5 resultados para Alkali metal halides.
em Iowa Publications Online (IPO) - State Library, State of Iowa (Iowa), United States
Resumo:
Cement-aggregate reactions were first reported in the 1940's. Depletion of quality aggregate, changes in cement and the use of fly ash make cement-aggregate reactions a problem still today. This latest research into alkali-aggregate reactivity was initiated to evaluate the new ASTM style test containers and evaluate the effect of Class C fly ash on the expansive reaction. Three aggregates were tested in combination with three cements and three fly ashes available in Iowa. Thirty-six combinations were made and tested over a six-month period. The conclusions were: (1) the new style ASTM containers were much more effective than the containers used by the Iowa DOT in the past; (2) some mixes with 15 percent Class C fly ash had increased expansion over comparative mixes without fly ash; and (3) the Oreapolis #8 pit did not appear to have an alkali-silica reaction problem based on this testing and earlier reported testing.
Resumo:
Sodium and potassium are the common alkalis present in fly ash. Excessive amounts of fly ash alkalis can cause efflorescence problems in concrete products and raise concern about the effectiveness of the fly ash to mitigate alkali-silica reaction (ASR). The available alkali test, which is commonly used to measure fly ash alkali, takes approximately 35 days for execution and reporting. Hence, in many instances the fly ash has already been incorporated into concrete before the test results are available. This complicates the job of the fly ash marketing agencies and it leads to disputes with fly ash users who often are concerned with accepting projects that contain materials that fail to meet specification limits. The research project consisted of a lab study and a field study. The lab study focused on the available alkali test and how fly ash alkali content impacts common performance tests (mortar-bar expansion tests). Twenty-one fly ash samples were evaluated during the testing. The field study focused on the inspection and testing of selected, well documented pavement sites that contained moderately reactive fine aggregate and high-alkali fly ash. A total of nine pavement sites were evaluated. Two of the sites were control sites that did not contain fly ash. The results of the lab study indicated that the available alkali test is prone to experimental errors that cause poor agreement between testing labs. A strong (linear) relationship was observed between available alkali content and total alkali content of Class C fly ash. This relationship can be used to provide a quicker, more precise method of estimating the available alkali content. The results of the field study failed to link the use of high-alkali fly ash with the occurrence of ASR in the various concrete sites. Petrographic examination of the pavement cores indicated that Wayland sand is an ASR-sensitive aggregate. This was in good agreement with Iowa DOT field service records. It was recommended that preventative measures should be used when this source of sand is used in concrete mixtures.
Resumo:
Questionnaires were sent to transportation agencies in all 50 states in the U.S., to Puerto Rico, and all provinces in Canada asking about their experiences with uplift problems of - corrugated metal pipe (CMP). Responses were received from 52 agencies who reported 9 failures within the last 5 years. Some agencies also provided design standards for tiedowns to resist uplift. There was a wide variety in restraining forces used; for example for a pipe 6 feet in diameter, the resisting force ranged from 10 kips to 66 kips. These responses verified the earlier conclusion based on responses from Iowa county engineers that a potential uplift danger exists.when end restraint is not provided for CMP and that existing designs have an unclear theoretical or experimental basis. In an effort to develop more rational design standards, the longitudinal stiffness of three CMP ranging from 4 to 8 feet in diameter were measured in the laboratory. Because only three tests were conducted, a theoretical model to evaluate the stiffness of pipes of a variety of gages and corrugation geometries was also developed. The experimental results indicated a "stiffness" EI in the range of 9.11 x 10^5 k-in^2 to 34.43 x 10^5 k-in^2 for the three pipes with the larger diameter pipes having greater stiffness. The theoretical model developed conservatively estimates these stiffnesses.
Resumo:
This investigation is the final phase of a three part study whose overall objectives were to determine if a restraining force is required to prevent inlet uplift failures in corrugated metal pipe (CMP) installations, and to develop a procedure for calculating the required force when restraint is required. In the initial phase of the study (HR-306), the extent of the uplift problem in Iowa was determined and the forces acting on a CMP were quantified. In the second phase of the study (HR- 332), laboratory and field tests were conducted. Laboratory tests measured the longitudinal stiffness ofCMP and a full scale field test on a 3.05 m (10 ft) diameter CMP with 0.612 m (2 ft) of cover determined the soil-structure interaction in response to uplift forces. Reported herein are the tasks that were completed in the final phase of the study. In this phase, a buried 2.44 m (8 ft) CMP was tested with and without end-restraint and with various configurations of soil at the inlet end of the pipe. A total of four different soil configurations were tested; in all tests the soil cover was constant at 0.61 m (2 ft). Data from these tests were used to verify the finite element analysis model (FEA) that was developed in this phase of the research. Both experiments and analyses indicate that the primary soil contribution to uplift resistance occurs in the foreslope and that depth of soil cover does not affect the required tiedown force. Using the FEA, design charts were developed with which engineers can determine for a given situation if restraint force is required to prevent an uplift failure. If an engineer determines restraint is needed, the design charts provide the magnitude of the required force. The design charts are applicable to six gages of CMP for four flow conditions and two types of soil.
Resumo:
The purpose of this investigation was to obtain information relative to the alkali-silica reaction in Iowa aggregates. Of particular concern were those aggregates in southwestern Iowa thought to be potentially alkali reactive. Further, should those aggregates have proven to be alkali-reactive, at what cement alkali content could these aggregates be considered to be deleteriously reactive? If the aggregates were proven to be reactive, what types of effects might show up in a structure in which an alkali-silica reaction has occurred? Also, what environmental conditions would cause the reaction? Finally, based on the information obtained from the investigation, would it be possible to raise the cement alkali content specifications? Would the Iowa DOT eliminate the alkali content limits altogether except for cement used with reactive aggregate in the same manner as AASHTO or ASTM? Also, would there be any other side effects that might occur as the result of using high alkali-cement?