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em Iowa Publications Online (IPO) - State Library, State of Iowa (Iowa), United States


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In conventional construction practices, a longitudinal joint is sawed in a PCC (Portland Cement Concrete) pavement to control concrete shrinkage cracking between two lanes of traffic. Sawing a joint in hardened concrete is an expensive and time consuming operation. The longitudinal joint is not a working joint (in comparison to a transverse joint) as it is typically tied with a tie bar at 30 inch spacing. The open joint reservoir, left by the saw blade, typically is filled or sealed with a durable crack sealant to keep incompressibles and water from getting into the joint reservoir. An experimental joint forming knife has been developed. It is installed under the paving machine to form the longitudinal joint in the wet concrete as a part of the paving process. Through this research method, forming a very narrow longitudinal joint during the paving process, two conventional paving operations can be eliminated. Joint forming eliminates the need of the joint sawing operation in the hard concrete, and as the joint that is formed does not leave a wide-open reservoir, but only a hairline crack, it does not need the joint filling or sealing operation. Therefore, the two conventional longitudinal joint sawing and sealing operations are both being eliminated by this innovation. A laboratory scale prototype joint forming knife was built and tested, initially forming joints in small concrete beams. The results were positive so the method was proposed for field testing. Initial field tests were done in the construction season of 2001, limited to one paving contractor. A number of modifications were made to the knife throughout the field tests. About 3000 feet of longitudinal joint was formed in 2001. Additional testing was done in the 2002 construction season, working with the same contractor. About 150,000 feet of longitudinal joint was formed in 2002. Evaluations of the formed joints were done to determine longitudinal joint hairline crack development rate and appearance. Additional tests will be done in the next construction season to improve or perfect the longitudinal joint forming technique.

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The Iowa DOT has been using blended cements in ternary mixes since 1999. Use of these supplementary cementitious materials gives concrete with higher strengths and much lower permeability. Use of these materials has been incorporated for use in High Performance Concrete (HPC) decks to achieve lower permeability and thus long term performance. Since we have been using these materials in paving, it would be informative to determine what concrete pavement properties are enhanced as related to high performance concrete. The air void system was excellent at a spacing factor of 0.0047 in (0.120 mm). AVA spacing factor results are much higher than the hardened air void analysis. Although only 3 samples were tested between the image analysis air content and the RapidAir457, there is pretty good agreement between those test methods. Air void analysis indicates that excessive vibration was not required to place the concrete. Vibration was well within the specification limits with an average of 6683 vpm’s with a standard deviation of 461. Overall ride of the project was very good. The average smoothness for the project was 2.1 in/mile (33.8 mm/km). The International Roughness Index (IRI) was 81 in/mi (1.29 m/km). The compressive strength was 6260 psi (43.2 MPa) at 28 days and 6830 (47.1 MPa) at 56 days. The modulus of rupture by third point loading (MOR-TPL) tested at 28 days was 660 psi (4.55 MPa). The AASHTO T277 rapid chloride permeability results at 28 days using the Virginia cure method correlate fairly well with the 56 and 90 day results with standard curing. The Virginia cure method 28 day results were 2475 coulombs and the standard cure 56 and 90 day test results were 2180 and 2118, respectively.

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Portland cement concrete pavements have given excellent service history for Iowa. Many of these pavements placed during the 1920’s and 1930’s are still in service today. Many factors go in to achieve a long term durable concrete pavement. Probably the most important is the durability of the aggregate. Until the 1930’s, pit run gravel was the most predominant aggregate used. Many of these gravels provided long term performance and their durability is dependent upon the carbonate fraction of the gravel. Later, limestone (calcium carbonate) and dolomite (calcium, magnesium carbonate) sources were mined across Iowa. The durability of these carbonate aggregates is largely dependent upon the pore system which can cause freeze thaw problems known as D-cracking, which was a problem with some sources during the 1960’s. Also, some of these carbonate aggregates are also susceptible to deterioration from deicing salts. Geologists have identified the major components that affect the durability of these carbonate aggregates and sources are tested to ensure long term performance in Portland cement concrete. Air entrainment was originally put in concrete to improve scaling resistance. It is well known that air entrainment is required to provide freeze thaw protection in concrete pavements today. In Iowa, air entrainment was not introduced in concrete pavements until 1952. This research investigates properties that made older concrete pavements durable without air entrainment.

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The purpose of this investigation was to determine the comparative effectiveness of standard D-57 concrete and Iowa system Low Slump Dense Concrete in preventing threshold levels of chloride from penetrating the concrete slabs to the reinforcing steel.

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This is a continuation of a project initiated a year ago to determine any differences in test results on recovered asphalt cements caused by the use of industrial grade of solvent as compared with the reagent grade. AASHTO specifies the use of reagent grade of trichlorethylene, but the Laboratory uses industrial grade which costs much less. Last year this objective of the project was aborted when it was found that a larger difference in test results was obtained between the two distillation apparatuses than between the two solvents, Then all efforts were directed toward obtaining uniformity in test results between the apparatuses under the east hood as compared with that under the west hood. Considerable progress was made toward this end. (See report under this same title dated April 1982). The objective this year was to again evaluate the results when using both variables (apparatuses and solvents). Another objective developed later in this investigation; this was to determine any differences in test results on recovered asphalt cements caused by the use of reclaimed trichlorethylene (from the distillation process) as compared with the use of industrial grade of solvent. At the present time the reclaimed trichlorethylene is discarded. If the reclaimed solvent could be used for further recoveries, a considerable savings in solvent costs would result.

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This past winter the sieve analysis of combined aggregate was investigated. This study was given No. 26 by the Central Laboratory. The purpose of this work was to try and develop a sieve analysis procedure for combined aggregate which is less time consuming and has the same accuracy as the method described in I.M. 304. In an attempt to use a variety of aggregates for this investigation, a request was made to each District Materials Office to obtain at least 3 different combined aggregate samples in their respective districts. At the same time it was also requested that the field technician test these samples, prior to submitting them to the Central Laboratory. The field technician was instructed to test each sample as described in method I.M. 304 and also by a modified AASHTO T27 method which will be identified in the report as Method A. The modified AASHTO Method A was identical to T27 with the exception that a smaller sample is used for testing. The field technicians submitted the samples, test results and also comments regarding the modified AASHTO procedure. The general comments of the modified AASHTO procedure were: The method was much simpler to follow; however, it took about the same amount of time so there was no real advantage. After reviewing AASHTO T27, T164, I.M. 304 and Report No. FHWA-RD-77-53 another test method was purposed. Report No. FHWA-RD-77-53 is a report prepared by FHWA from data they gathered concerning control practices and shortcut or alternative test methods for aggregate gradation. A second test method was developed which also was very similar to AASHTO T27, The test procedure for this method is attached and is identified as Method B. The following is a summary of test results submitted by the Field Technicians and obtained by the aggregate section of the Central Laboratory.

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Crop and livestock summaries for the state of Iowa, produced by the Iowa Department of Agriculture. Previously Agri-News