2 resultados para Effective notch stress method

em CaltechTHESIS


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This thesis presents the results of an experimental investigation of the initiation of brittle fracture and the nature of discontinuous yielding in small plastic enclaves in an annealed mild steel. Upper and lower yield stress data have been obtained from unnotched specimens and nominal fracture stress data have been obtained from specimens of two scale factors and two grain sizes over a range of nominal stress rates from 10^2 to 10^7 lb/in.^2 sec at -111°F and -200°F. The size and shape of plastic enclaves near the notches were revealed by an etch technique.

A stress analysis utilizing slip-line field theory in the plastic region has been developed for the notched specimen geometry employed in this investigation. The yield stress of the material in the plastic enclaves near the notch root has been correlated with the lower yield stress measured on unnotched specimens through a consideration of the plastic boundary velocity under dynamic loading. A maximum tensile stress of about 122,000 lb/in.^2 at the instant of fracture initiation was calculated with the aid of the stress analysis for the large scale specimens of ASTM grain size 8 1/4.

The plastic strain state adjacent to a plastic-elastic interface has been shown to cause the maximum shear stress to have a larger value on the elastic than the plastic side of the interface. This characteristic of dis continuous yielding is instrumental in causing the plastic boundaries to be nearly parallel to the slip-line field where the plastic strain is of the order of the Lüder's strain.

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This report presents the results of an investigation of a method of underwater propulsion. The propelling system utilizes the energy of a small mass of expanding gas to accelerate the flow of a large mass of water through an open ended duct of proper shape and dimensions to obtain a resultant thrust. The investigation was limited to making a large number of runs on a hydroduct of arbitrary design, varying between wide limits the water flow and gas flow through the device, and measuring the net thrust caused by the introduction and expansion of the gas.

In comparison with the effective exhaust velocity of about 6,000 feet per second observed in rocket motors, this hydroduct model attained a maximum effective exhaust velocity of more than 27,000 feet per second, using nitrogen gas. Using hydrogen gas, effective exhaust velocities of 146,000 feet per second were obtained. Further investigation should prove this method of propulsion not only to be practical but very efficient.

This investigation was conducted at Project No. 1, Guggenheim Aeronautical Laboratory, California Institute of Technology, Pasadena, California.