50 resultados para siphon


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Classical conditioning of Aplysia's siphon-withdrawal reflex is thought to be due to a presynaptic mechanism-activity-dependent presynaptic facilitation of sensorimotor connections. Recent experiments with sensorimotor synapses in dissociated cell culture, however, provide an alternative cellular mechanism for classical conditioning-Hebbian long-term potentiation (LTP) of sensorimotor connections. Induction of Hebbian LTP of these connections is mediated by activation of N-methyl-D-aspartate-related receptors and requires the postsynaptic elevation of intracellular Ca2+. To determine whether the enhancement of sensorimotor synapses during classical conditioning in Aplysia-like LTP of sensorimotor synapses in culture-also depends upon the elevation of postsynaptic Ca2+, we carried out experiments involving the cellular analog of classical conditioning of siphon withdrawal. We examined changes in the strength of monosynaptic siphon sensorimotor connections in the abdominal ganglion of Aplysia following paired presentations of sensory neuron activation and tail nerve shock. This training regimen resulted in significant enhancement of the monosynaptic sensorimotor excitatory postsynaptic potential, as compared with the sensorimotor excitatory postsynaptic potential in preparations that received only test stimulation. Infusing the motor neuron with 1,2-bis(2-aminophenoxy)ethane-N,N-N',N'-tetraacetic acid, a specific chelator of intracellular Ca2+, prior to paired stimulation training blocked this synaptic enhancement. Our results implicate a postsynaptic, possibly Hebbian, mechanism in classical conditioning in Aplysia.

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Hydrocephalus is a condition commonly encountered in paediatric and adult neurosurgery and cerebrospinal fluid (CSF) shunting remains the treatment of choice for many cases. Despite improvements in shunt technology and technique, morbidity and mortality remain. The incidence of early shunt obstruction is high with later failures seen less frequently. This review aims to examine mortality associated with mechanical failure of CSF shunts within Queensland. Neurosurgical and Intensive Care databases were reviewed for cases of mortality associated with shunt failure. Eight cases were identified between the years of 1992 and 2002 with the average age at death 7.7 years. Deaths occurred on average 2 years after last shunt revision. Seven of the eight patients lived outside the metropolitan area. Shunting remains an imperfect means of treating hydrocephalus. Mortality may be encountered at any time post surgery and delays to surgical intervention influence this. Alternative measures such as third ventriculostomy or the placement of a separate access device should be considered. In the event of emergency, a spinal needle could be used to access the ventricle along the course of the ventricular catheter. (C) 2004 Elsevier Ltd. All rights reserved.

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A new instrument and method are described that allow the hydraulic conductivities of highly permeable porous materials, such as gravels in constructed wetlands, to be determined in the field. The instrument consists of a Mariotte siphon and a submersible permeameter cell with manometer take-off tubes, to recreate in-situ the constant head permeameter test typically used with excavated samples. It allows permeability to be measured at different depths and positions over the wetland. Repeatability obtained at fixed positions was good (normalised standard deviation of 1–4%), and results obtained for highly homogenous silica sand compared well when the sand was retested in a lab permeameter (0.32 mm.s–1 and 0.31 mm.s–1 respectively). Practical results have a ±30% associated degree of uncertainty because of the mixed effect of natural variation in gravel core profiles, and interstitial clogging disruption during insertion of the tube into the gravel. This error is small, however, compared to the orders of magnitude spatial variations detected. The technique was used to survey the hydraulic conductivity profile of two constructed wetlands in the UK, aged 1 and 15 years respectively. Measured values were high (up to 900 mm.s –1) and varied by three orders of magnitude, reflecting the immaturity of the wetland. Detailed profiling of the younger system suggested the existence of preferential flow paths at a depth of 200 mm, corresponding to the transition between more coarse and less coarse gravel layers (6–12 mm and 3–6 mm respectively), and transverse drift towards the outlet.

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The objective of the work is to develop a fuel delivery system for potable direct methanol fuel cell. Currently, one of the most fundamental limitations of direct methanol fuel cells is that the fuel supplied to the anode of the DMFC must be a very dilute aqueous methanol solution (usually 0.5∼1.5 M). If a DMFC is filled with a dilute aqueous methanol solution, the fuel cell operation time per refuel would be very short, which would considerably diminish the advantage of a DMFC over a conventional battery. To overcome this difficulty, a complex fuel delivery system based on the modern micro system technology was proposed by the author. The proposed fuel delivery system would include micro-pumps, a methanol sensor, and a control unit. The fuel delivery system adds considerable costs to the fuel cell system and consume considerable amount of electricity from the fuel cell, which in turn significantly reduces the net power output of the fuel cell. As a result, the DMFC would have tremendous difficulty to compete with the conventional battery technology in terms of costs and power output. ^ This work presents a novel passive fuel delivery system for direct methanol fuel cells. In this particular system, a methanol fuel and an aqueous methanol solution are stored separately in two containers and a wick is disposed between the two containers in a siphon fashion, with the container of the aqueous methanol solution communicating with the anode of the DMFC. Methanol is siphoned from the methanol container to the aqueous solution container in-situ when the methanol in the aqueous methanol solution is consumed during the operation of the fuel cell. Through a proper selection of the wick and the containers, the methanol concentration near the anode of the DMFC could be maintained within a preferable range. ^

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The life history of a population of Lutraria lutraria in a depth of 7m at Hunterston, Ayrshire is discussed. Much of the present population Is thought to have settled in 1967. The functional morphology of Lutraria is described and related to its life as a large, deep-burrowing bivalve. Lutraria spawned in late spring and continued to do so through the summer in 1979 and 1980. Animals became spent in August and September. Unsuccessful attempts were made to induce spawning in the laboratory. Artificial fertilization was successful but development did not proceed beyond the ciliated gastrula stage. Larvae of Lutraria were not identified in plankton samples and young stages were not encountered in sieved sediment samples. The biochemical cycle of the total animal and five component parts (gonad and visceral mass, digestive gland, adductor muscle, siphon and 'other' tissue) is investigated. A marked increase in weight, reflected in an increase in weight of the component parts, was recorded in Autumn 1979. This is thought to be related to an exceptional increase in the phytoplankton at this time. Although a relationship between the biochemical cycle and reproductive cycle remains uncertain, definite seasonal changes were recorded in the respiration rate of Lutraria. At 10°C, the maximum rate of a standard 20g animal was 0.1283m1s 02/g. dry wt./hr. in May 1980 and the minimum rate was 0.O59mls 02/g. dry wt./hr. in October 1980. The effect of temperature on respiration rate was also investigated. Significant differences were recorded for five experimental temperatures (10°C, 15°C, 20°C, 25°C and 30 °C) in August and October but only between two temperatures (10 C and 30 C) in April. There was a decrease in respiration rate at 30 C in August and October, but an increase in April. Respiration rate is affected by a reduction in oxygen tension. A variety of responses were recorded with a small degree of regulation shown. Individuals of Lutraria were able to survive 48 hours under anaerobic conditions. In fully oxygenated conditions heart rate ranged from 4-15 beats per minute with an average of 8 beats per minute. Heart beat was markedly affected by changes in temperature and oxygen tension, increasing to a maximum 22 beats per minute at 25 C, and decreasing to a minimum 2 beats per minute in anaerobic conditions. Heart rate is reduced (12 beats per minute to 5 beats per minute) on exposure to air. Lutraria exhibits an intermittent pattern of pumping activity. Under normal conditions 35% of the time is spent pumping and this Increases as oxygen is reduced (3.00mls 02/litre) to 65% of the time spent pumping. 15. Under normal conditions the respiratory flow varies between 0.382 litres per hour and 1.023 litres per hxir. Adult Lutraria maintain their ability to burrow, albeit slowly.