898 resultados para control the coil voltage
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Fundação de Amparo à Pesquisa do Estado de São Paulo (FAPESP)
Power performance evaluation of an electric home fan with triac-based automatic speed control system
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In order to provide a low cost system of thermal comfort, a common model of home fan, 40 cm diameter size, had its manual four-button control system replaced by an automatic speed control. The new control system has a temperature sensor feeding a microcontroller that, by using an optic coupling, DIAC or TRIAC-based circuit, varies the RMS value of the fan motor input voltage and its speed, according to the room temperature. Over a wide range of velocity, the fan net power and the motor fan input power were measured working under both control system. The temperature of the motor stator and the voltage waveforms were observed too. Measured values analysis showed that the TRIAC-based control system makes the fan motor work at a very low power factor and efficiency values. The worst case is at low velocity range where the higher fan motor stator temperatures were registered. The poor power factor and efficiency and the harmonics signals inserted in the motor input voltage wave by the TRIAC commutation procedure are correlated.
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Conselho Nacional de Desenvolvimento Científico e Tecnológico (CNPq)
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A novel single-phase voltage source rectifier capable to achieve High-Power-Factor (HPF) for variable speed refrigeration system application, is proposed in this paper. The proposed system is composed by a single-phase high-power-factor boost rectifier, with two cells in interleave connection, operating in critical conduction mode, and employing a soft-switching technique, controlled by a Field Programmable Gate Array (FPGA), associated with a conventional three-phase IGBT bridge inverter (VSI - Voltage Source Inverter), controlled by a Digital Signal Processor (DSP). The soft-switching technique for the input stage is based on zero-current-switching (ZCS) cells. The rectifier's features include the reduction in the input current ripple, the reduction in the output voltage ripple, the use of low stress devices, low volume for the EMI input filter, high input power factor (PF), and low total harmonic distortion (THD) in the input current, in compliance with the EEC61000-3-2 standards. The digital controller for the output stage has been developed using a conventional voltage-frequency control (scalar V/f control), and a simplified stator oriented Vector control, in order to verify the feasibility and performance of the proposed digital controls for continuous temperature control applied at a refrigerator prototype.
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When the electro-optic and acousto-optic effects are combined into a single device, the resulting acousto-electro-optic (AEO) modulator shows improved flexibility to overcome some limitations of the individual modulators or their cascade combinations. By using optical interferometry, it is possible to investigate the AEO modulator behavior as a function of this applied voltage. By this way, a lithium niobate AEO modulator is positioned in one of the arms of a Mach-Zehnder interferometer and operates at 62 MHz frequency, which constitutes the intermediate frequency of the heterodyne interferometer. Operating the AEO modulator in the acousto-optic small diffraction efficiency regime, the photodetected signal amplitude and phase are analyzed, and the induced phase shift, transmission curve and linearity response are obtained. The experimental results show good agreement with that expected from the coupled-mode theory. The possibility of linear control of the optical phase shift by the external voltage, from 0 to 2 p radians, is demonstrated.
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An experimental investigation of air enrichment in a combustion chamber designed to incinerate aqueous residues is presented. Diesel fuel and liquefied petroleum gas (LPG) were used independently as fuels. An increase of 85% in the incineration capacity was obtained with nearly 50% O-2 in the oxidant gas, in comparison to incineration with air only. The incineration capacity continues increasing for enrichment levels above 50% O-2 , although at a lower pace. For complete oxy-flame combustion (100% O-2 ), the increase of the incineration capacity was about 110% relative to the starting conditions and about 13.5% relative to the condition with 50% O-2 . The CO concentration measured near the flame front decreases drastically with the increase of O-2 content in the oxidant gas. At the chamber exit, the CO concentration was always near zero, indicating that the chamber residence time was sufficient to complete fuel oxidation in any test setting. For diesel fuel, the NOx was entirely formed in the first region of the combustion chamber. For diesel fuel, there was some increase in the NOx concentration up to 35% of O-2 ; this increase became very sharp after that. From 60 ppm, at operation with air only, the NOx concentration raises to 200 ppm at 35% O-2 , and then to 2900 ppm at 74% O-2 . The latter corresponds to six times more NOx in terms of the ratio of mass of NO to mass of residue, compared to the situation of combustion with air only. For LPG, the NOx concentrations reached 4200 ppm at 80% O-2 , corresponding to nine times more, also in terms of the ratio of mass of NO to mass of residue, in comparison with combustion with air only. Results of different techniques used to control the NOx emission during air enrichment are discussed: (a) variation of the recirculated zone intensity, (b) increase of the spray Sauter mean diameter, (c) fuel staging, (d) oxidizer staging, and (e) ammonia injection. The present paper shows that NOx emission may be controlled without damage of the increase of incineration capacity by the enrichment and with low emission of partial oxidation pollutants such as CO.
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Crowbar switches are largely used in plasma devices, such as field-reversed configuration (FRC) machines and tokamaks, to avoid energy return from the discharge coil to the capacitor bank. A method of identification of all resistances, inductances and currents involved in capacitor bank discharges using a crowbar is proposed based on the derivation of the general analytical form of the coil current. This analysis can also be used for optimization of the discharge, reducing the ripple amplitude inherent in the crowbar-switched current. Fitting results of the TC-1 UNICAMP FRC device are also presented in this work.
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In this article, we consider the synthetic control chart with two-stage sampling (SyTS chart) to control the process mean and variance. During the first stage, one item of the sample is inspected; if its value X, is close to the target value of the process mean, then the sampling is interrupted. Otherwise, the sampling goes on to the second stage, where the remaining items are inspected and the statistic T = Sigma [x(i) - mu(0) + xi sigma(0)](2) is computed taking into account all items of the sample. The design parameter is function of X-1. When the statistic T is larger than a specified value, the sample is classified as nonconforming. According to the synthetic procedure, the signal is based on Conforming Run Length (CRL). The CRL is the number of samples taken from the process since the previous nonconforming sample until the occurrence of the next nonconforming sample. If the CRL is sufficiently small, then a signal is generated. A comparative study shows that the SyTS chart and the joint X and S charts with double sampling are very similar in performance. However, from the practical viewpoint, the SyTS chart is more convenient to administer than the joint charts.
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A microactuator made from poly(vinylidene fluoride) (PVDF), a piezoelectric polymer, was fabricated to control the gas flow rate through a glass micronozzle. The actuator was formed by gluing together two PVDF sheets with opposite polarization directions. The sheets were covered with thin conducting films on one side, that were then used as electrodes to apply an electric field to move the valve. The actuator has a rectangular shape, 3 mm x 6 mm. The device was incorporated with a micronozzle fabricated by a powder blasting technique. Upon applying a DC voltage across the actuator electrodes, one sheet expands while the other contracts, generating an opening motion. A voltage of +300 V DC was used to open the device by moving the actuator 30 mu m, and a voltage of -200 V DC was used to close the device by moving the actuator 20 mu m lower than the relaxed position. Flow measurements were performed in a low-pressure vacuum system, maintaining the microvalve inlet pressure constant at 266 Pa. Tests carried out with the actuator in the open position and with a pressure ratio (inlet pressure divided by outlet pressure) of 0.5, indicated a flow rate of 0.36 sccm. In the closed position, and with a pressure ratio of 0.2, a flow rate of 0.32 sccm was measured.
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ZnO seed particles and Cr2O3 were used in this study to control the microstructure of ZnO varistors. The seed particles were prepared by adding 1.0 mol % BaO to ZnO. The powder was then calcined at 800-degrees-C for 2 h, pressed into pellets and sintered at 1400-degrees-C for 8 h. The sintered ZnO was ground and the BaO eliminated by washing in water. The remaining ZnO powder was classified into a size fraction ranging from 38 to 149 mum. The addition of a small amount (1 weight %) ZnO seed grains produces varistors with low breakdown voltages (7.6 V/mm) and an alpha coefficient of approximately 10. The addition of Cr2O3 stabilizes the spinel phase yielding a more homogeneous microstructure, but degraded electrical behaviour of the ZnO varistor.
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A constant-current stimulator for high-impedance loads using only low-cost standard high-voltage components Is presented. A voltage-regulator powers an oscillator built across the primary of a step-up transformer whose secondary supplies, after rectification, the high voltage to a switched current-mirror in the driving stage. Adjusting the regulated voltage controls the pulsed-current intensity. A prototype produces stimulus of amplitude and pulsewidth within 0 less than or equal to I-skin less than or equal to 20 mA and 50 mus less than or equal to T-pulse less than or equal to 1 ms, respectively. Pulse-repetition spans from 1 Hz to 10 Hz. Worst case ripple is 3.7% at I-skin = 1 mA. Overall consumption is 5.6 W at I-skin = 20 mA.
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This paper proposes a methodology to incorporate voltage/reactive representation to Short Term Generation Scheduling (STGS) models, which is based on active/reactive decoupling characteristics of power systems. In such approach STGS is decoupled in both Active (AGS) and Reactive (RGS) Generation Scheduling models. AGS model establishes an initial active generation scheduling through a traditional dispatch model. The scheduling proposed by AGS model is evaluated from the voltage/reactive points of view, through the proposed RGS model. RGS is formulated as a sequence of T nonlinear OPF problems, solved separately but taking into account load tracking between consecutive time intervals. This approach considerably reduces computational effort to perform the reactive analysis of the RGS problem as a whole. When necessary, RGS model is capable to propose active generation redispatches, such that critical reactive problems (in which all reactive variables have been insufficient to control the reactive problems) can be overcome. The formulation and solution methodology proposed are evaluated in the IEEE30 system in two case studies. These studies show that the methodology is robust enough to incorporate reactive aspects to STGS problem.
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This paper deals with the design and analysis of a Dynamic Voltage Restorer output voltage control. Such control is based on a multiloop strategy, with an inner current PID regulator and an outer P+Resonant voltage controller. The inner regulator is applied on the output inductor current. It will be also demonstrated how the load current behavior may influence in the DVR output voltage, which. justifies the need for the resonant controller. Additionally, it will be discussed the application of a modified algorithm for the identification of the DVR voltage references, which is based on a previously presented positive sequence detector. Since the studied three-phase DVR is assumed to be based on three identical H-bridge converters, all the analysis and design procedures were realized by means of single-phase equivalent circuits. The discussions and conclusions are supported by theoretical calculations, nonlinear simulations and some experimental results.
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Conselho Nacional de Desenvolvimento Científico e Tecnológico (CNPq)
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This experiment was developed in order to evaluation the efficiency of pheromone to control the pink bollworm and the total time of its release in cotton field. The experiment was installed in field conditions, in Chapadao do Sul/SP/Brazil, from January to April, 1998. The treatments consisted of 2 areas, being one of 30ha, where it was applied the pheromone and another of 10ha that was chosen as control area and did not receive pheromone. In the treated area, the laboratory synthesized sex pheromone (PB-Rope) was used thought of dispensers that allowed the slow and gradual release of the active substance. A total of 250 dispenser per hectare were evenly hand distributed in the area. The dispensers were wrapped around the plants. Both areas (treated area and untreated area) were monitored by delta trap. For evaluation of the boll damage, the treatment area was divided into 4 sub-areas. Twenty five green bolls were collected at random from each sub-area at 48 and 65 days after pheromone treatment. Bolls were cracked open by hand, and number of the bolls with symptoms of pink bollworm attacks was recorded. For evaluation of the productivity four areas were demarcated in each treatment, where all fibers and seeds harvested were weighted. Release rate of pheromone from dispenser was evaluated through of the weigh of the dispensers. Were marked and weighed in analytic scale, 20 dispensers contend the pheromone, being placed 10 dispensers under the cotton plants in treated area and other 10 dispensers in an open area. To every 15 days the dispensers were retired and weighed in analytic scale and soon after put back in the field in the same places. The results showed that only one application of mating disrupt pheromone, used in a dosage of 250 dispenser/ha, reached 80% of control for pink bollworm. the release period of pheromone from dispenser, after the application, was 120 days.