by these catalysts are caused by excessively high concentrations of HC and CO in the exhaust gas which are, in turn, caused by a rich AFR and the loss of neat fuel to the exhaust during the scavenging period. The effects of catalyst poisoning due to additives in the oil is often regarded as a secondary, or even negligible, deactivating mechanism in two-stroke catalysts and has therefore received little attention. However, with the introduction of direct in-cylinder fuel injection to some larger versions of this engine, the quantities of HC escaping to the exhaust can be reduced to levels similar to those found on four-stroke gasoline engines. Under these conditions, the effects of poisoning are much more significant to catalyst durability, particularly for crankcase scavenged derivatives which allow considerable quantities of oil to escape into the exhaust in a neat, or partially burned form. In this paper the effects of oil-derived sulphur on catalyst performance are examined using specialised test apparatus. The oil used throughout the study was formulated specifically for a two-stroke engine fitted with direct in-cylinder fuel injection. The sulphur content of this oil was 0.21% by mass and particular attention was paid to the role of this element in the resulting deactivation. The catalyst was also designed for two-stroke applications and contained a high palladium loading of 300g/ft3 (28g/l) to prolong the life of the catalyst. It was found that the sulphur caused permanent deactivation of the CO reaction and increased the light-off temperature by around 40oC after oiling for 60 hours. This deactivation was progressive and led to a reduction in surface area of the washcoat, particularly in the micropores of around 5Å diameter. By using a validated catalyst model the change in surface area of the precious metal was estimated. It was found that the simulated palladium surface area had to be reduced by a factor of around 7.5 to produce the light-off temperature of the deactivated catalyst. Conversely, the light-off temperature of the C3H6 reaction was barely affected by the deactivation.