1000 resultados para Bed dip direction
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In this study it was evaluated the start-up procedures of anaerobic treatment system with three horizontal anaerobic reactors (R1, R2 and R3), installed in series, with volume of 1.2 L each. R1 had sludge blanket, and R2 and R3 had half supporter of bamboo and coconut fiber, respectively. As an affluent, it was synthesized wastewater from mechanical pulping of the coffee fruit by wet method, with a mean value of total chemical oxygen demand (CODtotal) of 16,003 mg L-1. The hydraulic retention time (HRT) in each reactor was 30 h. The volumetric organic loading (VOL) applied in R1 varied from 8.9 to 25.0 g of CODtotal (L d)-1. The mean removal efficiencies of CODtotal varied from 43 to 97% in the treatment system (R1+R2+R3), stabilizing above 80% after 30 days of operation. The mean content of methane in the biogas were of 70 to 76%, the mean volumetric production was 1.7 L CH4 (L reactor d)-1 in the system, and the higher conversions were around at 0.20 L CH4 (g CODremoved)-1 in R1 and R2. The mean values of pH in the effluents ranged from 6.8 to 8.3 and the mean values of total volatile acids remained below 200 mg L-1 in the effluent of R3. The concentrations of total phenols of the affluent ranged from 45 to 278 mg L-1, and the mean removal efficiency was of 52%. The start-up of the anaerobic treatment system occurred after 30 days of operation as a result of inoculation with anaerobic sludge with active microbiota.
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Attempting to associate waste treatment to the production of clean and renewable energy, this research sought to evaluate the biological production of hydrogen using wastewater from the cassava starch treatment industry, generated during the processes of extraction and purification of starch. This experiment was carried out in a continuous anaerobic reactor with a working volume of 3L, with bamboo stems as the support medium. The system was operated at a temperature of 36°C, an initial pH of 6.0 and under variations of organic load. The highest rate of hydrogen production, of 1.1 L.d-1.L-1, was obtained with application of an organic loading rate of 35 g.L-1.d-1, in terms of total sugar content and hydraulic retention time of 3h, with a prevalence of butyric and acetic acids as final products of the fermentation process. Low C/N ratios contributed to the excessive growth of the biomass, causing a reduction of up to 35% in hydrogen production, low percentages of H2 and high concentrations of CO2in the biogas.
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1854/11/01 (A1,N2).
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1855/02/20 (N9).
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1854/12/01 (A1,N4).
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1855/03/05 (N10).
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1854/11/15 (A1,N3).
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1855/02/05 (N8).
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1855/01/20 (N7).
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1855/01/01 (N6).
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1854/12/15 (A1,N5).
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Variante(s) de titre : État religieux de la France et de l'Europe, d'après les sources les plus authentiques, avec les controverses sur la séparation de l'Église et de l'État...
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17 x 21 cm
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In this thesis, a model called CFB3D is validated for oxygen combustion in circulating fluidized bed boiler. The first part of the work consists of literature review in which circulating fluidized bed and oxygen combustion technologies are studied. In addition, the modeling of circulating fluidized bed furnaces is discussed and currently available industrial scale three-dimensional furnace models are presented. The main features of CFB3D model are presented along with the theories and equations related to the model parameters used in this work. The second part of this work consists of the actual research and modeling work including measurements, model setup, and modeling results. The objectives of this thesis is to study how well CFB3D model works with oxygen combustion compared to air combustion in circulating fluidized bed boiler and what model parameters need to be adjusted when changing from air to oxygen combustion. The study is performed by modeling two air combustion cases and two oxygen combustion cases with comparable boiler loads. The cases are measured at Ciuden 30 MWth Flexi-Burn demonstration plant in April 2012. The modeled furnace temperatures match with the measurements as well in oxygen combustion cases as in air combustion cases but the modeled gas concentrations differ from the measurements clearly more in oxygen combustion cases. However, the same model parameters are optimal for both air and oxygen combustion cases. When the boiler load is changed, some combustion and heat transfer related model parameters need to be adjusted. To improve the accuracy of modeling results, better flow dynamics model should be developed in the CFB3D model. Additionally, more measurements are needed from the lower furnace to find the best model parameters for each case. The validation work needs to be continued in order to improve the modeling results and model predictability.