6 resultados para Reynolds, Irving

em Iowa Publications Online (IPO) - State Library, State of Iowa (Iowa), United States


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In advance of the 2012 legislative session, I am pleased to provide for your review this legislative brief on Gov. Terry E. Branstad’s and Lt. Gov. Kim Reynolds’ education reform package. The purpose is to provide a broad overview of the components of the package, give some examples of where similar approaches are in place, and provide cost estimates. In collaboration with the Governor’s Office, the staff at the Iowa Department of Education and I have worked intensively to prepare a set of legislative proposals worthy of careful consideration. I believe this package puts us on the path to our unshakable vision of having one of the best school systems in the world. Iowa’s children deserve nothing less.

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Research project HR-219 was sponsored by the Iowa Highway Research Board and the Iowa Department of Transportation. The funding authorized from the Primary Road Research Fund was $11,200. The author wishes to express his appreciation to Iowa DOT personnel for their participation in the research. The special features were incorporated into the plans by Road Design personnel. Office of Materials personnel developed the proportions for the flowable mortar. Project inspection was provided by the Creston Resident Engineer and his staff. The excellent cooperation of the contractors contributed to the success of the research. The prime contractor was Irving F. Jensen Company, Inc. of Sioux City, Iowa who retained Reilly Construction Company of Ossian, Iowa and GNA Concrete, Inc. of Grimes, Iowa as subcontractors for the special culvert backfilling.

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A laboratory investigation was undertaken to determine the limiting model Reynolds number above which the scour behavior of rock protected structures can be reproduced in hydraulic models scaled according to the Froude criterion. A submerged jet was passed over an initially full scour pocket containing uniform glass spheres and the rate of scour was measured as a function of time. The dimensions of the scour pocket and jet and the particle diameters were varied as needed to maintain strict geometric similarity. For each of two different Froude numbers the Reynolds number was varied over a wide range. The normalized scour rate was found to be practically independent of the Reynolds number, R, (based on the jet velocity and particle diameter) at values of R above about 2.5 x 10^3, and to decrease with Rat smaller values. A grid placed in the jet was found to have a very strong effect on the scour rate. In an attempt to explain the effect of R on the scour behavior, turbulent pressure and velocity fluctuations were measured in air flows and water flows, respectively, over rigid scour pockets having the same geometry as those formed in the scour experiments. The normalized spectra of the fluctuations were found to be nearly independent of R, but the flow pattern was found to be very sensitive to the inlet condition, the jet deflecting upward or downward in a not wholly explainable manner. This indicates that scour behavior can be modeled only if the approach flow is also accurately modeled.

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In 1982 the Iowa DOT allowed a successful bidder the option of submitting materials and proportions using fly ash to produce a portland cement concrete (PCC) paving mixture to meet a specified compressive strength. The contractor, Irving F. Jensen, received approval for the use of a concrete mixture utilizing 500 lbs. of portland cement and 88 lbs. of fly ash as a replacement of 88 lbs. of portland cement. The PCC mixture was utilized on the Muscatine County US 61 relocation bypass paved as project F-61-4(32)--20-70. A Class "C" fly ash obtained from the Chillicothe electric generating plant approximately 100 miles away was used in the project. This use of fly ash in lieu of portland cement resulted in a cost savings of $64,500 and an energy savings of approximately 16 billion BTU. The compressive strength of this PCC mixture option was very comparable to concrete mixtures produced without the use of fly ash. The pavement has been performing very well. The substitution of fly ash for 15% of the cement has been allowed as a contractor's option since 1984. Due to the cost savings, it has been used in almost all Iowa PCC paving since that time.

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The main objective of the proposed study is to use Computational Fluid Dynamics (CFD) tools to determine the wind loads by accurate numerical simulations of air flow characteristics around large highway sign structures under severe wind speeds conditions. Fully three-dimensional Reynolds- Averaged Navier-Stokes (RANS) simulations are used to estimate the total force on different panels, as well as the actual pressure distribution on the front and back faces of the panels. In particular, the present study investigates the effects of aspect ratio and sign spacing for regular panels, the effect of sign depth for the dynamic message signs that are now being used on Iowa highways, the effect induced by the presence of back-to-back signs, the effect of the presence of add-on exit signs, and the effect of the presence of trucks underneath the signs potentially creating “wind tunnel” effect.

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In 1982 the Iowa DOT allowed a successful bidder the option of submitting materials and proportions using fly ash to produce a portland cement concrete (PCC) paving mixture to meet a specified compressive strength. The contractor, Irving F. Jensen, received approval for the use of a concrete mixture utilizing 500 lbs. of portland cement and 88 lbs. of fly ash as a replacement of 88 lbs. of portland cement. The PCC mixture was utilized on the Muscatine County US 61 relocation bypass paved as project F-61-4(32)--20-70. A Class "C" fly ash obtained from the Chillicothe electric generating plant approximately 100 miles away was used in the project. This use of fly ash in lieu of portland cement resulted in a cost savings of $64,500 and an energy savings of approximately 16 billion BTU. The compressive strength of this PCC mixture option was very comparable to concrete mixtures produced without the use of fly ash. The pavement has been performing very well. The substitution of fly ash for 15% of the cement has been allowed as a contractor's option since 1984. Due to the cost savings, it has been used in almost all Iowa PCC paving since that time.