137 resultados para setup carryover


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Fundação de Amparo à Pesquisa do Estado de São Paulo (FAPESP)

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Conselho Nacional de Desenvolvimento Científico e Tecnológico (CNPq)

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Pós-graduação em Engenharia Mecânica - FEG

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Fundação de Amparo à Pesquisa do Estado de São Paulo (FAPESP)

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Conselho Nacional de Desenvolvimento Científico e Tecnológico (CNPq)

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The Virgo detector is a kilometer-scale interferometer for gravitational wave detection located near Pisa (Italy). About 13 months of data were accumulated during four science runs (VSR1, VSR2, VSR3 and VSR4) between May 2007 and September 2011, with increasing sensitivity. In this paper, the method used to reconstruct, in the range 10 Hz-10 kHz, the gravitational wave strain time series h(t) from the detector signals is described. The standard consistency checks of the reconstruction are discussed and used to estimate the systematic uncertainties of the h(t) signal as a function of frequency. Finally, an independent setup, the photon calibrator, is described and used to validate the reconstructed h(t) signal and the associated uncertainties. The systematic uncertainties of the h(t) time series are estimated to be 8% in amplitude. The uncertainty of the phase of h(t) is 50 mrad at 10 Hz with a frequency dependence following a delay of 8 mu s at high frequency. A bias lower than 4 mu s and depending on the sky direction of the GW is also present.

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Conselho Nacional de Desenvolvimento Científico e Tecnológico (CNPq)

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In heavy machining industries, a critical point that must be taken into account is setup. Because the characteristics of machine tools and parts to be machined, usually pieces robust and large, the preparation of these parts must be made accurately for machining has a good result as planned. As a result of the difficulty raised in the setup machining of heavy parts, companies in this segment seek alternatives to reduce the unproductive time caused by setup and optimize machining processes. One way was found that these companies create operating instructions that describe and standardize the operation between its employees, as well as deploy a control machining times to measure the unproductive time caused by the setup. This work studied a new system for the realization of centering and alignment of Rotating Deck R-9350 in CNC Milling Machine PAMA Speedram 3000, in Liebherr Brazil company. The part Rotating Deck R-9350 is a critical part in which its machining in PAMA Milling Machine is made in three phases and their setup times are quite high and involve stopping the machine. It has been tested and proposed a solution to the realization of this part of the setup without the use of the machine, but of the measuring instrument three-dimensional Laser tracker, with which the machine continued to work, while he was in the centering and alignment of other parts. It was noted that the instrument technically attended the need and it was possible to perform this operation more accurately

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This paper aims to survey data to analyze the productive capacity of a machining process of rolling bearings by methods-time measurement, in order to identify its bottlenecks and propose improvements in the system. The production times at the company are not known, the method of separation of operations and identification of its activities and the timing of production times and setup become points of departure for this paper. The results from this method of analysis provide clarity in identifying system weaknesses and by them it was possible to carry out the proposals for improvement in some process steps. The implementation of the improvements was not performed, but with the goals of this work was made possible to raise relevant information of the analyzed system

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Currently, the major method for controlling leaf-cutting ants uses toxic baits containing the insecticide sulfluramide. Such compound presents harmful effects to the environment and to human health, which drive the community’s concerns towards new strategies for controlling these insects. Previous studies showed the occurrence of Syncephalastrum racemosum in nests of the leaf-cutting ants submitted to treatments using insecticides. In order to understand the role of S. racemosum in nests of leaf-cutting ants, the present work investigated the antagonism of S. racemosum towards the leaf-cutting ant-cultivar (Leucoagaricus gongylophorus). Using in vitro essays, we co-cultivated L. gongylophorus and S. racemosum (n= 6 lineages). For comparison, we also used the same setup to test one strain of Escovopsis weberi, since this fungus is considered a specialized parasite of the leaf-cutting ant cultivar. All S. racemosum strains inhibited the growth of L. gongylophorus (ANOVA 2 way, F= 23,61, P< 0,01). The same was observed for E. weberi. There were no significant difference between S. racemosum and E. weberi inhibition (Bonferroni test, P> 0,05). In addition, we verified that all S. racemosum strains colonized and sporulated over the fungus garden up to 96 h after garden fragments without workers were inoculated with spores suspensions. Similar results were observed on gardens that were inoculated with spores of E. weberi. The results indicate that S. racemosum act as antagonist of the leaf-cutting ant cultivar. The putative possibility for using S. racemosum as biological control agent of leaf-cutting ants is discussed in the present work

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Due to globalization, is increasingly common for companies to make their products more competitive. With this background, the industries seek more efficient ways to produce. This paper aims to examine the tools of Lean Manufacturing applied in an industry luminaries ,addressing the positive aspects. Were applied tools like value stream mapping, Kanban, setup reduction and 5S program. With the application of these tools obtained improvements in processes, reducing lead time from factory and reducing the cost of the luminaries

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Many variables are indirectly involved in the transformation of raw material into a metallurgical industry, such as machine hours, hours of hand labor directly and / or indirect, setup time, etc. This research focuses on the complexity of formulating the cost of metallurgical products, based on a case study, in which one has incurred a large loss on the sale of a product called Punch. The main objective of this work is to define the variables of the cost of members and other metallurgical products, so simplified general, checking what were the failures costing the case studied, in order to help others. The method of formulating cost was determined as recommended by SEBRAE guidance for small businesses. The results showed a loss R$ 13.201,00 in the batch of 15 units of punch. Possible improvements have been identified for reducing the production cost

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The materials designed to be used in electroluminescent (EL) devices construction are studied and improved since 1936. Great interests in the development of this kind of devices are mainly due to its low power consumption, flexibility, low cost and easy processing. One class of ELs devices with these characteristics are produced by employing a organic-polymeric/inorganic composite from a conductive polymer blend and an inorganic electroluminescent material (Zn2SiO4:Mn) dispersed in the polymeric matrix. This kind of device operates in d.c. or a.c. potentials, with EL of hundreds candela in the green region of the visible spectrum. However, few studies on the light emission were performed for these devices. In order to characterize devices made from composites, in this work is proposed a method of characterizing the electroluminescence associated with the impedance spectroscopy technique. To implement the technique of impedance spectroscopy was employ an experimental setup consisting of a source of a.c. voltage, an oscilloscope, and a reference resistor. Associated with this system, was use a photo diode and an analog electrometer to characterize the emitted light signal from the sample. The system was implemented allows characterization by impedance spectroscopy in the frequency range from 0.2 Hz up to 2 MHz and voltage amplitudes of 5 mV up to 20 kV. This system permits, at the same time, measurement of the RMS value of the luminance for devices in frequency range from 20 Hz up to 2 MHz. To test the system efficiency, an EL device was characterized showing analogous results to those reported in literature. By doing this, was demonstrated the efficiency of the system for electroluminescence characterization associated with the electrical characterization by impedance spectroscopy, for devices

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The cosmetic industry has presenting growth in Brazil and one way to support this demand is improving production and reducing waste. Wastes can be related to setup time, which is spent to support demand of product´s mix and volume. One of the methodologies used to reduce setup time is SMED (Single Minute Exchange of Die). This paper aims to describe and analyze the setup process in a production line in a cosmetic industrial branch, before and after the application of SMED methodology, highlighting good practices and difficulties in order to help other companies develop fast setup. The research method used was the case study. From the analysis of the implementation of the methodology on the company which is object from the case study was possible to summarize good practices, such as: the use of pillar E&T to store information about the training on the SMED methodology; creation of a multifunctional teamwork and involving different areas; creation of a “From-To” matrix. Difficulties were identified, such as: high and constant turnover of people who work on the shop floor; lack of discipline in filling the forms and by doing the setup activities that were standardized; lack of financial resources; lack of people´s availability in orer to conduct necessary meetings and trainings. Recommendations for other companies have also been proposed, such as: training of the team involved, before starting the project and a refresher training; standardization of training, forms and documentation of all steps of the project; create a multifunctional team; training after an employee, who is responsible for the setup, leaves the company