106 resultados para 220

em QUB Research Portal - Research Directory and Institutional Repository for Queen's University Belfast


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Torrefaction based co-firing in a pulverized coal boiler has been proposed for large percentage of biomass co-firing. A 220 MWe pulverized coal-power plant is simulated using Aspen Plus for full understanding the impacts of an additional torrefaction unit on the efficiency of the whole power plant, the studied process includes biomass drying, biomass torrefaction, mill systems, biomass/coal devolatilization and combustion, heat exchanges and power generation. Palm kernel shells (PKS) were torrefied at same residence time but 4 different temperatures, to prepare 4 torrefied biomasses with different degrees of torrefaction. During biomass torrefaction processes, the mass loss properties and released gaseous components have been studied. In addition, process simulations at varying torrefaction degrees and biomass co-firing ratios have been carried out to understand the properties of CO2 emission and electricity efficiency in the studied torrefaction based co-firing power plant. According to the experimental results, the mole fractions of CO 2 and CO account for 69-91% and 4-27% in torrefied gases. The predicted results also showed that the electrical efficiency reduced when increasing either torrefaction temperature or substitution ratio of biomass. A deep torrefaction may not be recommended, because the power saved from biomass grinding is less than the heat consumed by the extra torrefaction process, depending on the heat sources. 

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Traditionally the simulation of the thermodynamic aspects of the internal combustion engine has been undertaken using one-dimensional gas-dynamic models to represent the intake and exhaust systems. CFD analysis of engines has been restricted to modelling of in-cylinder flow structures. With the increasing accessibility of CFD software it is now worth considering its use for complete gas-dynamic engine simulation. This paper appraises the accuracy of various CFD models in comparison to a 1D gas-dynamic simulation. All of the models are compared to experimental data acquired on an apparatus that generates a single gas-dynamic pressure wave. The progress of the wave along a constant area pipe and its subsequent reflection from the open pipe end are recorded with a number of high speed pressure transducers. It was found that there was little to choose between the accuracy of the 1D model and the best CFD model. The CFD model did not require experimentally derived loss coefficients to accurately represent the open pipe end; however, it took several hundred times longer to complete its analysis. The best congruency between the CFD models and the experimental data was achieved using the RNG k-e turbulence model. The open end of the pipe was most effectively represented by surrounding it with a relatively small volume of cells connected to the rest of the environment using a pressure boundary.

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Variable geometry turbines provide an extra degree of flexibility in air management in turbocharged engines. The pivoting stator vanes used to achieve the variable turbine geometry necessitate the inclusion of stator vane endwall clearances. The consequent leakage flow through the endwall clearances impacts the flow in the stator vane passages and an understanding of the impact of the leakage flow on stator loss is required. A numerical model of a typical variable geometry turbine was developed using the commercial CFX-10 computational fluid dynamics software, and validated using laser doppler velocimetry and static pressure measurements from a variable geometry turbine with stator vane endwall clearance. Two different stator vane positions were investigated, each at three different operating conditions representing different vane loadings. The vane endwall leakage was found to have a significant impact on the stator loss and on the uniformity of flow entering the turbine rotor. The leakage flow changed considerably at different vane positions and flow incidence at vane inlet was found to have a significant impact.

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The introduction of advanced welding methods as an alternative joining process to riveting in the manufacture of primary aircraft structure has the potential to realize reductions in both manufacturing costs and structural weight. Current design and analysis methods for aircraft panels have been developed and validated for riveted fabrication. For welded panels, considering the buckling collapse design philosophy of aircraft stiffened panels, strength prediction methods considering welding process effects for both local-buckling and post-buckling behaviours must be developed and validated. This article reports on the work undertaken to develop analysis methods for the crippling failure of stiffened panels fabricated using laser beam and friction stir welding. The work assesses modifications to conventional analysis methods and finite-element analysis methods for strength prediction. The analysis work is validated experimentally with welded single stiffener crippling specimens. The experimental programme has demonstrated the potential static strength of laser beam and friction stir welded sheet-stiffener joints for post-buckling panel applications. The work undertaken has demonstrated that the crippling behaviour of welded stiffened panels may be analysed considering standard-buckling behaviour. However, stiffened panel buckling analysis procedures must be altered to account for the weld joint geometry and process altered material properties. © IMechE 2006.

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The Irish hospitals sweepstake was established by statute in the Irish Free State in 1930 to fund the state’s hospital service. The vast majority of tickets were sold outside Ireland, particularly in countries where such gambling was illegal at the time. Initially the largest market was in the United Kingdom, but following the introduction of restrictive legislation there in 1934, the promoters of the sweepstake turned their attentions to North America and after 1936 the United States became the largest source of contributions to the Irish sweep. This article examines a number of factors concerning the relationship of the Irish sweep with the USA, including: an effort to estimate the amount of money contributed to the sweep by Americans; the role of the Irish diaspora and of prominent republicans, including Joseph McGarrity and Connie Neenan, in the illegal ticket distribution network; the efforts of American Federal agencies and government departments to disrupt the sweepstake organisation in America; how the sweep was used by those who sought to legalise gambling in the USA; the attitudes of both the Irish and American governments to the sweep’s activities in America; and how the legalisation of gambling in America brought about the demise of the Irish sweep.

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