931 resultados para production cycle


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Conselho Nacional de Desenvolvimento Científico e Tecnológico (CNPq)

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Fundação de Amparo à Pesquisa do Estado de São Paulo (FAPESP)

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Pós-graduação em Agronomia (Energia na Agricultura) - FCA

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Fundação de Amparo à Pesquisa do Estado de São Paulo (FAPESP)

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Conselho Nacional de Desenvolvimento Científico e Tecnológico (CNPq)

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Conselho Nacional de Desenvolvimento Científico e Tecnológico (CNPq)

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Conselho Nacional de Desenvolvimento Científico e Tecnológico (CNPq)

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Um experimento de campo com diferentes níveis de irrigação e nitrogênio foi conduzido no Centro de Ciências Agrárias da Universidade Federal de Alagoas com o objetivo de determinar a função de produção e as isoquantas de produtividade agrícola da cana-de-açúcar com base nas lâminas de irrigação e doses de nitrogênio (N). A precipitação pluvial efetiva durante o ciclo de produção foi 1.037 mm e a lâmina de irrigação bruta máxima foi 873 mm. A produtividade agrícola ficou entre 118 e 188 Mg ha-1, média de 160 Mg ha-1. Na isoquanta da produtividade agrícola média da cana-de-açúcar, a taxa marginal de substituição de água por N é 0,36 kg mm-1 (na interseção das retas de 25 kg de N ha-1 e 760 mm de irrigação) e infinita (na interseção das retas de 125 kg de N ha-1 e 390 mm de irrigação). A quantidade de água e nitrogênio de menor custo para produzir 160 Mg ha-1 foi 390 mm de irrigação e 112 kg de N ha-1. A regressão polinomial de segundo grau apresentou ajuste médio (r2 = 62%) para a produtividade agrícola em relação às lâminas de irrigação e doses de nitrogênio. A resposta da cana-de-açúcar à adubação nitrogenada aumenta em proporção direta com disponibilidade hídrica do solo.

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Conselho Nacional de Desenvolvimento Científico e Tecnológico (CNPq)

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Evaluated the evapotranspiration (ETc) and the efficiency of water use (USA) by the fig tree 'Purple Valinhos' submitted to irrigation and mulching (bagacilho of sugar cane crushed) in the first production cycle, at conditions of Botucatu, St. Paul. We used the method of soil water balance and to obtain the reference evapotranspiration method was used Montheit FAO Penman 56. For the assessment of crop coefficients (kc) we adopted the following phenological distribution: phase 1 - between transplanting and 20% of the vegetative (DV), ii) phase 2 - 20 to 80% DV, and iii) phase 3 - fruiting. Observe the cumulative ETc 409.4 and 465.8 mm in 254 days after transplanting (DAT) and averages of 1.47 and 1.67 mm day(-1), with and without mulching (CC and SC). The crop coefficients (kc) mediums were 0.16, 0.43 and 0.49 for SC and 0.18, 0.44 and 0.50 for CC, in phases 1 and 3, respectively. The EUA values decrease with increasing the volume of water received and ranged between 1.65 and 3.32 kg of green figs per m(3) of water for irrigated SC and CC.

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Based on the fierce competitiveness of manufacturing companies and the planning problems arising from the lack of flexibility and forecasting demand, companies are increasingly looking to reflect on the most appropriate methods to manage its manufacture. Today it is possible to obtain higher gains and lower costs through very efficient tools, this paper uses action-research to model and implement the physical layout of a manufacturing cell, with strong theoretical basement returned to Lean Production System and acting systematically in flexibility in mounting. Through observation and joint action of the observer and staff can report problems that occurred during the phases of planning and implementation of improvements. With the improvement of the physical arrangement in the assembly was possible to obtain significant gains by reducing the production cycle, the manpower required, spending of non-compliance and increasing productivity, final product quality and health in the workplace

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This study aims to prove the economic feasibility of the installation of mechanical compression chillers on plastic injection molding machines in order to reduce the production cycle time of toothbrush cables in a specific case study. This evidence was confirmed by the comparative analysis of the system replaced and the new system installed. The old system had only one closed loop cooling tower which pumped chilled water to the injection molds, and the new system has the same tower sending cold water to the condensers of individual chillers installed on each injection machine. We conducted an analysis of energy efficiency in each system, showing that in terms of thermal efficiency virtually nothing has changed, but in terms of electricity demand the new system consumes 60.3 kW more. We conducted an analysis of machine productivity for both systems, showing a much higher productivity of the new system due to reduced cycle times caused by the presence of chillers and their greater cooling capacities. Equipped with data such as electricity rates, increases in operating costs and initial investments, the increase in consumption and demand of electricity plus the cycle time reduction were also calculated over so the simple payback 1 year and 2 months was reached