369 resultados para Steel-concrete bonding


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Iowa has been using low slump concrete for repair and surfacing of deteriorated bridge decks on a routine basis since the mid 1960'2. More than 150 bridges have been resurfaced by this method with good results. A study was initiated in 1973 to evaluate 15 bridges resurfaced with low slump concrete, and one bridge resurfaced with latex modified concrete. The evaluation includes an assessment of concrete physical properties, chloride penetration rates, concrete consolidation, and riding qualities of the finished bridge deck. Results indicate that the overall properties of these two types of concrete are quite similar and have resulted in a contractor option concerning which system shall be used on bridge deck repair/resurfacing projects.

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A new machine, the ROTO-MILL Profiler, became available in early 1976. This machine, manufactured by CMI Corporation of Oklahoma City, Oklahoma provides pavement surface Scarification at a much higher production rate than was previously possible. Iowa had the opportunity to observe and evaluate this machine on two separate sections of primary portland cement concrete pavement in October, 1976. The marked improvement in the profile index and the skid resistance indicates this machine may be considered a viable method for improving rideability and skid resistance of a roadway that is otherwise reasonably sound.

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A research project involving 2, 3, 4, and 5 in. (5.1, 7.6, 10.2, and 12.7 cm) of bonded portland cement concrete (PCC) overlay on a 1.3 mile (2.1 km) PCC pavement was conducted in Clayton County, Iowa, during September 1977, centering on the following objectives: (1) Determine the mixing and proportioning procedures required in using a conventional, central mix proportioning plant to produce a dense PCC mixture using standard mixes with super water reducing admixtures; (2) Determine the economics, longevity and maintenance performance of a bonded, thin-lift, non-reinforced PCC resurfacing course using conventional procedures, equipment and concrete paving mixtures both with and without super water reducing admixtures; and (3) Determine if an adequate bond between the existing pavement and an overlay of thin-lift, dense, non-reinforced PCC can be obtained with only special surface cleaning and no surface removal or grinding. The conclusions are as follows: (1) Normal mixing equipment and proportioning procedures could be used using a conventional central-mix proportioning plant. This was successful when used with super water reducing admixtures. Only minor changes need be made in procedures and timing. (2) The time has been too short since the completion of the project to determine how the new pavement will perform, however, initially it appears that the method is economical and no reason is seen at this time why the life of the pavement should not be comparable to an all new pavement. (3) The initial test results show that bond strength, regardless of which method of cleaning is used, scarifying, sand blasting or water blasting, far exceed what is considered the minimum bond strength of 200 psi (1379 kPa) except where the paint stripes were intentionally left, thus showing that the paint must be removed. (4) It appears that either cement and water grout or sand, cement and water grout may be used and still obtain the required bond.

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Two objectives were involved in this recycling project: To determine if the asphalt concrete surfacing from an existing roadway could be removed, the existing portland cement concrete pavement broken, removed, crushed to 1-1/2 inch minus, proportioned through a conventional central mix proportioning plant with the addition of concrete sand, and placed with a conventional slipform paver; and to determine if a two course, composite pavement, each course of different mix proportions, could be placed monolithically with conventional slipform equipment after being proportioned and mixed in a conventional central mix plant. The project was completed with no major problem. The objectives were satisfactorily met. The project was a success to the degree that the Iowa D.O.T. is proceeding with at least two projects for the 1977 construction season that will utilize the old pavement as appregate for the new pavement.

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This report provides details of IADOT's experience removing and crushing asphaltic concrete and portland cement concrete for recycling. The recycled material was used on interstate highways for the subbase and shoulders. The major problem IADOT encountered on this project was the removal of reinforcing steel from the broken concrete. The contractor used hydraulic powered shears to clip off all protruding steel during the removal and loading of the concrete on the grade. This project took place in 1977.

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A concrete admixture, Gla-Zit, was evaluated in 1970 by the Iowa State Highway Commission and found to be lacking in providing beneficial effects to concrete. This current evaluation is similar to that conducted in 1970 with slight modifications in the actual concrete mixes studied. At the request of the manufacturer, all concrete mixes containing Gla-Zit were non-air entrained. Concrete properties examined were compressive strength, salt scaling resistance, absorption, resistance to chloride penetration, and freeze-thaw durability. The differences found in the mixes studied are much more attributible to air entrainment, or the lack thereof, than the influence of Gla-Zit. The study re-affirms that it is necessary to have properly air entrained concrete to lessen the detrimental effects of freeze and thaw and scaling caused by salting. There is no data in the study to suggest that Gla-Zit has any significant effect on any of the concrete properties examined.

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The textured concrete surface on all PCC primary paving projects (and when specified on secondary projects) is required to be grooved in a specified manner. The laboratory test for determining the efficiency index of concrete curing compounds is made on slabs that are not grooved. This short investigation was undertaken to determine any changes in the curing efficiency index when using various rates of application of curing compound on grooved concrete. Currently a 95 percent curing efficiency index is specified at an application rate of 15 square yards per gallon. Can this efficiency be achieved, and if so at what application rate, on grooved concrete? Grooving the concrete greatly increases the surface area and also causes the liquid curing compound to run off the high spots and collect in the grooves.

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Fine limestone aggregate is abundant in several areas of the state. The aggregate is a by-product from the production of concrete stone. Roller compacted concrete (RCC) is a portland cement concrete mixture that can be produced with small size aggregate. The objective of the research was to evaluate limestone screenings in RCC mixes. Acceptable strength and freeze/thaw durability were obtained with 300 pounds of portland cement and 260 pounds of Class C fly ash. The amount of aggregate passing the number 200 sieve ranged from 4.6 to 11 percent. Field experience in Iowa indicates that the aggregate gradation is more critical to placeability and compactibility than laboratory strength and durability.

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Bridge deck cracking occasionally occurs during construction for any number of reasons. Improper design, concrete placement or deck curing can result in cracks. One contributing factor toward cracking may be dead load deflections induced during concrete placement. For both continuous and non-continuous bridges, specific placement sequences are required to minimize harmful deflections in previously placed sections. Set retarding admixtures are also used to keep previously placed concrete plastic until the pour is completed. The problem is--at what point does movement of the concrete cause permanent damage to the deck. The study evaluated the time to crack formation relationship for mixes with low and high dosages of set retarding admixtures currently approved for use in Iowa state and county projects.

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Two specialty cements are currently being marketed as a way to achieve portland cement concrete pavement opening strengths at less than 12 hours after placement. The cements are Pyrament from Pyrament/Lone Star Industries of Houston, Texas and Ideal Regulated-Set (RS) Portland Cement from Ideal Cement Company of Saratoga, Arkansas. The objective of the study was to evaluate the strength gain and durability of concrete produced with Pyrament and Ideal RS cement as Fast Track concrete. Mixes with 610 lb/cu yd (362 kg/cu m) cement were made and tested. Both Pyrament and Ideal RS are capable of producing pavement opening times less than 12 hours. Recent changes to Ideal RS cement have produced concrete flexural strengths of 550 psi (3792 kPa) at 4 hours in Iowa tests. Freeze/thaw durability of the concrete was not adversely affected by using either cement.

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There are projects where opening the pavement to traffic in less than the 5 to 7 days is needed, but an 8 to 12 hour opening time is not necessary. The study examined fast track concrete with Type I cement and admixtures. The variables studied were: (1) cure temperature, (2) cement brand, (3) accelerators, and (4) water reducers. A standard water reducer and curing blankets appear to be effective at producing a 24 hour to 36 hour opening strength. An accelerator and/or high range water reducer may produce opening strength in 12 to 24 hours. Calcium chloride was most effective at achieving high-early strength.

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Chloride ion penetration through concrete to reinforcing steel is causing the premature deterioration of numerous bridge decks in Iowa. The purpose of the research reported in this paper was to determine whether any of several additives or alternative deicing chemicals could inhibit corrosion of reinforcing steel. The deicers tested were calcium magnesium acetate (CMA), CMA plus NaCl (NaCl: sodium chloride), Quicksalt plus PCI, and CG-90, a polyphosphate solution being developed by Cargill. Two tests were established. First, steel coupons were placed in a 15% solution of a deicer and distilled water to determine which alternative deicer would cause the least amount of corrosion in solution. The coupons were weighed periodically to determine each coupon's weight loss from corrosion. The second test involved ponding a 15% solution of each material on reinforced concrete blocks. Weekly copper-copper sulfate electrical half-cell (CSE) potential readings were taken on each block to determine whether corrosive activity was occurring at the steel surface. When the ponding research was concluded, concrete samples were taken from one of the three blocks ponded with each deicer. The samples were used to determine the chloride ion content at the level of the steel. Results show that all the deicers were less corrosive than NaCl. Only pure CMA, however, significantly inhibited the corrosion of steel embedded in concrete.

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Ten bridges were chosen to have their concrete barrier rails constructed with one rail having "Fibermesh" synthetic fibers added and the other rail without the fibers. The rails were constructed in 1985, 1986, or 1987. All the bridges were inspected in 1988 and no consistent reduction in cracking was achieved using Fibermesh fibers in the p.c. concrete bridge barrier rails.

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Crack formation has been a problem on some recently constructed bridges in Iowa. Drying shrinkage has been considered a contributing factor in that cracking. The study was undertaken to evaluate some of those material properties that contribute to the magnitude of drying shrinkage. Cement content, cement composition, fly ash and retarding admixture were the factors studied. Concrete prisms were cast for seven mixes and, after curing, were exposed to 100 deg F heat at ambient humidity for 280 days. The following were observed from the testing: (1) Higher C3A content cement concrete produced larger shrinkage; (2) Use of fly ash increased shrinkage; (3) Use of retarder increased shrinkage; and (4) Lowering the cement content reduced the shrinkage.

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This report summarizes the findings of a research which was intended to evaluate the concrete strength and opening time for the full depth patching projects in Iowa under cold weather and whether or not cold water could be allowed in the mix. This research was performed both in the laboratory and in the field. The results indicated that with the present specification the concrete strength after five hours for two-lane patches which requires hot water and calcium chloride is about 1,600 psi. Hence, if a higher strength is desired, a longer curing time is required. Hot water will have to be used and water reducer is not recommended for two-lane patches. On the other hand, the concrete strength for multi-lane patches with either hot or cold water approaches 4,000 psi in less than 24 hours. There was only a slight difference in compressive strengths between the 24-hour and 36-hours curing times.