35 resultados para Full bridge converters

em Doria (National Library of Finland DSpace Services) - National Library of Finland, Finland


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In this thesis, the main point of interest is the robust control of a DC/DC converter. The use of reactive components in the power conversion gives rise to dynamical effects in DC/DC converters and the dynamical effects of the converter mandates the use of active control. Active control uses measurements from the converter to correct errors present in the converter’s output. The controller needs to be able to perform in the presence of varying component values and different kinds of disturbances in loading and noises in measurements. Such a feature in control design is referred as robustness. This thesis also contains survey of general properties of DC/DC converters and their effects on control design. In this thesis, a linear robust control design method is studied. A robust controller is then designed and applied to the current control of a phase shifted full bridge converter. The experimental results are shown to match simulations.

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Ilmastonmuutos ja fossiilisten polttoaineiden ehtyminen ovat edesauttaneet uusiutuvien energialähteiden tutkimusta huomattavasti. Lisäksi alati kasvava sähköenergian tarve lisää hajautetun sähköntuotannon ja vaihtoehtoisten energialähteiden kiinnostavuutta. Yleisimpiä hajautetun sähköntuotannon energialähteitä ovat tuulivoima, aurinkovoima ja uutena tulokkaana polttokennot. Polttokennon kytkeminen sähköverkkoon vaatii tehoelektroniikkaa, ja yleensä yksinkertaisessa polttokennosovelluksessa polttokenno kytketään galvaanisesti erottavan yksisuuntaisen DC/DC-hakkurin ja vaihtosuuntaajan kanssa sarjaan. Polttokennon rinnalla voidaan käyttää akkua tasaamaan polttokennon syöttämää jännitettä, jolloin akun ja polttokennon väliin tarvitaan kaksisuuntainen DC/DC-hakkuri, joka pystyy siirtämään energiaa molempiin suuntiin. Tässä diplomityössä on esitetty kaksisuuntaisen DC/DC-hakkurin tilayhtälökeskiarvoistusmenetelmään perustuva malli sekä mallin perusteella toteutettu virtasäätö. Tutkittava hakkuritopologia on kokosilta-tyyppinen boost-hakkuri, ja säätömenetelmä keskiarvovirtasäätö. Työn tuloksena syntyi tilayhtälömalli kaksisuuntaiselle FB boost -hakkurille sekä sen tulokelan virran säätämiseen soveltuva säädin. Säädin toimii normaalitilanteissa hyvin, mutta erikoistilanteissa, kuten hakkurin tulojännitteen äkillisessä muutostilanteessa, vaadittaisiin tehokkaampi säädin, jolla saavutettaisiin nopeampi nousuaika ilman ylitystä ja oskillointia.

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Pienjännitejakeluverkko Suomessa on toteutettu 400 V:n kolmivaiheisella vaihtosähköllä. Pienestä jännitteestä johtuen 20/0.4 kV:n muuntajat täytyy sijoittaa lähelle kuluttajaa, jotta siirtohäviöt eivät nouse liian suuriksi. Suuremman vaihto- tai tasajännitteen käyttö pienjännitejakelussa kasvattaisi verkon tehonsiirtokapasiteettia ja mahdollistaisi pidempien siirtomatkojen käytön. Käynnissä olevassa tutkimushankkeessa käsitellään vaihtoehtoa, jossa tasajännitettä käytettäisiin 20 kV:n verkon ja kuluttajan välisessä tehonsiirrossa ja kuluttajalla sijaitseva vaihtosuuntaaja muodostaisi tasasähköstä standardien mukaista yksi- tai kolmivaiheista vaihtosähköä. Tässä diplomityössä käsitellään tehoelektroniikan soveltamista kuluttajalle sijoitetussa vaihtosuuntaajassa. Työssä tarkastellaan yksivaiheisia invertteritopologioita, niiden ohjausta ja soveltamista erilaisissa vaihtosuuntaajaratkaisuissa sekä LC- ja LCL-suotimien soveltuvuutta invertterin lähtöjännitteen suodatukseen. Lisäksi esitellään erilaisia rakenneratkaisuja vaihtosuuntauksen toteutukseen ja tarkastellaan näiden järjestelmien vikatilanteita ja sähköturvallisuutta. Lopuksi käsitellään koko järjestelmän häviöitä ja hyötysuhdetta eri suodinkomponenteilla sekä kytkentätaajuuksilla ja esitellään laboratorioprototyyppi. Työssä saatiin selville, että puolisiltainvertteri ei sovellu suurten kondensaattorien vuoksi syöttämään verkkotaajuista kuormaa, vaan joudutaan käyttämään kokosiltainvertteriä. Kokosiltainvertterin ja LC- tai LCL-suotimen käsittävää kokonaisuutta tarkasteltaessa havaittiin, että pienimmät häviöt saavutetaan LC-suotimella 5 %:n ja LCL-suotimella 1 %:n särövaatimuksella. Hyötysuhdekäyrää tarkasteltaessa saatiin sama tulos läpi koko invertterin tehoalueen. Suotimen häviöiden tarkka laskenta on kuitenkin erittäin haasteellista, joten tulokset ovat suuntaa-antavia.

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Invertteritekniikalla voidaan toteuttaa nykyaikainen, monipuolinen ja tehokas pääteaste moneen eri käyttötarkoitukseen. Tässä työssä suunnitellaan invertteripääteaste mittalaite- ja virtalähdesovelluksiin. Suunnittelussa otetaan huomioon muunneltavuus, valmistuskustannukset ja mitat. Näiden kriteerien lisäksi pääteaste suunnitellaan niin, että se täyttää mittalaite- ja virtalähdesovelluksien vaatimat standardit. Pääteasteen teho rajoittuu 500 VA:iin, mutta vaatimukset lähtöjännitteen erimuotoisuudelle aiheuttavat suunnittelulle omat vaikeutensa. Työssä täytyy tutkia, minkälainen tuloaste, invertteri, suodin ja lähtöaste sopivat parhaiten pääteasteen toteutukseen. Sopivien topologioiden löydyttyä pääteaste simuloidaan tietokoneella, jonka jälkeen voidaan suunnitella prototyyppi käytännön testauksia varten. Suunnittelussa päädyttiin seuraaviin topologioihin: Tuloasteeksi valittiin PFC-piiri, joka on nykyaikana pakollinen invertterikäytössä, koska verkkoon palaavat harmoniset yliaaltokomponentit täytyy suodattaa. Invertteritopologiaksi valittiin kokosiltainvertteri, jolla saadaan parhaiten muutettua lähtöjännitteen taajuutta ja amplitudia. Suodintopologiaksi valittiin LC-suodin, jolla saadaan tehokkaasti suodatettua invertterin aiheuttamat harmoniset yliaallot. Lähtöön sijoitetaan muuntaja, jonka muuntosuhdetta muuntamalla saadaan lähtöjännite halutuksi eri käyttötarkoituksia varten.

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Polttokennojen, erityisesti SOFC-kennojen, tutkimuksessa on viime vuosina saavutettu merkittäviä edistysaskelia ja mahdollisuudet kennojen laajamittaiseen hyödyntämiseen paranevat koko ajan. Polttokennojen yleistyessä tarvitaan tehoelektroniikkaa muokkaamaan kennojen tasajännite verkkoon sopivaksi vaihtojännitteeksi. Verkkovaihtosuuntaaja vaatii korkeamman jännitetason, kuin polttokennosta on saatavissa, joten tasajännitetasoa on ensin nostettava. Tässä diplomityössä esitellään kolme eri hakkuritopologiaa ja perehdytään kokosiltahakkurin optimointiin. Hakkurin pääasialliset häviölähteet olivat toision diodisilta ja transistorit. Diodien vaihtaminen piidiodeista piikarbididiodeihin ei parantanut hyötysuhdetta, koska toision jännite tarkastellussa sovelluksessa oli matala. Muuntajan käämiminen litz-johtimella paransi hyötysuhdetta merkittävästi.

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The objective of this master’s thesis is to investigate the loss behavior of three-level ANPC inverter and compare it with conventional NPC inverter. The both inverters are controlled with mature space vector modulation strategy. In order to provide the comparison both accurate and detailed enough NPC and ANPC simulation models should be obtained. The similar control model of SVM is utilized for both NPC and ANPC inverter models. The principles of control algorithms, the structure and description of models are clarified. The power loss calculation model is based on practical calculation approaches with certain assumptions. The comparison between NPC and ANPC topologies is presented based on results obtained for each semiconductor device, their switching and conduction losses and efficiency of the inverters. Alternative switching states of ANPC topology allow distributing losses among the switches more evenly, than in NPC inverter. Obviously, the losses of a switching device depend on its position in the topology. Losses distribution among the components in ANPC topology allows reducing the stress on certain switches, thus losses are equally distributed among the semiconductors, however the efficiency of the inverters is the same. As a new contribution to earlier studies, the obtained models of SVM control, NPC and ANPC inverters have been built. Thus, this thesis can be used in further more complicated modelling of full-power converters for modern multi-megawatt wind energy conversion systems.

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Due to functional requirement of a structural detail brackets with and without scallop are frequently used in bridges, decks, ships and offshore structure. Scallops are designed to serve as passage way for fluids, to reduce weld length and plate distortions. Moreover, scallops are used to avoid intersection of two or more welds for the fact that there is the presence of inventible inherent initial crack except for full penetrated weld and the formation of multi-axial stress state at the weld intersection. Welding all around the scallop corner increase the possibility of brittle fracture even for the case the bracket is not loaded by primary load. Avoiding of scallop will establish an initial crack in the corner if bracket is welded by fillet welds. If the two weld run pass had crossed, this would have given a 3D residual stress situation. Therefore the presences and absence of scallop necessitates the 3D FEA fatigue resistance of both types of brackets using effective notch stress approach ( ). FEMAP 10.1 with NX NASTRAN was used for the 3D FEA. The first and main objective of this research was to investigate and compare the fatigue resistance of brackets with and without scallop. The secondary goal was the fatigue design of scallops in case they cannot be avoided for some reason. The fatigue resistance for both types of brackets was determined based on approach using 1 mm fictitiously rounded radius based on IIW recommendation. Identical geometrical, boundary and loading conditions were used for the determination and comparison of fatigue resistance of both types of brackets using linear 3D FEA. Moreover the size effect of bracket length was also studied using 2D SHELL element FEA. In the case of brackets with scallop the flange plate weld toe at the corner of the scallop was found to exhibit the highest and made the flange plate weld toe critical for fatigue failure. Whereas weld root and weld toe at the weld intersections were the highly stressed location for brackets without scallop. Thus weld toe for brackets with scallop, and weld root and weld toe for brackets without scallop were found to be the critical area for fatigue failure. Employing identical parameters on both types of brackets, brackets without scallop had the highest except for full penetrated weld. Furthermore the fatigue resistance of brackets without scallop was highly affected by the lack of weld penetration length and it was found out that decreased as the weld penetration was increased. Despite the fact that the very presence of scallop reduces the stiffness and also same time induce stress concentration, based on the 3D FEA it is worth concluding that using scallop provided better fatigue resistance when both types of brackets were fillet welded. However brackets without scallop had the highest fatigue resistance when full penetration weld was used. This thesis also showed that weld toe for brackets with scallop was the only highly stressed area unlike brackets without scallop in which both weld toe and weld root were the critical locations for fatigue failure when different types of boundary conditions were used. Weld throat thickness, plate thickness, scallop radius, lack of weld penetration length, boundary condition and weld quality affected the fatigue resistance of both types of brackets. And as a result, bracket design procedure, especially welding quality and post weld treatment techniques significantly affect the fatigue resistance of both type of brackets.

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Multilevel converters provide an attractive solution to bring the benefits of speed-controlled rotational movement to high-power applications. Therefore, multilevel inverters have attracted wide interest in both the academic community and in the industry for the past two decades. In this doctoral thesis, modulation methods suitable especially for series connected H-bridge multilevel inverters are discussed. A concept of duty cycle modulation is presented and its modification is proposed. These methods are compared with other well-known modulation schemes, such as space-vector pulse width modulation and carrier-based modulation schemes. The advantage of the modified duty-cycle modulation is its algorithmic simplicity. A similar mathematical formulation for the original duty cycle modulation is proposed. The modified duty cycle modulation is shown to produce well-formed phase-to-neutral voltages that have lower total harmonic distortion than the space-vector pulse width modulation and the duty cycle modulation. The space-vector-based solution and the duty cycle modulation, on the other hand, result in a better-quality line-to-line voltage and current waveform. The voltage of the DC links in the modules of the series-connected H-bridge inverter are shown to fluctuate while they are under load. The fluctuation causes inaccuracies in the voltage production, which may result in a failure of the flux estimator in the controller. An extension for upper-level modulation schemes, which changes the switching instants of the inverter so that the output voltage meets the reference voltage accurately regardless of the DC link voltages, is proposed. The method is shown to reduce the error to a very low level when a sufficient switching frequency is used. An appropriate way to organize the switching instants of the multilevel inverter is to make only one-level steps at a time. This causes restrictions on the dynamical features of the modulation schemes. The produced voltage vector cannot be rotated several tens of degrees in a single switching period without violating the above-mentioned one-level-step rule. The dynamical capabilities of multilevel inverters are analyzed in this doctoral thesis, and it is shown that the multilevel inverters are capable of operating even in dynamically demanding metal industry applications. In addition to the discussion on modulation schemes, an overvoltage in multilevel converter drives caused by cable reflection is addressed. The voltage reflection phenomenon in drives with long feeder cables causes premature insulation deterioration and also affects the commonmode voltage, which is one of the main reasons for bearing currents. Bearing currents, on the other hand, cause fluting in the bearings, which results in premature bearing failure. The reflection phenomenon is traditionally prevented by filtering, but in this thesis, a modulationbased filterless method to mitigate the overvoltage in multilevel drives is proposed. Moreover, the mitigation method can be implemented as an extension for upper-level modulation schemes. The method exploits the oscillations caused by two consecutive voltage edges so that the sum of the oscillations results in a mitigated peak of the overvoltage. The applicability of the method is verified by simulations together with experiments with a full-scale prototype.

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Åke Backström

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Line converters have become an attractive AC/DC power conversion solution in industrial applications. Line converters are based on controllable semiconductor switches, typically insulated gate bipolar transistors. Compared to the traditional diode bridge-based power converters line converters have many advantageous characteristics, including bidirectional power flow, controllable de-link voltage and power factor and sinusoidal line current. This thesis considers the control of the lineconverter and its application to power quality improving. The line converter control system studied is based on the virtual flux linkage orientation and the direct torque control (DTC) principle. A new DTC-based current control scheme is introduced and analyzed. The overmodulation characteristics of the DTC converter are considered and an analytical equation for the maximum modulation index is derived. The integration of the active filtering features to the line converter isconsidered. Three different active filtering methods are implemented. A frequency-domain method, which is based on selective harmonic sequence elimination, anda time-domain method, which is effective in a wider frequency band, are used inharmonic current compensation. Also, a voltage feedback active filtering method, which mitigates harmonic sequences of the grid voltage, is implemented. The frequency-domain and the voltage feedback active filtering control systems are analyzed and controllers are designed. The designs are verified with practical measurements. The performance and the characteristics of the implemented active filtering methods are compared and the effect of the L- and the LCL-type line filteris discussed. The importance of the correct grid impedance estimate in the voltage feedback active filter control system is discussed and a new measurement-based method to obtain it is proposed. Also, a power conditioning system (PCS) application of the line converter is considered. A new method for correcting the voltage unbalance of the PCS-fed island network is proposed and experimentally validated.

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IIn electric drives, frequency converters are used to generatefor the electric motor the AC voltage with variable frequency and amplitude. When considering the annual sale of drives in values of money and units sold, the use of low-performance drives appears to be in predominant. These drives have tobe very cost effective to manufacture and use, while they are also expected to fulfill the harmonic distortion standards. One of the objectives has also been to extend the lifetime of the frequency converter. In a traditional frequency converter, a relatively large electrolytic DC-link capacitor is used. Electrolytic capacitors are large, heavy and rather expensive components. In many cases, the lifetime of the electrolytic capacitor is the main factor limiting the lifetime of the frequency converter. To overcome the problem, the electrolytic capacitor is replaced with a metallized polypropylene film capacitor (MPPF). The MPPF has improved properties when compared to the electrolytic capacitor. By replacing the electrolytic capacitor with a film capacitor the energy storage of the DC-linkwill be decreased. Thus, the instantaneous power supplied to the motor correlates with the instantaneous power taken from the network. This yields a continuousDC-link current fed by the diode rectifier bridge. As a consequence, the line current harmonics clearly decrease. Because of the decreased energy storage, the DC-link voltage fluctuates. This sets additional conditions to the controllers of the frequency converter to compensate the fluctuation from the supplied motor phase voltages. In this work three-phase and single-phase frequency converters with small DC-link capacitor are analyzed. The evaluation is obtained with simulations and laboratory measurements.

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Electric motors driven by adjustable-frequency converters may produce periodic excitation forces that can cause torque and speed ripple. Interaction with the driven mechanical system may cause undesirable vibrations that affect the system performance and lifetime. Direct drives in sensitive applications, such as elevators or paper machines, emphasize the importance of smooth torque production. This thesis analyses the non-idealities of frequencyconverters that produce speed and torque ripple in electric drives. The origin of low order harmonics in speed and torque is examined. It is shown how different current measurement error types affect the torque. As the application environment, direct torque control (DTC) method is applied to permanent magnet synchronous machines (PMSM). A simulation model to analyse the effect of the frequency converter non-idealities on the performance of the electric drives is created. Themodel enables to identify potential problems causing torque vibrations and possibly damaging oscillations in electrically driven machine systems. The model is capable of coupling with separate simulation software of complex mechanical loads. Furthermore, the simulation model of the frequency converter's control algorithm can be applied to control a real frequency converter. A commercial frequencyconverter with standard software, a permanent magnet axial flux synchronous motor and a DC motor as the load are used to detect the effect of current measurement errors on load torque. A method to reduce the speed and torque ripple by compensating the current measurement errors is introduced. The method is based on analysing the amplitude of a selected harmonic component of speed as a function oftime and selecting a suitable compensation alternative for the current error. The speed can be either measured or estimated, so the compensation method is applicable also for speed sensorless drives. The proposed compensation method is tested with a laboratory drive, which consists of commercial frequency converter hardware with self-made software and a prototype PMSM. The speed and torque rippleof the test drive are reduced by applying the compensation method. In addition to the direct torque controlled PMSM drives, the compensation method can also beapplied to other motor types and control methods.

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Pienitehoisessa taajuusmuuttajassa verkkojännite tasasuunnataan yleisesti diodisillalla. Taajuusmuuttajaa kuormitettaessa diodisilta aiheuttaa sen, että verkosta otettava virta on epäsinimuotoista ja sisältää runsaasti eri kertalukujen yliaaltoja. Tällainen virta vääristää verkon jännitettä sekä aiheuttaa häviöitä, resonansseja ja toimintaepävarmuutta sähkönjakeluverkkoon liitetyissä laitteissa ja komponenteissa. Työssä on tarkasteltu pienitehoisen kolmivaiheisen taajuusmuuttajan tulovirrassa esiintyviä yliaaltoja ja keinoja niiden rajoittamiseksi. Laitevalmistajien osalta syynä aiheen tutkimiseen ja kiinnostavuuteen ovat lähinnä uudet yliaaltoja käsittelevät standardit. Työssä onkin tutustuttu tarvittavin osin standardoinnin nykytilaan sekä seurattu standardeja valmistelevien työryhmien työtä ja tätä kautta perehdytty alaa käsittelevien standardien tulevaisuudennäkymiin Euroopan Unionin alueella. Käsittely on kohdistettu kolmivaiheisiin laitteisiin. Standardi IEC 61000-3-2 asettaa yliaaltorajat ammattikäyttöön tarkoitetuille laitteille, kun laitteen tuloteho on korkeintaan 1 kW. Tällä tehoalueella riittää kolmivaihelaitteille kuristimilla suoritettu passiivinen suodatus täyttämään asetetut viranomaisvaatimukset. Tähän liittyen on suunniteltu kolmivaihekuristin, joka on tarkoitettu käytettäväksi taajuusmuuttajasarjan lisävarusteena tehoalueella 0.12…2.2 kW.

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The CO2-laser-MAG hybrid welding process has been shown to be a productive choice for the welding industry, being used in e.g. the shipbuilding, pipe and beam manufacturing, and automotive industries. It provides an opportunity to increase the productivity of welding of joints containing air gaps compared with autogenous laser beam welding, with associated reductions in distortion and marked increases in welding speeds and penetration in comparison with both arc and autogenous laser welding. The literature study indicated that the phenomena of laser hybrid welding are mostly being studied using bead-on-plate welding or zero air gap configurations. This study shows it very clearly that the CO2 laser-MAG hybrid welding process is completely different, when there is a groove with an air gap. As in case of industrial use it is excepted that welding is performed for non-zero grooves, this study is of great importance for industrial applications. The results of this study indicate that by using a 6 kW CO2 laser-MAG hybrid welding process, the welding speed may also be increased if an air gap is present in the joint. Experimental trials indicated that the welding speed may be increased by 30-82% when compared with bead-on-plate welding, or welding of a joint with no air gap i.e. a joint prepared as optimum for autogenous laser welding. This study demonstrates very clearly, that the separation of the different processes, as well as the relative configurations of the processes (arc leading or trailing) affect welding performance significantly. These matters influence the droplet size and therefore the metal transfer mode, which in turn determined the resulting weld quality and the ability to bridge air gaps. Welding in bead-onplate mode, or of an I butt joint containing no air gap joint is facilitated by using a leading torch. This is due to the preheating effect of the arc, which increases the absorptivity of the work piece to the laser beam, enabling greater penetration and the use of higher welding speeds. With an air gap present, air gap bridging is more effectively achieved by using a trailing torch because of the lower arc power needed, the wider arc, and the movement of droplets predominantly towards the joint edges. The experiments showed, that the mode of metal transfer has a marked effect on gap bridgeability. Transfer of a single droplet per arc pulse may not be desirable if an air gap is present, because most of the droplets are directed towards the middle of the joint where no base material is present. In such cases, undercut is observed. Pulsed globular and rotational metal transfer modes enable molten metal to also be transferred to the joint edges, and are therefore superior metal transfer modes when bridging air gaps. It was also found very obvious, that process separation is an important factor in gap bridgeability. If process separation is too large, the resulting weld often exhibits sagging, or no weld may be formed at all as a result of the reduced interaction between the component processes. In contrast, if the processes are too close to one another, the processing region contains excess molten metal that may create difficulties for the keyhole to remain open. When the distance is optimised - i.e. a separation of 0-4 mm in this study, depending on the welding speed and beam-arc configuration - the processes act together, creating beneficial synergistic effects. The optimum process separation when using a trailing torch was found to be shorter (0-2 mm) than when a leading torch is used (2-4 mm); a result of the facilitation of weld pool motion when the latter configuration is adopted. This study demonstrates, that the MAG process used has a strong effect on the CO2-laser-MAG hybrid welding process. The laser beam welding component is relatively stable and easy to manage, with only two principal processing parameters (power and welding speed) needing to be adjusted. In contrast, the MAG process has a large number of processing parameters to optimise, all of which play an important role in the interaction between the laser beam and the arc. The parameters used for traditional MAG welding are often not optimal in achieving the most appropriate mode of metal transfer, and weld quality in laser hybrid welding, and must be optimised if the full range of benefits provided by hybrid welding are to be realised.