39 resultados para Internal combustion engine
Resumo:
Moving from combustion engine to electric vehicle (EV)-based transport is recognized as having a major role to play in reducing pollution, combating climate change and improving energy security. However, the introduction of EVs poses major challenges for power system operation. With increasing penetration of EVs, uncontrolled coincident charging may overload the grid and substantially increase peak power requirements. Developing smart grid technologies and appropriate charging strategies to support the role out of EVs is therefore a high priority. In this paper, we investigate the effectiveness of distributed additive increase and multiplicative decrease (AIMD) charging algorithms, as proposed by Stu¨dli et al. in 2012, at mitigating the impact of domestic charging of EVs on low-voltage distribution networks. In particular, a number of enhancements to the basic AIMD implementation are introduced to enable local power system infrastructure and voltage level constraints to be taken into account and to reduce peak power requirements. The enhanced AIMD EV charging strategies are evaluated using power system simulations for a typical low-voltage residential feeder network in Ireland. Results show that by using the proposed AIMD-based smart charging algorithms, 50% EV penetration can be accommodated, compared with only 10% with uncontrolled charging, without exceeding network infrastructure constraints.
Resumo:
The Li-O2 battery may theoretically possess practical gravimetric energy densities several times greater than the current state-of-the-art Li-ion batteries.1 This magnitude of development is a requisite for true realization of electric vehicles capable of competing with the traditional combustion engine. However, significant challenges must be addressed before practical application may be considered. These include low efficiencies, low rate capabilities and the parasitic decomposition reactions of electrolyte/electrode materials resulting in very poor rechargeability.2-4 Ionic liquids, ILs, typically display several properties, extremely low vapor pressure and high electrochemical and thermal stability, which make them particularly interesting for Li-O2 battery electrolytes. However, the typically sluggish transport properties generally inhibit rate performance and cells suffer similar inefficiencies during cycling.5,6
In addition to the design of new ILs with tailored properties, formulating blended electrolytes using molecular solvents with ILs has been considered to improve their performance.7,8 In this work, we will discuss the physical properties vs. the electrochemical performance of a range of formulated electrolytes based on tetraglyme, a benchmark Li-O2 battery electrolyte solvent, and several ILs. The selected ILs are based on the bis{(trifluoromethyl)sulfonyl}imide anion and alkyl/ether functionalized cyclic alkylammonium cations, which exhibit very good stability and moderate viscosity.9 O2 electrochemistry will be investigated in these media using macro and microdisk voltammetry and O2 solubility/diffusivity is quantified as a function of the electrolyte formulation. Furthermore, galvanostatic cycling of selected electrolytes in Li-O2 cells will be discussed to probe their practical electrochemical performance. Finally, the physical characterization of the blended electrolytes will be reported in parallel to further determine structure (or formulation) vs. property relationships and to, therefore, assess the importance of certain electrolyte properties (viscosity, O2supply capability, donor number) on their performance.
This work was funded by the EPSRC (EP/L505262/1) and Innovate UK for the Practical Lithium-Air Batteries project (project number: 101577).
1. P. G. Bruce, S. A. Freunberger, L. J. Hardwick and J.-M. Tarascon, Nat. Mater., 11, 19 (2012).
2. S. A. Freunberger, Y. Chen, N. E. Drewett, L. J. Hardwick, F. Barde and P. G. Bruce, Angew. Chem., Int. Ed., 50, 8609 (2011).
3. B. D. McCloskey, A. Speidel, R. Scheffler, D. C. Miller, V. Viswanathan, J. S. Hummelshøj, J. K. Nørskov and A. C. Luntz, J. Phys. Chem. Lett., 3, 997 (2012).
4. D. G. Kwabi, T. P. Batcho, C. V. Amanchukwu, N. Ortiz-Vitoriano, P. Hammond, C. V. Thompson and Y. Shao-Horn, J. Phys. Chem. Lett., 5, 2850 (2014).
5. Z. H. Cui, W. G. Fan and X. X. Guo, J. Power Sources, 235, 251 (2013).
6. F. Soavi, S. Monaco and M. Mastragostino, J. Power Sources, 224, 115 (2013).
7. L. Cecchetto, M. Salomon, B. Scrosati and F. Croce, J. Power Sources, 213, 233 (2012).
8. A. Khan and C. Zhao, Electrochem. Commun., 49, 1 (2014).
9. Z. J. Chen, T. Xue and J.-M. Lee, RSC Adv., 2, 10564 (2012).
Resumo:
The internal combustion (IC) engines exploits only about 30% of the chemical energy ejected through combustion, whereas the remaining part is rejected by means of cooling system and exhausted gas. Nowadays, a major global concern is finding sustainable solutions for better fuel economy which in turn results in a decrease of carbon dioxide (CO2) emissions. The Waste Heat Recovery (WHR) is one of the most promising techniques to increase the overall efficiency of a vehicle system, allowing the recovery of the heat rejected by the exhaust and cooling systems. In this context, Organic Rankine Cycles (ORCs) are widely recognized as a potential technology to exploit the heat rejected by engines to produce electricity. The aim of the present paper is to investigate a WHR system, designed to collect both coolant and exhausted gas heats, coupled with an ORC cycle for vehicle applications. In particular, a coolant heat exchanger (CLT) allows the heat exchange between the water coolant and the ORC working fluid, whereas the exhausted gas heat is recovered by using a secondary circuit with diathermic oil. By using an in-house numerical model, a wide range of working conditions and ORC design parameters are investigated. In particular, the analyses are focused on the regenerator location inside the ORC circuits. Five organic fluids, working in both subcritical and supercritical conditions, have been selected in order to detect the most suitable configuration in terms of energy and exergy efficiencies.
Resumo:
With the legislative demands increasing on recreational vehicles and utility engined applications, the two-stroke engine is facing increasing pressure to meet these requirements. One method of achieving the required reduction is via the introduction of a catalytic converter. The catalytic converter not only has to deal with the characteristically higher CO and HC concentration, but also any oil which is added to lubricate the engine. In a conventional two-stroke engine with a total loss lubrication system, the oil is either scavenged straight out the exhaust port or is entrained, involved in combustion and is later exhausted. This oil can have a significant effect on the performance of the catalyst.
To investigate the oiling effect, three catalytic converters were aged using a 400cm₃ DI two-stroke engine. A finite level of oil was added to the inlet air of the engine to lubricate the internal workings. The oil flow rate is independent of the engine speed and load.
Three catalysts were aged for 50 hours, experiencing a constant space velocity and set engine conditions. The engine was fueled on petrol and later on propane to eliminate the effects, if any, of petrol additives on catalyst deactivation. The oiling rate was varied to investigated deactivation from oil contamination. Post-mortem analysis was performed on the three catalysts. This consisted of a controlled light-off test performed on a catalyst rig, during which period, temperatures were measured and recorded towere aged for 50 hours, experiencing a constant space velocity and set engine conditions. The engine was fueled on petrol and later on propane to eliminate the effects, if any, of petrol additives on catalyst deactivation. The oiling rate was varied to investigated deactivation from oil contamination. Post-mortem analysis was performed on the three catalysts. This consisted of a controlled light-off test performed on a catalyst rig, during which period, temperatures were measured and recorded to find out where deactivation of each catalyst was occurring. The recorded results were all analyzed and these showed that from the measured light-off temperatures the aged catalysts behaved similarly. However the pattern in the light-off was significantly different when the engine was fueled by propane as opposed to gasoline.
Resumo:
Turbocompounding is the process of recovering a proportion of an engine’s fuel energy that would otherwise be lost in the exhaust process and adding it to the output power. This was first seen in the 1930s and is carried out by coupling an exhaust gas turbine to the crankshaft of a reciprocating engine. It has since been recognised that coupling the power turbine to an electrical generator instead of the crankshaft has the potential to reduce the fuel consumption further with the added flexibility of being able to decide how this recovered energy is used. The electricity generated can be used in automotive applications to assist the crankshaft using a flywheel motor generator or to power ancillaries that would otherwise have run off the crankshaft. In the case of stationary power plants, it can assist the electrical power output. Decoupling the power turbine from the crankshaft and coupling it to a generator allows the power electronics to control the turbine speed independently in order to optimise the specific fuel consumption for different engine operating conditions. This method of energy recapture is termed ‘turbogenerating’.
This paper gives a brief history of turbocompounding and its thermodynamic merits. It then moves on to give an account of the validation of a turbogenerated engine model. The model is then used to investigate what needs to be done to an engine when a turbogenerator is installed. The engine being modelled is used for stationary power generation and is fuelled by an induced biogas with a small portion of palm oil being injected into the cylinder to initiate combustion by compression ignition. From these investigations, optimum settings were found that result in a 10.90% improvement in overall efficiency. These savings relate to the same engine without a turbogenerator installed operating with fixed fuelling.