865 resultados para real interest rate, marginal product of capital, IS curve.


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Statement of problem. Prosthetic restorations that fit poorly may affect periodontal health and occlusion. Studies that have evaluated the accuracy of fit of ceramic restorations before and after cementation assessed primarily intracoronal restorations.Purpose. This in vitro study evaluated the effect of different finish lines, ceramic manufacturing techniques, and luting agents on the vertical discrepancy of ceramic copings.Material and methods. Two stainless steel molars were prepared for complete crowns with 2 different finish lines (heavy chamfer and rounded shoulder); each molar was duplicated to fabricate 90 copings. A total of 180 copings generated 18 groups (n=10 for each finish line-coping material-luting agent combination). Luting agents tested included zinc phosphate, resin-modified glass ionomer (Fuji Plus), and resin composite cements (Panavia F). A metal frame was developed on which to screw the stainless steel model and a ceramic coping; the distance (mum) between 2 predetermined points was measured before and after cementation by a profile projector under a torquing force. A 4-way ANOVA with repeated measurements was performed to assess the influence of each factor in the vertical marginal discrepancy: 3 between-coping factors (finish line-coping material-luting agent) and 1 within-coping factor (before and after cementation) (alpha=.05).Results. Procera copings presented the lowest mean values (P<.05) of vertical marginal discrepancy before and after cementation (25/44 mum) when compared to Empress 2 (68/110 mum) and InCeram Alumina copings (57/117 mum), regardless of any combinations among all finish lines and luting agents tested.Conclusion. Considering each factor separately, the ceramic manufacturing technique appeared to be the most important factor tested for the definitive vertical discrepancy of all-ceramic copings, with lower mean values for Procera copings.

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Recently a protocol was developed that precisely synchronizes the time of ovulation in lactating dairy cows (Ovsynch; GnRH-7d-PGF(2 alpha)-2d-GnRH). We evaluated whether initiation of Ovsynch on different days of the estrous cycle altered the effectiveness of this protocol. The percentage of cows (n=156) ovulating to the first GnRH was 64% and varied (P<0.01) by stage of estrous cycle. Treatment with PGF(2 alpha) was effective, with 93% of cows having low progesterone at second GnRH. The overall percentage of cows that ovulated after second GnRH (synchronization rate) was 87% and varied by response to first GnRH (92% if ovulation to first GnRH vs 79% if no ovulation; P<0.05). There were 6% of cows that ovulated before the second injection of GnRH and 7% with no detectable ovulation by 48 h after second GnRH. Maximal diameter of the ovulatory follicle varied by stage of estrous cycle, with cows in which Ovsynch was initiated at midcycle having the smallest follicles. In addition, milk production and serum progesterone concentration on the day of PGF(2 alpha) affected (P<0.05) size of the ovulatory follicle. Using these results we analyzed pregnancy rate at Days 28 and 98 after Al for cows (n=404) in which Ovsynch was initiated on known days of the estrous cycle. Pregnancy rate was lower for cows expected to ovulate larger follicles than those expected to ovulate smaller follicles (P<0.05; 32 vs 42%). Thus, although overall synchronization rate with Ovsynch was above, 85%, there were clear differences in response according to day of protocol initiation. Cows in which Ovsynch was initiated near midcycle had smaller ovulatory follicles and greater pregnancy rates. (C) 1999 by Elsevier B.V.

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Objectives: This study evaluated the marginal gaps on several surfaces of onlays created with the Cerec 3D system using one intraoral and two extraoral optical impression methods. Methods: A human molar (#19) was mounted with its adjacent teeth on a typodont (Frasaco) and prepared for a MODL onlay. The typodont was assembled in the mannequin head in order to simulate clinical conditions. The same operator took 36 individual optical impressions using a CEREC 3D camera. For group 1 (IP), a thin layer of titanium dioxide powder (CEREC powder-VITA) was applied directly onto the surface of the preparation for imaging (n=12). For group 2 (EP), a sectional impression was taken with hydrocolloid Identic Syringable (Dux Dental), a die made with polyvinylsiloxane KwikkModel Scan (R-dental Dentalerzeugnisse GmbH) and powdered with titanium dioxide for imaging (n=12). For group 3 (ES), a sectional impression was taken with PVS and a sectional stock tray, a die fabricated in stone (Diamond die- HI-TEC Dental Products) and the die being imaged without powdering (n=12). One operator designed and machined the onlays in Vita Blocks Mark II for Cerec (VITA) using a CEREC 3D. The marginal gaps (pm) were measured with an optical microscope (50x) at 12 points, three on each surface of the MODL. The results were analyzed by two-way ANOVA/Tukey's (p=0.05). Results: The overall mean marginal gaps (mu m) for the three methods were: IP=111.6 (+/- 34.0); EP=161.4 (+/- 37.6) and ES=116.8 (+/- 42.3). IP and ES were equal, but both were significantly less than EP. The pooled mean marginal gaps (mu m) for the occlusal = 110.5 (+/- 39) and lingual = 111.5 (+/- 30.5) surfaces were equivalent and significantly less than the distal = 136.5 (+/- 42.5) and mesial = 161.1 (+/- 43.3). Conclusion: The marginal gap of CEREC 3D onlay restorations was not different when the optical impression was taken intraorally vs extraorally using a stone cast that does not require powdering. The lingual and occlusal surfaces showed the lowest gaps.

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OBJECTIVE: To evaluate the influence of cavity design and photocuring method on the marginal seal of resin composite restorations. METHOD AND MATERIALS: Seventy-two bovine teeth were divided into 2 groups: group 1 received box-type cavity preparations, and group 2 received plate-type preparations. Each group was divided into 3 subgroups. After etching and bonding, Z250 resin composite (3M Espe) was applied in 2 equal increments and cured with 1 of 3 techniques: (1) conventional curing for 30 seconds at 650 mW/cm2; (2) 2-step photocuring, in which the first step was performed 14 mm from the restoration for 10 seconds at 180 mW/cm2 and the second step was performed in direct contact for 20 seconds at 650 mW/cm2; or (3) progressive curing using Jetlite 4000 (J. Morita) for 8 seconds at 125 mW/cm2 and then 22 seconds at 125 mW/cm2 up to 500 mW/cm2. The specimens were thermocycled for 500 cycles and then submitted to dye penetration with a 50% silver nitrate solution. Microleakage was assessed using a stereomicroscope. Data were analyzed using analysis of variance and Tukey test (5% level of significance). RESULTS: A statistically significant difference was found between groups when a double interaction between photocuring and cavity preparation was considered (P = .029). CONCLUSIONS: No one type of cavity preparation or photocuring method prevented micro-leakage. The plate-type preparation showed the worst dye penetration when conventional and progressive photocuring methods were used. The best results were found using the 2-step photocuring with the plate-type preparation.

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Objectives: This study assessed the effect of cast rectifiers on the marginal misfit of cast UCLA abutments compared to premachined UCLA abutments. The influence of casting and porcelain baking on the marginal misfit of these components was also investigated. Methods: Two groups were analyzed: test group - 10 cast UCLA abutments, finished with cast rectifier and submitted to ceramic application; control group - 10 premachined UCLA abutments, cast with noble metal alloy and submitted to ceramic application. Vertical misfit measurements were performed under light microscopy. In the test group, measurements were performed before and after the use of cast rectifiers, and after ceramic application. In the control group, measurements were performed before and after casting, and after ceramic application. Data were submitted to statistical analysis by ANOVA and Tukey's test (α= 5%). Results: The use of cast rectifiers significantly reduced the marginal misfit of cast UCLA abutments (from 25.68μm to 14.83μm; p<0.05). After ceramic application, the rectified cylinders presented misfit values (16.18μm) similar to those of premachined components (14.3 μm). Casting of the premachined UCLA abutments altered the marginal misfit of these components (from 9.63 μm to 14.6 μm; p<0.05). There were no significant changes after porcelain baking, in both groups. Conclusion: The use of cast rectifiers reduced the vertical misfit of cast UCLA abutments. Even with carefully performed laboratory steps, changes at the implant interface of premachined UCLA abutments occurred. Ceramic application did not alter the marginal misfit values of UCLA abutments.

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The objective of this study was to assess the effects of an activating solution on the sperm motility duration (SMD) of 'curimbatá', Prochilodus lineatus through of the definition of qualitative and quantitative parameters of the semen pool used in the experiment; evaluation of the effects of different ratios of semen dilution corresponding to 1-:-1, 1-:-2, 1-:-20, 1-:-200, 1-:-2000, 1-:-20-000 and 1-:-100-000 semen:dilute solution on the SMD and, assessment of the effects of different temperatures of the activating solution (5, 10, 15, 20, 25, 30, 35, 40, 45 and 50°C) on the SMD. The results of SMD were directly proportional to the dilution (P<0.05), starting from the dilution of 1-:-2 (semen:water), with 23.04-s. Were used three replicates of the semen pool for each test. Two-year-old brookstock were maintained in ponds culture conditions. In November-December 2006, twelve mature males broodfish were selected (mean weight and length of 405.8±134.2-g and 25.6±3.1-cm, respectively). The males released that semen under slight pressure of the urogenital papilla were selected for the experiment. The SMD increased proportionally to the increase in dilution, until it reached a maximum of 28.83-s for the ratio 1-:-100-000 semen: dilute solution. The results of SMD in relation to the temperature of the activating solution exhibited a quadratic behavior (P<0.05) with a maximum theoretical performance in terms of sperm motility duration of 21.36-s at a temperature of 17.3°C. Thus, for the species considered, the increase in the dilution ratio proved favorable for the rise in motility duration until the maximum value studied of 1-:-100-000 semen:dilute solution. As for the temperature of the activating solution, the best results of SMD were obtained at the temperature of 17.3°C. At higher temperatures used in the experiment (25, 30, 35, 40, 45 and 50°C), a decrease in motility duration. © 2010 Blackwell Verlag, Berlin.

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