2 resultados para Body-water Measurement
em Bucknell University Digital Commons - Pensilvania - USA
Resumo:
There are two main types of bone in the human body, trabecular and cortical bone. Cortical bone is primarily found on the outer surface of most bones in the body while trabecular bone is found in vertebrae and at the end of long bones (Ross 2007). Osteoporosis is a condition that compromises the structural integrity of trabecular bone, greatly reducing the ability of the bone to absorb energy from falls. The current method for diagnosing osteoporosis and predicting fracture risk is measurement of bone mineral density. Limitations of this method include dependence on the bone density measurement device and dependence on type of test and measurement location (Rubin 2005). Each year there are approximately 250,000 hip fractures in the United States due to osteoporosis (Kleerekoper 2006). Currently, the most common method for repairing a hip fracture is a hip fixation surgery. During surgery, a temporary guide wire is inserted to guide the permanent screw into place and then removed. It is believed that directly measuring this screw pullout force may result in a better assessment of bone quality than current indirect measurement techniques (T. Bowen 2008-2010, pers. comm.). The objective of this project is to design a device that can measure the force required to extract this guide wire. It is believed that this would give the surgeon a direct, quantitative measurement of bone quality at the site of the fixation. A first generation device was designed by a Bucknell Biomedical Engineering Senior Design team during the 2008- 2009 Academic Year. The first step of this project was to examine the device, conduct a thorough design analysis, and brainstorm new concepts. The concept selected uses a translational screw to extract the guide wire. The device was fabricated and underwent validation testing to ensure that the device was functional and met the required engineering specifications. Two tests were conducted, one to test the functionality of the device by testing if the device gave repeatable results, and the other to test the sensitivity of the device to misalignment. Guide wires were extracted from 3 materials, low density polyethylene, ultra high molecular weight polyethylene, and polypropylene and the force of extraction was measured. During testing, it was discovered that the spring in the device did not have a high enough spring constant to reach the high forces necessary for extracting the wires without excessive deflection of the spring. The test procedure was modified slightly so the wires were not fully threaded into the material. The testing results indicate that there is significant variation in the screw pullout force, up to 30% of the average value. This significant variation was attributed to problems in the testing and data collection, and a revised set of tests was proposed to better evaluate the performance of the device. The fabricated device is a fully-functioning prototype and further refinements and testing of the device may lead to a 3rd generation version capable of measuring the screw pullout force during hip fixation surgery.
Resumo:
Studying liquid fuel combustion is necessary to better design combustion systems. Through more efficient combustors and alternative fuels, it is possible to reduce greenhouse gases and harmful emissions. In particular, coal-derived and Fischer-Tropsch liquid fuels are of interest because, in addition to producing fewer emissions, they have the potential to drastically reduce the United States' dependence on foreign oil. Major academic research institutions like the Pennsylvania State University perform cutting-edge research in many areas of combustion. The Combustion Research Laboratory (CRL) at Bucknell University is striving to develop the necessary equipment to be capable of both independent and collaborative research efforts with Penn State and in the process, advance the CRL to the forefront of combustion studies. The focus of this thesis is to advance the capabilities of the Combustion Research Lab at Bucknell. Specifically, this was accomplished through a revision to a previously designed liquid fuel injector, and through the design and installation of a laser extinction system for the measurement of soot produced during combustion. The previous liquid fuel injector with a 0.005" hole did not behave as expected. Through spray testing the 0.005" injector with water, it was determined that experimental errors were made in the original pressure testing of the injector. Using data from the spray testing experiment, new theoretical hole sizes of the injector were calculated. New injectors with 0.007" and 0.0085" orifices were fabricated and subsequently tested to qualitatively validate their behavior. The injectors were installed in the combustion rig in the CRL and hot-fire tested with liquid heptane. The 0.0085" injector yielded a manageable fuel pressure and produced a broad flame. A laser extinction system was designed and installed in the CRL. This involved the fabrication of a number of custom-designed parts and the specification of laser extinction equipment for purchase. A standard operating procedure for the laser extinction system was developed to provide a consistent, safe method for measuring soot formation during combustion.