575 resultados para Cable


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Frequency converters are widely used in the industry to enable better controllability and efficiency of variable speed AC motor drives. Despite these advantages, certain challenges concerning the inverter and motor interfacing have been present for decades. As insulated gate bipolar transistors entered the market, the inverter output voltage transition rate significantly increased compared with their predecessors. Inverters operate based on pulse width modulation of the output voltage, and the steep voltage edge fed by the inverter produces a motor terminal overvoltage. The overvoltage causes extra stress to the motor insulation, which may lead to a prematuremotor failure. The overvoltage is not generated by the inverter alone, but also by the sum effect of the motor cable length and the impedance mismatch between the cable and the motor. Many solutions have been shown to limit the overvoltage, and the mainstream products focus on passive filters. This doctoral thesis studies an alternative methodology for motor overvoltage reduction. The focus is on minimization of the passive filter dimensions, physical and electrical, or better yet, on operation without any filter. This is achieved by additional inverter control and modulation. The studied methods are implemented on different inverter topologies, varying in nominal voltage and current.For two-level inverters, the studied method is termed active du/dt. It consists of a small output LC filter, which is controlled by an independent modulator. The overvoltage is limited by a reduced voltage transition rate. For multilevel inverters, an overvoltage mitigation method operating without a passive filter, called edge modulation, is implemented. The method uses the capability of the inverter to produce two switching operations in the same direction to cancel the oscillating voltages of opposite phases. For parallel inverters, two methods are studied. They are both intended for two-level inverters, but the first uses individual motor cables from each inverter while the other topology applies output inductors. The overvoltage is reduced by interleaving the switching operations to produce a similar oscillation accumulation as with the edge modulation. The implementation of these methods is discussed in detail, and the necessary modifications to the control system of the inverter are presented. Each method is experimentally verified by operating industrial frequency converters with the modified control. All the methods are found feasible, and they provide sufficient overvoltage protection. The limitations and challenges brought about by the methods are discussed.

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Tässä diplomityössä kehitetään Loviisan voimalaitoksen todennäköisyyspohjaisen paloriskianalyysin kaapelitietokantaa tulevaisuuden haasteita varten. Tietokannan kehittämistä varten tutustutaan todennäköisyyspohjaiseen riskianalyysiin varsin-kin paloriskianalyysin osalta. Käytännönläheisempää kehittämistä varten tutustu-taan voimalaitoksella nykyisin käytössä oleviin kaapelitietokantoihin: paloriski-tutkimusta varten laadittuun PSA-ELTIEen, kunnossapidon tiedonhallintajärjes-telmä LOMAXiin, sähkö- ja automaatiosuunnitteluyksikköjen arkistoihin sekä automaatiouudistuksen tietokantaan. Tietokannan käytännönläheisempien ominai-suuksien selvittämiseksi voimalaitoksella kokeiltiin kenttätarkastusmenetelmää, joka on ensisijainen kaapelikartoitusmenetelmä. Tietokantoihin tutustumisen perusteella vaihtoehtoisiksi tulevaisuuden tietokan-noiksi mietittiin LOMAXia, PSA-ELTIEtä tai uutta tietokantaa. Tulevaisuuden tietokantavaihtoehdoksi on päädytty ehdottamaan LOMAXia, joka vaatii vähem-män muutoksia muihin vaihtoehtoihin nähden. Tällainen laajalti käytössä oleva yhteinen tietokanta mahdollistaa sen, että tiedot ovat helpommin ja varmemmin kaikkien niitä tarvitsevien käytettävissä ja asiantuntijoiden muokattavissa, millä myös varmistetaan tietojen oikeellisuutta ja pysymistä ajan tasalla. Tulevaan LOMAX päivitykseen on ehdotettu tarpeellisia tietokenttien lisäyksiä ja kaapeli-hierarkian parantamista kaapelitietokannaksi käyttöönottamista varten.

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Työssä tutkitaan, kuinka pitkää moottorikaapelia on jännitevälipiiritaajuusmuuttajan kanssa mahdollista käyttää niin, että määritellyt reunaehdot vielä toteutuvat. Tavoitteena on tuottaa tietoa myynnille, markkinoinnille, tuotehallinnalle sekä tuoteylläpidolle siitä, miten taajuus-muuttaja toimii pidemmillä moottorikaapeleilla kuin valmistaja suosittelee. Tutkitut moottori-kaapelipituudet olivat 175…1025 metriä ja tutkitut laitteet nimellislähtövirroiltaan 2,4...25 A. Työssä aihetta käsitellään jänniteheijastusten näkökulmasta. Lisäksi tutkitaan moottorikaapelin pituuden vaikutusta taajuusmuuttajan eri komponenttien lämpenemiseen. Taajuusmuuttajan toiminnallisuutta arvioidaan moottorin suunnanvaihtojen avulla sekä turvallista toimintaa oikosulkutestein. Tutkittujen taajuusmuuttajien kohdalla on mahdollista käyttää taajuusmuuttajavalmistajan suositusta pidempiä moottorikaapeleita. Moottoriliittimien ylijännitteitä aiheuttavat jännite-heijastukset eivät aiheuttaneet raja-arvoja ylittäviä huippujännitteitä tutkituilla laitekokoon-panoilla. Myös lämpötilannousu oli maltillista tai jopa vähäistä taajuusmuuttajasta mitatuilla komponenteilla. Moottorisäätö havaittiin toimintakykyiseksi pidemmilläkin moottorikaape-leilla, tosin moottorin vääntömomentti heikkeni moottorikaapelien pituutta kasvatettaessa. Virranmittaus toimi hyvin myös pitkillä kaapeleilla, tuottaen vikalaukaisun kaikissa tehdyissä oikosulkutilanteissa. Moottorin ja taajuusmuuttajan melutaso nousivat moottorikaapelien pi-tuutta kasvatettaessa, vaikkakin moottorin käynti oli tasaista ja katkotonta Moottorikaapelin pituutta voidaan kasvattaa 325 metriin kaikissa tutkituissa laitteissa ilman, että mikään tutkittu ominaisuus vielä olennaisesti heikkenisi. Vielä 525 metrin moottorikaape-leita on mahdollista käyttää, mutta tällöin vääntömomentin tuotto on jo heikompaa.

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Large amplitude bus bar aeolian vibration may lead to post insulator damage. Different damping applications are used to decrease the risk of large amplitude aeolian vibration. In this paper the post insulator load caused by the bus bar aeolian vibration and the effect of damping methods are evaluated. The effects of three types of bus bar connectors and three types of primary structures are studied. Two actual damping devices, damping cable and their combinations are studied. The post insulator loads are studied with strain gage based custom made force sensors installed on the both ends of the post insulator and with the displacement sensor installed on the midpoint of the bus bar. The post insulator loads are calculated from the strain values and the damping properties are determined from the displacement history. The bus bar is deflected with a hanging weight. The weight is released and the bus bar is left to free damped vibration. Both actual bus bar vibration dampers RIBE and SBI were very effective against the aeolian vibration. Combining vibration damper with damping cable will increase the damping ratio but it may be unnecessary considering the extra effort. Bus bar connector type or primary structure have no effect on the vertical load. The bending moment at the post insulator with double sided bus bar connector is significantly higher than at the post insulator with single sided bus bar connector. No reliable conclusions about bus bar connector type effect can be done, but the roller bearing type or central bearing type connector may reduce the bending moment. The RHS steel frame as primary structure may increase the bending moment peak values since it is the least rigid primary structure type and it may start to vibrate as a response to the awakening force of the vibrating bus bar.

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Työssä tutkitaan tiedonsiirtoa eri modulaatioilla, bittinopeuksilla ja amplitudin voimakkuuksilla ja tuloksia tarkastellaan Bit Error Ration avulla. Signaaleja siirrettiiin myös koodattuna ja vertailtiin koodauksen etuja ja haittoja verrattuna koodaamattomaan tietoon. Datavirta kulkee AXMK-kaapelissa, joko tasasähkön mukana, tai maadoituskaapelissa. Tuloksissa havaittiin, että suurempi bittinopeus ei kasvattanut häviöiden määrää. Koodauksen käyttö toisaalta vähenti bittivirheiden määrää.

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A three degree of freedom model of the dynamic mass at the middle of a test sample, resembling a Stockbridge neutraliser, is introduced. This model is used to identify the hereby called equivalent complex cross section flexural stiffness (ECFS) of the beam element which is part of the whole test sample. This ECFS, once identified, gives the effective cross section flexural stiffness of the beam as well as its effective damping, measured as the loss factor of an equivalent viscoelastic beam. The beam element of the test sample may be of any complexity, such as a segment of stranded cable of the ACSR type. These data are important parameters for the design of overhead power transmission lines and other cable structures. A cost function is defined and used in the identification of the ECFS. An experiment, designed to measure the dynamic masses of two test samples, is described. Experimental and identified results are presented and discussed.

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A three degree of freedom model of the dynamic mass at the middle of a test sample, resembling a Stockbridge neutraliser, is introduced. This model is used to identify the hereby called equivalent complex cross section flexural stiffness (ECFS) of the beam element which is part of the whole test sample. This ECFS, once identified, gives the effective cross section flexural stiffness of the beam as well as its effective damping, measured as the loss factor of an equivalent viscoelastic beam. The beam element of the test sample may be of any complexity, such as a segment of stranded cable of the ACSR type. These data are important parameters for the design of overhead power transmission lines and other cable structures. A cost function is defined and used in the identification of the ECFS. An experiment, designed to measure the dynamic masses of two test samples, is described. Experimental and identified results are presented and discussed.

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This doctoral thesis introduces an improved control principle for active du/dt output filtering in variable-speed AC drives, together with performance comparisons with previous filtering methods. The effects of power semiconductor nonlinearities on the output filtering performance are investigated. The nonlinearities include the timing deviation and the voltage pulse waveform distortion in the variable-speed AC drive output bridge. Active du/dt output filtering (ADUDT) is a method to mitigate motor overvoltages in variable-speed AC drives with long motor cables. It is a quite recent addition to the du/dt reduction methods available. This thesis improves on the existing control method for the filter, and concentrates on the lowvoltage (below 1 kV AC) two-level voltage-source inverter implementation of the method. The ADUDT uses narrow voltage pulses having a duration in the order of a microsecond from an IGBT (insulated gate bipolar transistor) inverter to control the output voltage of a tuned LC filter circuit. The filter output voltage has thus increased slope transition times at the rising and falling edges, with an opportunity of no overshoot. The effect of the longer slope transition times is a reduction in the du/dt of the voltage fed to the motor cable. Lower du/dt values result in a reduction in the overvoltage effects on the motor terminals. Compared with traditional output filtering methods to accomplish this task, the active du/dt filtering provides lower inductance values and a smaller physical size of the filter itself. The filter circuit weight can also be reduced. However, the power semiconductor nonlinearities skew the filter control pulse pattern, resulting in control deviation. This deviation introduces unwanted overshoot and resonance in the filter. The controlmethod proposed in this thesis is able to directly compensate for the dead time-induced zero-current clamping (ZCC) effect in the pulse pattern. It gives more flexibility to the pattern structure, which could help in the timing deviation compensation design. Previous studies have shown that when a motor load current flows in the filter circuit and the inverter, the phase leg blanking times distort the voltage pulse sequence fed to the filter input. These blanking times are caused by excessively large dead time values between the IGBT control pulses. Moreover, the various switching timing distortions, present in realworld electronics when operating with a microsecond timescale, bring additional skew to the control. Left uncompensated, this results in distortion of the filter input voltage and a filter self-induced overvoltage in the form of an overshoot. This overshoot adds to the voltage appearing at the motor terminals, thus increasing the transient voltage amplitude at the motor. This doctoral thesis investigates the magnitude of such timing deviation effects. If the motor load current is left uncompensated in the control, the filter output voltage can overshoot up to double the input voltage amplitude. IGBT nonlinearities were observed to cause a smaller overshoot, in the order of 30%. This thesis introduces an improved ADUDT control method that is able to compensate for phase leg blanking times, giving flexibility to the pulse pattern structure and dead times. The control method is still sensitive to timing deviations, and their effect is investigated. A simple approach of using a fixed delay compensation value was tried in the test setup measurements. The ADUDT method with the new control algorithm was found to work in an actual motor drive application. Judging by the simulation results, with the delay compensation, the method should ultimately enable an output voltage performance and a du/dt reduction that are free from residual overshoot effects. The proposed control algorithm is not strictly required for successful ADUDT operation: It is possible to precalculate the pulse patterns by iteration and then for instance store them into a look-up table inside the control electronics. Rather, the newly developed control method is a mathematical tool for solving the ADUDT control pulses. It does not contain the timing deviation compensation (from the logic-level command to the phase leg output voltage), and as such is not able to remove the timing deviation effects that cause error and overshoot in the filter. When the timing deviation compensation has to be tuned-in in the control pattern, the precalculated iteration method could prove simpler and equally good (or even better) compared with the mathematical solution with a separate timing compensation module. One of the key findings in this thesis is the conclusion that the correctness of the pulse pattern structure, in the sense of ZCC and predicted pulse timings, cannot be separated from the timing deviations. The usefulness of the correctly calculated pattern is reduced by the voltage edge timing errors. The doctoral thesis provides an introductory background chapter on variable-speed AC drives and the problem of motor overvoltages and takes a look at traditional solutions for overvoltage mitigation. Previous results related to the active du/dt filtering are discussed. The basic operation principle and design of the filter have been studied previously. The effect of load current in the filter and the basic idea of compensation have been presented in the past. However, there was no direct way of including the dead time in the control (except for solving the pulse pattern manually by iteration), and the magnitude of nonlinearity effects had not been investigated. The enhanced control principle with the dead time handling capability and a case study of the test setup timing deviations are the main contributions of this doctoral thesis. The simulation and experimental setup results show that the proposed control method can be used in an actual drive. Loss measurements and a comparison of active du/dt output filtering with traditional output filtering methods are also presented in the work. Two different ADUDT filter designs are included, with ferrite core and air core inductors. Other filters included in the tests were a passive du/dtfilter and a passive sine filter. The loss measurements incorporated a silicon carbide diode-equipped IGBT module, and the results show lower losses with these new device technologies. The new control principle was measured in a 43 A load current motor drive system and was able to bring the filter output peak voltage from 980 V (the previous control principle) down to 680 V in a 540 V average DC link voltage variable-speed drive. A 200 m motor cable was used, and the filter losses for the active du/dt methods were 111W–126 W versus 184 W for the passive du/dt. In terms of inverter and filter losses, the active du/dt filtering method had a 1.82-fold increase in losses compared with an all-passive traditional du/dt output filter. The filter mass with the active du/dt method was 17% (2.4 kg, air-core inductors) compared with 14 kg of the passive du/dt method filter. Silicon carbide freewheeling diodes were found to reduce the inverter losses in the active du/dt filtering by 18% compared with the same IGBT module with silicon diodes. For a 200 m cable length, the average peak voltage at the motor terminals was 1050 V with no filter, 960 V for the all-passive du/dt filter, and 700 V for the active du/dt filtering applying the new control principle.

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Power line modelling has become an interesting research area in recent years as a result of advances in the power line distribution network system. Extensive knowledge about the power line cable characteristics can be implemented in a software algorithm in a modern broadband power-line communication modem. In this study, a novel approach for modelling power line cables (AMCMK) based on the broadband impedance spectroscopy (BIS) and transmission line matrix (TLM) techniques is recommended in characterizing a healthy cable and the various faults associated with low-voltage cables for both open and short circuit situation. Models for different cable conditions are developed and tuned, which include six models for both healthy and faulty cables situations. The models are on the basis of impedance response analysis of the cable. The resulting spectra from the simulations are also cross-correlated to determine the degree of similarities between the healthy cable spectra and their respective faulty spectra.

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La Cámara de Comercio de Bogotá inscribió el acta No. AA-021 de la asamblea de accionistas de la SOCIEDAD DE TELECOMUNICACIONES, INGENIERÍA MERCADEO TELEVISIÓN POR CABLE Y SERVICIOS SAS, en la cual se hizo nombramiento de gerente general, gerente ejecutivo y presidente de la asamblea de accionistas.

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In 1818 Parkhurst Whitney built stairs leading to the river’s edge at Prospect Point. In 1825 Porter Brother replaced that staircase with a spiral one. In 1844 Whitney started a water powered incline railway there although the staircase was also used until 1890. In 1906 the water wheel was replaced by an electric power plant. There were lower buildings which included Shadow of the Rock which was a concession stand and also rented raincoats to the tourists. This was destroyed by fire and ice in 1892 and replaced by a chalet-style building in 1894-95. On July 6th, 1907 a cable on the incline railway broke. One person was killed and several sustained injuries. An elevator was constructed and it opened in January of 1910. It was condemned in 1954 when water entered the shaft, this was at the time of the collapse of Prospect Point which occurred at 4:50 pm. on July 28, 1954. This photograph was taken prior to 1954. Today the New York State Observation Tower stands at Prospect Point and The Maid of the Mist boat ride is available from the base of the tower. with information from: Niagara Falls Canada: a History by the Kiwanis Club of Stamford, Ontario

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In 1948, The St. Catharines Civic Orchestra was founded by Jan Wolanek who was also the first conductor. Initially, this was a community orchestra and in 1963 its governing body assumed the name St. Catharines Symphony Association. In 1978 the name was again changed to The Niagara Symphony Association to reflect regional responsibilities. Wally Laughton was named Assistant Conductor in 1952/53. R.C. Clarke took over the orchestra for an interim period after Wolanek left in 1957. In 1958 Leonard Pearlman became the Music Director. It was under his direction that the Niagara Symphony Chorus came into existence in 1963. Milton Barnes succeeded Pearlman in 1964 and he was responsible for directing the symphony’s first opera production. He also made a concerted effort to attract younger people to symphonic music. In 1972 Leonard Atherton became the Music Director. He started the Cantata Choir and the Madrigal Singers. It was under his tenure that the orchestra became professional. When Atherton left in 1980, there were three seasons of guest conductors, the most notable of these conductors was Uri Mayer. In 1981 James Vincent Fusco was appointed as composer in residence and in 1983 Ermanno Florio became the Music Director. He retained this position until 1995 when Michael Reason took over. Daniel Swift was appointed as Music Director and Conductor in 1999 and the Niagara Symphony Orchestra became the orchestr in residence at Brock University. Laura Thomas was appointed as Associate Conductor 1n 2004. Daniel Swift’s resignation in 2008 began a search for a new Music Director. Bradley Thachuck was appointed as Music Director Designate and Principal Conductor in 2010. The orchestra is a fully professional, charitable institution with 52 members.The orchestra has also been led by Victor Feldbrill and Howard Cable. A junior symphony was first formed under Leonard Pearlman in 1960/61, but it wasn’t until 1965 that The St. Catharines Youth Orchestra was founded. The orchestra has consistently been an award winner in music festivals. The musicians range in age from 12 to 18 years. The highlight of the 1973-74 season was the orchestra’s participation in the first Canadian Festival of Youth Orchestras at The Banff School of Fine Arts. The St. Catharines Youth Orchestra has evolved from the St. Catharines School String and Brass Ensembles to a full scale symphony under the direction of conductor Paul van Dongen. In 1974 the Symphony House music program came into existence. It was 1976 when Richard Grymonpre was hired as the principal violinist of the St. Catharines Symphony Orchestra and conductor of the St. Catharines Youth Orchestra. Tak Ng Lai took over the position as conductor in 1978. Laura Thomas is currently the Music Director of The Niagara Youth Orchestra. Source: Niagara Symphony, Orchestra in Residence, Brock University website and notes from Niagara Symphony files

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Board with five postcards of Niagara Falls attractions. First postcard, Lincoln Beachey's Flight under Niagara Falls Bridge (copyright 1911 by Photo Specialty Co.). Second postcard, Calvery Walking Niagara Gorge on 3/4 in. cable. Third postcard, Burning Spring, Niagara Falls, Canada. Fourth postcard, Mrs. Anna Edson Taylor "Shot Horseshoe Falls (165 feet) October 24, 1901, and survived - a feat never before accomplished. Entered barrel one and one-half miles above the Falls. Was in barrel one hour and fifteen minutes. Had 32 pounds of air in barrel; 100 pounds weight on foot of barrel. Rescued six hundred yards below falls on Canadian shore". Fifth postcard, Burning Spring, Niagara Falls, Canada.

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Tesis (Maestro en Ciencias de la Ingeniería Mecánica con Especialidad en Materiales) U.A.N.L.