996 resultados para tip leakage flow


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This paper describes a computer code aimed at solving the equations of three dimensional viscous compressible flow in turbomachine geometries. The code is applied to the study of the flowfield in a transonic axial compressor rotor at design speed at both maximum flow and towards stall. The predicted flowfield is compared with the laser measurements and the performance of the code discussed. In addition the discussion highlights the change in the predicted endwall and tip clearance flows as the rotor operating point is moved towards stall.

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This paper describes both the migration and dissipation of flow phenomena downstream of a transonic high-pressure turbine stage. The geometry of the HP stage exit duct considered is a swan-necked diffuser similar to those likely to be used in future engine designs. The paper contains results both from an experimental programme in a turbine test facility and from numerical predictions. Experimental data was acquired using three fast-response aerodynamic probes capable of measuring Mach number, whirl angle, pitch angle, total pressure and static pressure. The probes were used to make time-resolved area traverses at two axial locations downstream of the rotor trailing edge. A 3D time-unsteady viscous Navier-Stokes solver was used for the numerical predictions. The unsteady exit flow from a turbine stage is formed from rotordependent phenomena (such as the rotor wake, the rotor trailing edge recompression shock, the tip-leakage flow and the hub secondary flow) and vane-rotor interaction dependant phenomena. This paper describes the time-resolved behaviour and three-dimensional migration paths of both of these phenomena as they convect downstream. It is shown that the inlet flow to a downstream vane is dominated by two corotating vortices, the first caused by the rotor tip-leakage flow and the second by the rotor hub secondary flow. At the inlet plane of the downstream vane the wake is extremely weak and the radial pressure gradient is shown to have caused the majority of the high loss wake fluid to be located between the mid-height of the passage and the casing wall. The structure of the flow indicates that between a high pressure stage and a downstream vane simple two-dimensional blade row interaction does not occur. The results presented in this paper indicate that the presence of an upstream stage is likely to significantly alter the structure of the secondary flow within a downstream vane. The paper also shows that vane-rotor interaction within the upstream stage causes a 10° circumferential variation in the inlet flow angle of the 2nd stage vane.

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This paper provides a physical interpretation of the mechanism of stagnation enthalpy and stagnation pressure changes in turbomachines due to unsteady flow, the agency for all work transfer between a turbomachine and an inviscid fluid. Examples are first given to illustrate the direct link between the time variation of static pressure seen by a given fluid particle and the rate of change of stagnation enthalpy for that particle. These include absolute stagnation temperature rises in turbine rotor tip leakage flow, wake transport through downstream blade rows, and effects of wake phasing on compressor work input. Fluid dynamic situations are then constructed to explain the effect of unsteadiness, including a physical interpretation of how stagnation pressure variations are created by temporal variations in static pressure; in this it is shown that the unsteady static pressure plays the role of a time-dependent body force potential. It is further shown that when the unsteadiness is due to a spatial nonuniformity translating at constant speed, as in a turbomachine, the unsteady pressure variation can be viewed as a local power input per unit mass from this body force to the fluid particle instantaneously at that point. © 2012 American Society of Mechanical Engineers.

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Off-design performance is of key importance now in the design of automotive turbocharger turbines. Due to automotive drive cycles, a turbine that can extract more energy at high pressure ratios and lower rotational speeds is desirable. Typically a radial turbine provides peak efficiency at U/C values of 0.7, but at high pressure ratios and low rotational speeds, the U/C value will be low and the rotor will experience high values of positive incidence at the inlet. The positive incidence causes high blade loading resulting in additional tip leakage flow in the rotor as well as flow separation on the suction surface of the blade. An experimental assessment has been performed on a scaled automotive VGS (variable geometry system). Three different stator vane positions have been analyzed: minimum, 25%, and maximum flow position. The first tests were to establish whether positioning the endwall clearance on the hub or shroud side of the stator vanes produced a different impact on turbine efficiency. Following this, a back swept rotor was tested to establish the potential gains to be achieved during off-design operation. A single passage CFD model of the test rig was developed and used to provide information on the flow features affecting performance in both the stator vanes and turbine. It was seen that off-design performance was improved by implementing clearance on the hub side of the stator vanes rather than on the shroud side. Through CFD analysis and tests, it was seen that two leakage vortices form, one at the leading edge and one after the spindle of the stator vane. The vortices affect the flow angle at the inlet to the rotor, in the hub region. The flow angle is shifted to more negative values of incidence, which is beneficial at the off-design conditions but detrimental at the design point. The back swept rotor was tested with the hub side stator vane clearance configuration. The efficiency and MFR were increased at the minimum and 25% stator vane position. At the design point, the efficiency and MFR were decreased. The CFD investigation showed that the incidence angle was improved at the off-design conditions for the back swept rotor. This reduction in the positive incidence angle, along with the improvement caused by the stator vane tip leakage flow, reduced flow separation on the suction surface of the rotor. At the design point, both the tip leakage flow of the stator vanes and the back swept blade angle caused flow separation on the pressure surface of the rotor. This resulted in additional blockage at the throat of the rotor reducing MFR and efficiency.

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Conventionally, radial turbines have almost exclusively used radially fibred blades. While issues of mechanical integrity are paramount, there may be opportunities for improving turbine efficiency through a 3D blade design without exceeding mechanical limits. Off-design performance and understanding of the secondary flow structures now plays a vital role in the design decisions made for automotive turbocharger turbines. Of particular interest is extracting more energy at high pressure ratios and lower rotational speeds. Operating in this region means the rotor will experience high values of positive incidence at the inlet. A CFD analysis has been carried out on a scaled automotive turbine utilizing a swing vane stator system. To date no open literature exists on the flow structures present in a standard VGT system. Investigations were carried out on a 90 mm diameter rotor with the stator vane at the maximum, minimum and 25% mass flow rate positions. In addition stator vane endwall clearance existed at the hub side. From investigation of the internal flow fields of the baseline rotor, a number of areas that could be optimized in the future with three dimensional blading were identified. The blade loading and tip leakage flow near inlet play a significant role in the flow development further downstream at all stator vane positions. It was found that tip leakage flow and flow separation at off-design conditions could be reduced by employing back swept blading and redistributing the blade loading. This could potentially reduce the extent of the secondary flow structures found in the present study.

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The interaction between a high-pressure rotor and a downstream vane is dominated by vortex-blade interaction. Each rotor blade passing period two co-rotating vortex pairs, the tip-leakage and upper passage vortex and the lower passage and trailing shed vortex, impinge on, and are cut by, the vane leading edge. In addition to the streamwise vortex the tip-leakage flow also contains a large velocity deficit. This causes the interaction of the tip-leakage flow with a downstream vane to differ from typical vortex blade interaction. This paper investigates the effect these interaction mechanisms have on a downstream vane. The test geometry considered was a low aspect ratio second stage vane located within a S-shaped diffuser with large radius change mounted downstream of a shroudless high-pressure turbine stage. Experimental measurements were conducted at engine-representative Mach and Reynolds numbers, and data was acquired using a fast-response aerodynamic probe upstream and downstream of the vane. Time-resolved numerical simulations were undertaken with and without a rotor tip gap in order to investigate the relative magnitude of the interaction mechanisms. The presence of the upstream stage is shown to significantly change the structure of the secondary flow in the vane and to cause a small drop in its performance.

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This paper considers the effect of the rotor tip on the casing heat load of a transonic axial flow turbine. The aim of the research is to understand the dominant causes of casing heat-transfer. Experimental measurements were conducted at engine-representative Mach number, Reynolds number and stage inlet to casing wall temperature ratio. Time-resolved heat-transfer coefficient and gas recovery temperature on the casing were measured using an array of heat-transfer gauges. Time-resolved static pressure on the casing wall was measured using Kulite pressure transducers. Time-resolved numerical simulations were undertaken to aid understanding of the mechanism responsible for casing heat load. The results show that between 35% and 60% axial chord the rotor tip-leakage flow is responsible for more than 50% of casing heat transfer. The effects of both gas recovery temperature and heat transfer coefficient were investigated separately and it is shown that an increased stagnation temperature in the rotor tip gap dominates casing heat-transfer. In the tip gap the stagnation temperature is shown to rise above that found at stage inlet (combustor exit) by as much as 35% of stage total temperature drop. The rise in stagnation temperature is caused by an isentropic work input to the tip-leakage fluid by the rotor. The size of this mechanism is investigated by computationally tracking fluid path-lines through the rotor tip gap to understand the unsteady work processes that occur. Copyright © 2005 by ASME.