3 resultados para initial value problem

em Iowa Publications Online (IPO) - State Library, State of Iowa (Iowa), United States


Relevância:

30.00% 30.00%

Publicador:

Resumo:

A detailed investigation has been conducted on core samples taken from 17 portland cement concrete pavements located in Iowa. The goal of the investigation was to help to clarify the root cause of the premature deterioration problem that has become evident since the early 1990s. Laboratory experiments were also conducted to evaluate how cement composition, mixing time, and admixtures could have influenced the occurrence of premature deterioration. The cements used in this study were selected in an attempt to cover the main compositional parameters pertinent to the construction industry in Iowa. The hardened air content determinations conducted during this study indicated that the pavements that exhibited premature deterioration often contained poor to marginal entrained-air void systems. In addition, petrographic studies indicated that sometimes the entrained-air void system had been marginal after mixing and placement of the pavement slab, while in other instances a marginal to adequate entrained-air void system had been filled with ettringite. The filling was most probably accelerated because of shrinkage cracking at the surface of the concrete pavements. The results of this study suggest that the durability—more sciecifically, the frost resistance—of the concrete pavements should be less than anticipated during the design stage of the pavements. Construction practices played a significant role in the premature deterioration problem. The pavements that exhibited premature distress also exhibited features that suggested poor mixing and poor control of aggregate grading. Segregation was very common in the cores extracted from the pavements that exhibited premature distress. This suggests that the vibrators on the paver were used to overcome a workability problem. Entrained-air voids formed in concrete mixtures experiencing these types of problems normally tend to be extremely coarse, and hence they can easily be lost during the paving process. This tends to leave the pavement with a low air content and a poor distribution of air voids. All of these features were consistent with a premature stiffening problem that drastically influenced the ability of the contractor to place the concrete mixture. Laboratory studies conducted during this project indicated that most premature stiffening problems can be directly attributed to the portland cement used on the project. The admixtures (class C fly ash and water reducer) tended to have only a minor influence on the premature stiffening problem when they were used at the dosage rates described in this study.

Relevância:

30.00% 30.00%

Publicador:

Resumo:

Executive Summary I. Survey The Task Force conducted a wide-ranging survey of more than 9,000 licensed Iowa attorneys and judges to obtain their input on a variety of civil justice system topics. The survey results helped inform the Task Force of problem areas in Iowa’s civil justice system. II. Two-Tier Justice System The Task Force recommends a pilot program based on a two-tier civil justice system. A two-tier system would streamline litigation processes—including rules of evidence and discovery disclosures—and reduce litigation costs of certain cases falling below a threshold dollar value. III. One Judge/One Case and Date Certain for Trial Some jurisdictions in Iowa have adopted one judge/one case and date certain for trial in certain cases. The assignment of one judge to each case for the life of the matter and the establishment of dates certain for civil trials could enhance Iowans’ access to the courts, improve judicial management, promote consistency and adherence to deadlines, and reduce discovery excesses. IV. Discovery Processes Reforms addressing inefficient discovery processes will reduce delays in and costs of litigation. Such measures include adopting an aspirational purpose for discovery rules to “secure the just, speedy, and inexpensive determination of every action,” holding discovery proportional to the size and nature of the case, requiring initial disclosures, limiting the number of expert witnesses, and enforcing existing rules. V. Expert Witness Fees The Task Force acknowledges the probable need to revisit the statutory additional daily compensation limit for expert witness fees. Leaving the compensation level to the discretion of the trial court is one potential solution. VI. Jurors Additions to the standard juror questionnaire would provide a better understanding of the potential jurors’ backgrounds and suitability for jury service. The Task Force encourages adoption of more modern juror educational materials and video. Rehabilitation of prospective jurors who express an unwillingness or inability to be fair should include a presumption of dismissal. VII. Video and Teleconferencing Options When court resources are constrained both by limited numbers of personnel and budget cuts, it is logical to look to video and teleconferencing technology to streamline the court process and reduce costs. The judicial branch should embrace technological developments in ways that will not compromise the fairness, dignity, solemnity, and decorum of judicial proceedings. VIII. Court-Annexed Alternative Dispute Resolution(ADR) Litigants and practitioners in Iowa are generally satisfied with the current use of private, voluntary ADR for civil cases. There is concern, however, that maintaining the status quo may have steep future costs. Court-annexed ADR is an important aspect of any justice system reform effort, and the Task Force perceives benefits and detriments to reforming this aspect of the Iowa civil justice system. IX. Relaxed Requirement of Findings of Fact and Conclusions of Law A rule authorizing parties to waive findings of fact and conclusions of law could expedite resolution of nonjury civil cases. X. Business (Specialty) Courts Specialty business courts have achieved widespread support across the country. In addition, specialty courts provide excellent vehicles for implementing or piloting other court innovations that may be useful in a broader court system context. A business specialty court should be and could be piloted in Iowa within the existing court system framework of the Iowa Judicial Branch. Appendix included as a separate document, is 176 pages.

Relevância:

30.00% 30.00%

Publicador:

Resumo:

This investigation was initiated to determine the causes of a rutting problem that occurred on Interstate 80 in Adair County. 1-80 from Iowa 25 to the Dallas County line was opened to traffic in November, 1960. The original pavement consisted of 4-1/2" of asphalt cement concrete over 12" of rolled stone base and 12" of granular subbase. A 5-1/2" overlay of asphalt cement concrete was placed in 1964. In 1970-1972, the roadway was resurfaced with 3" of asphalt cement concrete. In 1982, an asphalt cement concrete inlay, designed for a 10-year life, was placed in the eastbound lane. The mix designs for all courses met or exceeded all current criteria being used to formulate job mixes. Field construction reports indicate .that asphalt usage, densities, field voids and filler bitumen determinations were well within specification limits on a very consistent basis. Field laboratory reports indicate that laboratory voids for the base courses were within the prescribed limits for the base course and below the prescribed limits for the surface course. Instructional memorandums do indicate that extreme caution should be exercised when the voids are at or near the lower limits and traffic is not minimal. There is also a provision that provides for field voids controlling when there is a conflict between laboratory voids and field voids. It appears that contract documents do not adequately address the directions that must be taken when this conflict arises since it can readily be shown that laboratory voids must be in the very low or dangerous range if field voids are to be kept below the maximum limit under the current density specifications. A rut depth survey of January, 1983, identified little or no rutting on this section of roadway. Cross sections obtained in October, 1983, identified rutting which ranged from 0 to 0.9" with a general trend of the rutting to increase from a value of approximately 0.3" at MP 88 to a rut depth of 0.7" at MP 98. No areas of significant rutting were identified in the inside lane. Structural evaluation with the Road Rater indicated adequate structural capacity and also indicated that the longitudinal subdrains were functioning properly to provide adequate soil support values. Two pavement sections taken from the driving lane indicated very little distortion in the lower 7" base course. Essentially all of the distortion had occurred in the upper 2" base course and the 1..;1/2" surface course. Analysis of cores taken from this section of Interstate 80 indicated very little densification of either the surface or the upper or lower base courses. The asphalt cement content of both the Type B base courses and the Type A surface course were substantially higher than the intended asphalt cement content. The only explanation for this is that the salvaged material contained a greater percent of asphalt cement than initial extractions indicated. The penetration and viscosity of the blend of new asphalt cement and the asphalt cement recovered from the salvaged material were relatively close to that intended for this project. The 1983 ambient temperatures were extremely high from June 20 through September 10. The rutting is a result of a combination of adverse factors including, (1) high asphalt content, (2) the difference between laboratory and field voids, (3) lack of intermediate sized crushed particles, (4) high ambient temperatures. The high asphalt content in the 2" upper base course produced an asphalt concrete mix that did not exhibit satisfactory resistance to deformation from heavy loading. The majority of the rutting resulted from distortion of the 2" upper base lift. Heater planing is recommended as an interim corrective action. Further recommendation is to design for a 20-year alternative by removing 2-1/2" of material from the driving lane by milling and replacing with 2-1/2" of asphalt concrete with improved stability. This would be .followed by placing 1-1/2" of high quality resurfacing on the entire roadway. Other recommendations include improved density and stability requirements for asphalt concrete on high traffic roadways.