37 resultados para pressure drop
Resumo:
A mathematical model is presented for steady fluid flow across microvessel walls through a serial pathway consisting of the endothelial surface glycocalyx and the intercellular cleft between adjacent endothelial cells, with junction strands and their discontinuous gaps. The three-dimensional flow through the pathway from the vessel lumen to the tissue space has been computed numerically based on a Brinkman equation with appropriate values of the Darcy permeability. The predicted values of the hydraulic conductivity Lp, defined as the ratio of the flow rate per unit surface area of the vessel wall to the pressure drop across it, are close to experimental measurements for rat mesentery microvessels. If the values of the Darcy permeability for the surface glycocalyx are determined based on the regular arrangements of fibres with 6nm radius and 8nm spacing proposed recently from the detailed structural measurements, then the present study suggests that the surface glycocalyx could be much less resistant to flow compared to previous estimates by the one-dimensional flow analyses, and the intercellular cleft could be a major determinant of the hydraulic conductivity of the microvessel wall.
Resumo:
The simulation of two-phase flow for an experimental airlift reactor (32-l volume) using commercially available software from Fluent Incorporated is presented here (http://www.fluent.co.uk). Data from the simulation is compared with the experimental data obtained by the tracking of a magnetic particle and analysis of the pressure drop to determine the gas hold-up. Comparisons between vertical velocity and gas hold-up were made for a series of experiments where the superficial gas velocity in the riser was adjusted between 0.01 and 0.075 m s-1. © 2003 Elsevier B.V. All rights reserved.
Resumo:
Basic hydrodynamic parameters of an airlift reactor with internal loop were estimated experimentally and simulated using commercially available CFD software from Fluent. Circulation velocity in a 32-dm(3)-airlift reactor was measured using the magnetic tracer method, meanwhile the gas hold-up was obtained by analysis of the pressure drop using the method of inverted U-tube manometers. Comparison of simulated (in two and three dimensions) and experimental data was performed at different superficial gas velocities in the riser.
Resumo:
The investigation of insulation debris generation, transport and sedimentation becomes important with regard to reactor safety research for PWR and BWR, when considering the long-term behavior of emergency core cooling systems during all types of loss of coolant accidents (LOCA). The insulation debris released near the break during a LOCA incident consists of a mixture of disparate particle population that varies with size, shape, consistency and other properties. Some fractions of the released insulation debris can be transported into the reactor sump, where it may perturb/impinge on the emergency core cooling systems. Open questions of generic interest are the sedimentation of the insulation debris in a water pool, its possible re-suspension and transport in the sump water flow and the particle load on strainers and corresponding pressure drop. A joint research project on such questions is being performed in cooperation between the University of Applied Sciences Zittau/Görlitz and the Forschungszentrum Dresden-Rossendorf. The project deals with the experimental investigation of particle transport phenomena in coolant flow and the development of CFD models for its description. While the experiments are performed at the University at Zittau/Görlitz, the theoretical modeling efforts are concentrated at Forschungszentrum Dresden-Rossendorf. Whereas the paper Alt et al. is focused on the experiments in the present paper the basic concepts for CFD modeling are described and feasibility studies including the conceptual design of the experiments are presented.
Resumo:
For micro gas turbines (MGT) of around 1 kW or less, a commercially suitable recuperator must be used to produce a thermal efficiency suitable for use in UK Domestic Combined Heat and Power (DCHP). This paper uses computational fluid dynamics (CFD) to investigate a recuperator design based on a helically coiled pipe-in-pipe heat exchanger which utilises industry standard stock materials and manufacturing techniques. A suitable mesh strategy was established by geometrically modelling separate boundary layer volumes to satisfy y + near wall conditions. A higher mesh density was then used to resolve the core flow. A coiled pipe-in-pipe recuperator solution for a 1 kW MGT DCHP unit was established within the volume envelope suitable for a domestic wall-hung boiler. Using a low MGT pressure ratio (necessitated by using a turbocharger oil cooled journal bearing platform) meant unit size was larger than anticipated. Raising MGT pressure ratio from 2.15 to 2.5 could significantly reduce recuperator volume. Dimensional reasoning confirmed the existence of optimum pipe diameter combinations for minimum pressure drop. Maximum heat exchanger effectiveness was achieved using an optimum or minimum pressure drop pipe combination with large pipe length as opposed to a large pressure drop pipe combination with shorter pipe length. © 2011 Elsevier Ltd. All rights reserved.
Resumo:
The aim of this study was to prepare gas-filled lipid-coated microbubbles as potential MRI contrast agents for imaging of fluid pressure. Air-filled microbubbles were produced with phospholipid 1,2-distearoyl-sn-glycero-3-phosphocholine (DSPC) in the presence or absence of cholesterol and/or polyethylene-glycol distearate (PEG-distearate). Microbubbles were also prepared containing a fluorinated phospholipid, perfluoroalkylated glycerol-phosphatidylcholine, F-GPC shells encompassing perfluorohexane-saturated nitrogen gas. These microbubbles were evaluated in terms of physico-chemical characteristics such as size and stability. In parallel to these studies, DSPC microbubbles were also formulated containing nitrogen (N2) gas and compared to air-filled microbubbles. By preventing advection, signal drifts were used to assess their stability. DSPC microbubbles were found to have a drift of 20% signal change per bar of applied pressure in contrast to the F-GPC microbubbles which are considerably more stable with a lower drift of 5% signal change per bar of applied pressure. By increasing the pressure of the system and monitoring the MR signal intensity, the point at which the majority of the microbubbles have been damaged was determined. For the DSPC microbubbles this occurs at 1.3 bar whilst the F-GPC microbubbles withstand pressures up to 2.6 bar. For the comparison between air-filled and N2-filled microbubbles, the MRI sensitivity is assessed by cycling the pressure of the system and monitoring the MR signal intensity. It was found that the sensitivity exhibited by the N2-filled microbubbles remained constant, whilst the air-filled microbubbles demonstrated a continuous drop in sensitivity due to continuous bubble damage.
Resumo:
Purpose - The UK Prospective Diabetic Study has confirmed the importance of blood pressure (BP) as a major risk factor for diabetic retinopathy (DR). We wanted to investigate whether measuring the BP in the diabetic eye clinic could identify new hypertensive patients and monitor control in existing ones. Patients and methods - We compared BP in patients attending the diabetic eye clinic with home blood pressure measurement (HBPM) and ambulatory BP measurement (ABPM). In all, 106 patients attending a diabetic eye clinic were selected at random from clinic attendees. BP measurement (on an Omron 705 CP) was performed in the eye clinic and also compared to HBPM three times per day with an Omron 705 CP machine, and was compared to diabetic clinic measurements. In addition, 11 randomly chosen patients had 24 h ABPM to validate the above techniques. Results - In all, 106 patients (70 male and 36 female) were recruited for the study, of which 71 were known to be hypertensive on antihypertensive medication. Of the total, 75 patients (70.8%) had BP>140/85 in the eye clinic, of which 51 (68%) were known to be hypertensive on treatment and this was confirmed in 46 (90%) on HBPM. A total of, 24 patients (22.6%) were newly diagnosed as hypertensive in the eye clinic, which was confirmed by HBPM in 22 patients (92%). The mean BP of the measurements performed in the eye clinic was significantly higher than that carried out in the diabetic clinic (P<0.01). Tropicamide 1% and phenylephrine 2.5% eye drop instillation had no effect on BP. In 11 randomly chosen patients, 24 h ABPM validated both diabetic eye clinic and home BP measurements. Conclusion - Attendance at the diabetic eye clinic is an important chance to detect both new patients with systemic hypertension and those with inadequate BP control. Ophthalmologists should be encouraged to measure BP in their diabetic patients attending diabetic eye clinics, as it is an important risk factor for DR. On the basis of our findings, good BP control is a goal yet to be achieved in diabetic patients with retinopathy.