1000 resultados para Hollow Section Joints
Resumo:
Bridge deck expansion joints are used to allow for movement of the bridge deck due to thermal expansion, dynamics loading, and other factors. More recently, expansion joints have also been utilized to prevent the passage of winter de-icing chemicals and other corrosives applied to bridge decks from penetrating and damaging substructure components of the bridge. Expansion joints are often one of the first components of a bridge deck to fail and repairing or replacing expansion joints are essential to extending the life of any bridge. In the Phase I study, the research team focused on the current means and methods of repairing and replacing bridge deck expansion joints. Research team members visited with Iowa Department of Transportation (DOT) Bridge Crew Leaders to document methods of maintaining and repairing bridge deck expansion joints. Active joint replacement projects around Iowa were observed to document the means of replacing expansion joints that were beyond repair, as well as, to identify bottlenecks in the construction process that could be modified to decrease the length of expansion joint replacement projects. After maintenance and replacement strategies had been identified, a workshop was held at the Iowa State Institute for Transportation to develop ideas to better maintain and replace expansion joints. Maintenance strategies were included in the discussion as a way to extend the useful life of a joint, thus decreasing the number of joints replaced in a year and reducing the traffic disruptions.
Resumo:
If adequately designed and high quality material and good construction practices are used, portland cement concrete is very durable. This is demonstrated by the oldest pavement in Iowa (second oldest in the U.S.) paved in 1904, which performed well for 70 years without resurfacing. The design thickness is an important factor in both the performance and cost of pavement. The objective of this paper is to provide a 30-year performance evaluation of a pavement constructed to determine the required design thickness for low volume secondary roadways. In 1951 Greene County and the Iowa Highway Research Board of the Iowa Department of Transportation initiated a four-mile (6.4 km) demonstration project to evaluate thicknesses ranging from 4-1/2" (11.4 cm) to 6" (15.2 cm). The project, consisting of 10 research sections, was formed pavement placed on a gravel roadbed with very little preparation except for redistribution of the loose aggregate. Eight sections were non-reinforced except for centerline tie bars and no contraction joints were used. Mesh reinforcing and contraction joints spaced at 29' 7" (9.02 m) intervals were used in two 4-1/2" (11.4 cm) thick sections. The only air entrained section was non-reinforced. The pavement performed well over its 30-year life carrying a light volume of traffic and did not require major maintenance. There was substantial cracking with average slab length varying directly with thickness. The 4-1/2" (11.4 cm) thick non-air entrained, mesh-reinforced pavement with contraction joints has performed the best.
Resumo:
The previous research performed laboratory experiments to measure the impacts of the curing on the indirect tensile strength of both CIR-foam and CIR-emulsion mixtures. However, a fundamental question was raised during the previous research regarding a relationship between the field moisture content and the laboratory moisture content. Therefore, during this research, both temperature and moisture conditions were measured in the field by embedding the sensors at a midpoint and a bottom of the CIR layer. The main objectives of the research are to: (1) measure the moisture levels throughout a CIR layer and (2) develop a moisture loss index to determine the optimum curing time of CIR layer before HMA overlay. To develop a set of moisture loss indices, the moisture contents and temperatures of CIR-foam and CIR-emulsion layers were monitored for five months. Based on the limited field experiment, the following conclusions are derived: 1. The moisture content of the CIR layer can be monitored accurately using the capacitance type moisture sensor. 2. The moisture loss index for CIR layers is a viable tool in determining the optimum timing for an overlay without measuring actual moisture contents. 3. The modulus back-calculated based on the deflection measured by FWD seemed to be in a good agreement with the stiffness measured by geo-gauge. 4. The geo-gauge should be considered for measuring the stiffness of CIR layer that can be used to determine the timing of an overlay. 5. The stiffness of CIR-foam layer increased as a curing time increased and it seemed to be more influenced by a temperature than moisture content. The developed sets of moisture loss indices based on the field measurements will help pavement engineers determine an optimum timing of an overlay without continually measuring moisture conditions in the field using a nuclear gauge.
Resumo:
There is an ongoing drive towards improvements and achieving success in effective and long term sealing of portland cement concrete pavement contraction joints. A variety of joint sealing products and procedures have been applied in Iowa in search of improvements in seal performance. Hot poured rubberized asphalt products were mainly used for sealing all joints in earlier years for highways. In the 1980s, silicone sealant products were becoming popular, especially for the major highways. As a high level of sealant performance was not achieved from silicones in Iowa conditions, other sealing products were tried. Preformed neoprene compression seals are being tried as a substitution for silicone sealants. Due to high costs of materials and installation with neoprene seals, the search for improvements through other joint sealing products and procedures continued. An agreement was made with Phoenix, North America, Inc., to provide and install preformed Ethylene Propylene Diene Monomer (EPDM) compression joint seals. The research site was a 600 ft (183 m) test section of northbound I-29 in Pottawattamie County, Iowa. Seal installation was done August 20, 1992. Seal performance has been good over the past seven years and the seals are still showing no significant signs of decreasing performance.