999 resultados para Cogeneration systems


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Portugal é um país dependente da energia do exterior, devido à elevada percentagem de consumo de energia a partir de fontes primárias, como por exemplo o gasóleo. Para colmatar este cenário, têm vindo a criar-se incentivos para o uso de energias renováveis e para intensificação de medidas de eficiência energética, como os sistemas de cogeração, de forma a tornar os processos industriais nacionais mais autónomos e mais competitivos. O presente trabalho, centra-se na determinação do potencial térmico disponível na central de trigeração da empresa Monteiro, Ribas-Indústria, SA, com a finalidade de identificar a quantidade de energia não utilizada, com vista ao aproveitamento dessa mesma energia nos processos mais problemáticos da empresa. Verificou-se que a água líquida era a fonte de maior energia não aproveitada, representando cerca de 30%, relativamente à energia disponível na água de refrigeração que é de 1890 kW. Assim, perante este facto, fez-se um estudo em dois setores autónomos da empresa, o setor dos revestimentos e o setor dos componentes técnicos da borracha. Pretendeu-se propor medidas para melhorar os seus processos produtivos, aproveitando essa energia. Para o efeito foi projetado um permutador de calor de placas com necessidade energética de 131,4 MWh, no setor dos revestimentos e um permutador compacto no setor de produção de placas de borracha, necessitando de uma energia de 335,2 MWh. Face à energia disponível na central de trigeração, de 161,9 MWh, verifica-se que esta apenas poderá ser aproveitada no setor dos revestimentos. Para tornar este objetivo real, a empresa Monteiro, Ribas- Indústria, SA necessitaria de efetuar um investimento no total de 49.390€. Além disso, foi contabilizado o rendimento das caldeiras da central térmica e da cogeração, ambas pelo método direto, apresentando estas os valores de 72% e 42%, respectivamente.

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The present Master dissertation is a project whose main objective is to identify value creation opportunities through fuel switching in the Portuguese industry, services, agriculture and fishing sectors. Fuel switching opportunities are characterized by type of fuel transition, type of technology transition, economy subsectors prone to have fuel switching and value created through fuel shift. Results suggest tomato concentrate, dairy, beer manufacturing and sugar refining subsectors is where prevalence of fuel oil steam boilers is high, for such cases conversion to natural gas steam boilers should result in operations having a ratio of NPV over CAPEX larger than ten and a payback period just under one year. Results further suggest food, beverages, textile, chemicals and wood subsectors currently operate between ten and twenty cogeneration Diesel engines that can be either modified to operate with natural gas or replaced by new natural gas cogeneration systems. Financial modeling indicates that both options have great value creation potential. The current analysis aims to be used by natural gas suppliers and energy project promoters to identify new potential deals as well as by heavy energy consumers to mitigate their energy related costs.

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Coordenação de Aperfeiçoamento de Pessoal de Nível Superior (CAPES)

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Coordenação de Aperfeiçoamento de Pessoal de Nível Superior (CAPES)

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Pós-graduação em Engenharia Mecânica - FEG

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Pós-graduação em Engenharia Mecânica - FEG

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The discussions about the energy rationalization are gaining more and more space on the everyday of engineers and other professionals in the field of energy. A greater focus is being tied to commercial buildings, because they are one of the biggest responsible for the high energetic expenditure according to the National Energetic Balance, especially by the use of air conditioners for the people’s thermal comfort. Such finding made INMETRO to develop a building labeling procedure through th National Program of Electric Energy Conservation in Buildings; by means of this systematic, the built areas are classified by levels that go from A(the best) to E(the worst), taking into account envelopment, illumination system and air conditioning. A bonus process based on water rationalization, use of renewable energy sources, cogeneration systems or technical innovations, allows the classification to be changed up to one level. A study made exactly on a commercial building, the building of Foundation for Technological and Scientific Development located inside of the College of Engineering of Guaratinguetá, sought to identify technical/economic alternatives for the building certification and appealed to the bonus based on water rationalization. The present study is based on analysis of deploying a cogeneration system formed by internal combustion engine and an absorption refrigeration system as bonus alternative, so that the costs are analyzed regarding energy consumption and use of the motor. With the calculations and results, the viability of the building to receive a bonus from INMETRO through its National Program for Energy Conservation in Buildings is studied and concluded from this study whether or not you can get a better level of energy efficiency for the building in question... (Complete abstract click electronic access below)

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In such territories where food production is mostly scattered in several small / medium size or even domestic farms, a lot of heterogeneous residues are produced yearly, since farmers usually carry out different activities in their properties. The amount and composition of farm residues, therefore, widely change during year, according to the single production process periodically achieved. Coupling high efficiency micro-cogeneration energy units with easy handling biomass conversion equipments, suitable to treat different materials, would provide many important advantages to the farmers and to the community as well, so that the increase in feedstock flexibility of gasification units is nowadays seen as a further paramount step towards their wide spreading in rural areas and as a real necessity for their utilization at small scale. Two main research topics were thought to be of main concern at this purpose, and they were therefore discussed in this work: the investigation of fuels properties impact on gasification process development and the technical feasibility of small scale gasification units integration with cogeneration systems. According to these two main aspects, the present work was thus divided in two main parts. The first one is focused on the biomass gasification process, that was investigated in its theoretical aspects and then analytically modelled in order to simulate thermo-chemical conversion of different biomass fuels, such as wood (park waste wood and softwood), wheat straw, sewage sludge and refuse derived fuels. The main idea is to correlate the results of reactor design procedures with the physical properties of biomasses and the corresponding working conditions of gasifiers (temperature profile, above all), in order to point out the main differences which prevent the use of the same conversion unit for different materials. At this scope, a gasification kinetic free model was initially developed in Excel sheets, considering different values of air to biomass ratio and the downdraft gasification technology as particular examined application. The differences in syngas production and working conditions (process temperatures, above all) among the considered fuels were tried to be connected to some biomass properties, such elementary composition, ash and water contents. The novelty of this analytical approach was the use of kinetic constants ratio in order to determine oxygen distribution among the different oxidation reactions (regarding volatile matter only) while equilibrium of water gas shift reaction was considered in gasification zone, by which the energy and mass balances involved in the process algorithm were linked together, as well. Moreover, the main advantage of this analytical tool is the easiness by which the input data corresponding to the particular biomass materials can be inserted into the model, so that a rapid evaluation on their own thermo-chemical conversion properties is possible to be obtained, mainly based on their chemical composition A good conformity of the model results with the other literature and experimental data was detected for almost all the considered materials (except for refuse derived fuels, because of their unfitting chemical composition with the model assumptions). Successively, a dimensioning procedure for open core downdraft gasifiers was set up, by the analysis on the fundamental thermo-physical and thermo-chemical mechanisms which are supposed to regulate the main solid conversion steps involved in the gasification process. Gasification units were schematically subdivided in four reaction zones, respectively corresponding to biomass heating, solids drying, pyrolysis and char gasification processes, and the time required for the full development of each of these steps was correlated to the kinetics rates (for pyrolysis and char gasification processes only) and to the heat and mass transfer phenomena from gas to solid phase. On the basis of this analysis and according to the kinetic free model results and biomass physical properties (particles size, above all) it was achieved that for all the considered materials char gasification step is kinetically limited and therefore temperature is the main working parameter controlling this step. Solids drying is mainly regulated by heat transfer from bulk gas to the inner layers of particles and the corresponding time especially depends on particle size. Biomass heating is almost totally achieved by the radiative heat transfer from the hot walls of reactor to the bed of material. For pyrolysis, instead, working temperature, particles size and the same nature of biomass (through its own pyrolysis heat) have all comparable weights on the process development, so that the corresponding time can be differently depending on one of these factors according to the particular fuel is gasified and the particular conditions are established inside the gasifier. The same analysis also led to the estimation of reaction zone volumes for each biomass fuel, so as a comparison among the dimensions of the differently fed gasification units was finally accomplished. Each biomass material showed a different volumes distribution, so that any dimensioned gasification unit does not seem to be suitable for more than one biomass species. Nevertheless, since reactors diameters were found out quite similar for all the examined materials, it could be envisaged to design a single units for all of them by adopting the largest diameter and by combining together the maximum heights of each reaction zone, as they were calculated for the different biomasses. A total height of gasifier as around 2400mm would be obtained in this case. Besides, by arranging air injecting nozzles at different levels along the reactor, gasification zone could be properly set up according to the particular material is in turn gasified. Finally, since gasification and pyrolysis times were found to considerably change according to even short temperature variations, it could be also envisaged to regulate air feeding rate for each gasified material (which process temperatures depend on), so as the available reactor volumes would be suitable for the complete development of solid conversion in each case, without even changing fluid dynamics behaviour of the unit as well as air/biomass ratio in noticeable measure. The second part of this work dealt with the gas cleaning systems to be adopted downstream the gasifiers in order to run high efficiency CHP units (i.e. internal engines and micro-turbines). Especially in the case multi–fuel gasifiers are assumed to be used, weightier gas cleaning lines need to be envisaged in order to reach the standard gas quality degree required to fuel cogeneration units. Indeed, as the more heterogeneous feed to the gasification unit, several contaminant species can simultaneously be present in the exit gas stream and, as a consequence, suitable gas cleaning systems have to be designed. In this work, an overall study on gas cleaning lines assessment is carried out. Differently from the other research efforts carried out in the same field, the main scope is to define general arrangements for gas cleaning lines suitable to remove several contaminants from the gas stream, independently on the feedstock material and the energy plant size The gas contaminant species taken into account in this analysis were: particulate, tars, sulphur (in H2S form), alkali metals, nitrogen (in NH3 form) and acid gases (in HCl form). For each of these species, alternative cleaning devices were designed according to three different plant sizes, respectively corresponding with 8Nm3/h, 125Nm3/h and 350Nm3/h gas flows. Their performances were examined on the basis of their optimal working conditions (efficiency, temperature and pressure drops, above all) and their own consumption of energy and materials. Successively, the designed units were combined together in different overall gas cleaning line arrangements, paths, by following some technical constraints which were mainly determined from the same performance analysis on the cleaning units and from the presumable synergic effects by contaminants on the right working of some of them (filters clogging, catalysts deactivation, etc.). One of the main issues to be stated in paths design accomplishment was the tars removal from the gas stream, preventing filters plugging and/or line pipes clogging At this scope, a catalytic tars cracking unit was envisaged as the only solution to be adopted, and, therefore, a catalytic material which is able to work at relatively low temperatures was chosen. Nevertheless, a rapid drop in tars cracking efficiency was also estimated for this same material, so that an high frequency of catalysts regeneration and a consequent relevant air consumption for this operation were calculated in all of the cases. Other difficulties had to be overcome in the abatement of alkali metals, which condense at temperatures lower than tars, but they also need to be removed in the first sections of gas cleaning line in order to avoid corrosion of materials. In this case a dry scrubber technology was envisaged, by using the same fine particles filter units and by choosing for them corrosion resistant materials, like ceramic ones. Besides these two solutions which seem to be unavoidable in gas cleaning line design, high temperature gas cleaning lines were not possible to be achieved for the two larger plant sizes, as well. Indeed, as the use of temperature control devices was precluded in the adopted design procedure, ammonia partial oxidation units (as the only considered methods for the abatement of ammonia at high temperature) were not suitable for the large scale units, because of the high increase of reactors temperature by the exothermic reactions involved in the process. In spite of these limitations, yet, overall arrangements for each considered plant size were finally designed, so that the possibility to clean the gas up to the required standard degree was technically demonstrated, even in the case several contaminants are simultaneously present in the gas stream. Moreover, all the possible paths defined for the different plant sizes were compared each others on the basis of some defined operational parameters, among which total pressure drops, total energy losses, number of units and secondary materials consumption. On the basis of this analysis, dry gas cleaning methods proved preferable to the ones including water scrubber technology in al of the cases, especially because of the high water consumption provided by water scrubber units in ammonia adsorption process. This result is yet connected to the possibility to use activated carbon units for ammonia removal and Nahcolite adsorber for chloride acid. The very high efficiency of this latter material is also remarkable. Finally, as an estimation of the overall energy loss pertaining the gas cleaning process, the total enthalpy losses estimated for the three plant sizes were compared with the respective gas streams energy contents, these latter obtained on the basis of low heating value of gas only. This overall study on gas cleaning systems is thus proposed as an analytical tool by which different gas cleaning line configurations can be evaluated, according to the particular practical application they are adopted for and the size of cogeneration unit they are connected to.

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En la actualidad la generación y utilización eficientes de la energía es el vector principal que permite el desarrollo sostenible en el marco ambiental, económico, seguro y rentable. Todo ello genera una necesidad en el ser humano de guiar a los avances tecnológicos hacia una manera cada vez más eficiente de generar nuestras necesidades básicas, como es el caso de la energía. La cogeneración ha sido uno de los resultados positivos en la búsqueda de la eficiencia energética, debido a tratarse de un sistema de producción simultánea de calor y electricidad partiendo inicialmente de un combustible como energía primaria. Es por ello, que en el presente proyecto se estudia, analiza y propone la posibilidad de implantar sistemas de cogeneración en el sector residencial, un sector que podría beneficiarse enormemente de los beneficios que ofrecen dichos sistemas. En una primera parte se analiza la tecnología de cogeneración y sus variantes, como son, la microcogeneración y la trigeneración. También se muestra la evolución legislativa que han sufrido estos sistemas. En una segunda parte se ha tomado un caso modelo, un edificio de 72 viviendas con sistema de calderas centralizado convencional, y se ha estudiado la posibilidad de implantar un sistema de cogeneración. Para ello se han calculado previamente las demandas energéticas del edificio y se han ido proponiendo diferentes modos de operación para cubrir dichas demandas por medio de sistemas de microcogeneración o cogeneración. Finalmente, una vez valoradas las opciones se muestra la elegida y se efectúa un análisis económico ABSTRACT Nowadays the efficient generation of energy is the main vector that allows sustainable development in environmental, economic, safety and cost effectiveness. All this generates a need in humans to lead to new technological advances towards an even more efficient way to generate our basic needs, such as energy. Cogeneration has been one of the positive results in the search for energy efficiency, due to the fact that it is a system of simultaneous production of heat and electricity initially starting from a primary energy fuel. It is for this reason that this project studies, analyzes and proposes the possibility of introducing cogeneration systems in the residential sector, a sector that could benefit greatly from the benefits offered by these systems. In the first part, cogeneration technology and its variants are analyzed, like, micro-cogeneration and trigeneration. The legislative evolutions that have suffered these systems are also displayed. In a second part, a model case has been taken; a building of 72 flats with conventional centralized boiler system, the possibility of introducing a cogeneration system has been studied. Previously the energy demands of the building have been calculated proposing different operating modes to meet those demands through micro-CHP or cogeneration systems. Finally, once the options are valued the chosen one is shown and an economic analysis is performed.

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Portugal é um país dependente da energia do exterior, devido à elevada percentagem de consumo de energia a partir de fontes primárias, como por exemplo o gasóleo. Para colmatar este cenário, têm vindo a criar-se incentivos para o uso de energias renováveis e para intensificação de medidas de eficiência energética, como os sistemas de cogeração, de forma a tornar os processos industriais nacionais mais autónomos e mais competitivos. O presente trabalho, centra-se na avaliação do chiller de absorção na central de trigeração da empresa Monteiro, Ribas-Indústria, SA, com a finalidade de identificar algum problema no funcionamento do chiller. Após efetuado o estudo do chiller, verificou-se que o coeficiente de performance do chiller apresenta valores que variam entre 0,75 e 0,81, que comparado com o valor especificado, não apresenta grande diferença. No que toca à potência do chiller, esta apresentou valores entre 948 e 1045 kW. Estes valores estavam bem abaixo da potência especificada pelos fornecedores. Assim, pretendeu-se propor medidas para melhor a potência obtida. Para o efeito foi sugerido o aquecimento da corrente que atua como fonte de calor para o chiller, a corrente de água quente. Embora a empresa apresente a solução para o problema, um permutador de vapor para o aquecimento da corrente de água quente, este não se encontra em funcionamento contínuo, levando a uma potência mais baixa.

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Building integrated photovoltaic (BiPV) systems generate electricity, but also heat, which is typically wasted and also reduces the efficiency of generation. A heat recovery unit can be combined with a BiPV system to take advantage of this waste heat, thus providing cogeneration. Two different photovoltaic (PV) cell types were combined with a heat recovery unit and analysed in terms of their life-cycle energy consumption to determine the energy payback period. A net energy analysis of these PV systems has previously been performed, but recent improvements in the data used for this study allow for a more comprehensive assessment of the combined energy used throughout the entire life-cycle of these systems to be performed. Energy payback periods between 4 and 16.5 years were found, depending on the BiPV system. The energy embodied in PV systems is significant, emphasised here due to the innovative use of national average input–output (I–O) data to fill gaps in traditional life-cycle inventories, i.e. hybrid analysis. These findings provide an insight into the net energy savings that are possible with a well-designed and managed BiPV system.

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Using renewable energy sources for onsite cogeneration from structural building elements is a relatively new concept and is gaining considerable interest. In this study the design, development, manufacturing and testing of a novel building integrated photovoltaic/thermal (BIPVT) solar energy cogeneration system is discussed.

Adhesives (ADH), resistance seam welding (RSW) and autoclaving (ATC) were identified as the most appropriate for fabricating BIPVT roofing panels. Of these manufacturing methods ADH was found to be most suitable for low volume production systems due to its low capital cost.

A prototype panel, fabricated using ADH methods, exhibited good thermal performance. It was also shown that BIPVT performance could be theoretically predicted using a one dimensional heat transfer model and showed excellent agreement with experimental data. The model was used to suggest further design improvements. Finally, a transient simulation of the BIPVT was performed in TRNSYS and is used to illustrate the benefits of the system.

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This article presents an thermoeconomic analysis of cogeneration plants, applied as a rational technique to produce electric power and saturated steam. The aim of this new methodology is the minimum exergetic manufacturing cost (EMC), based on the Second Law of Thermodynamics. The decision variables selected for the optimization are the pressure and the temperature of the steam leaving the boiler in the case of using steam turbine, and the pressure ratio, turbine exhaust temperature and mass flow in the case of using gas turbines. The equations for calculating the capital costs of the components and products are formulated as a function of these decision variables. An application of the method using real data of a multinational chemical industry located in São Paulo state is presented. The conditions which establish the minimum cost are presented as finals conclusions.

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In this work a detailed thermodynamic analysis for an extraction-condensation steam turbine capable to drive a 40 MVA electricity generator in a sugar-alcohol factory was carried out. The use of this turbine in the cogeneration system showed that its efficiency contributed to increase the power generation, although the condensation reduces the overall efficiency of the plant. Sensibility analyses were performed to evaluate the behavior of the overall energy efficiency of a plant with the extraction-condensation turbine in function of the boiler efficiency, the specific consumption of steam in the processes and the condensation rate in the turbine. It was observed that the plant efficiency is very sensible to the condensation rate variation and it increases when there is an increase in the demand of steam for processes.

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This article presents a thermoeconomic analysis of cogeneration plants, applied as a rational technique to produce electric power and saturated steam. The aim of this new methodology is the minimum Exergetic Production Cost (EPC), based on the Second Law of Thermodynamics. The variables selected for the optimization are the pressure and the temperature of the steam leaving the boiler in the case of using steam turbine, and the pressure ratio, turbine exhaust temperature and mass flow in the case of using gas turbines. The equations for calculating the capital costs of the components and products are formulated as a function of these decision variables. An application of the method using real data of a multinational chemical industry located in São Paulo state is presented. The conditions which establish the minimum cost are presented as final output. (C) 2003 Elsevier Ltd. All rights reserved.