27 resultados para rail tunnel


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Using a prism-air gap-sample (Otto) configuration we have optically excited surface plasmon polaritons at the Ag-air interface of passive Al-Al oxide-Ag tunnel junction structures at wavelength 632.8 nm. It is found that the internal damping of this excitation is more than a factor of 2 greater for samples with a very thin (approximately 15 nm) Ag electrode than for samples with a thicker (approximately 40 nm) Ag electrode. This observation is explained by the fact that the fields of the surface plasmon polariton penetrate more substantially into the lossy Al base electrode when the Ag top electrode is very thin.

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Visible light is emitted from the Au-air interface of Al-I-Au thin-film tunnel junctions (deposited over a thin layer of CaF2 on glass) as a result of the decay of surface plasmon polaritons (SPPs). We show the surface topography of such a Au film and relate its large-scale features to the outcoupling of fast SPP's to photons. The absence of short-scale roughness features is explained by thier disappearance through surface diffusion. To confirm this a controlled sequence of 5-nm, 20-ms scanning tunneling microscope (STM) W tip crashes has been used to produce indentations 3 nm deep with a lateral dimension of 5-7 nm on a Au crystal in air at room temperature. Four sequences of indentations were drawn in the form of a square box. Right from the start, feature decay is observed and over a period of 2 h a succession of images shows that the structure disappears into the background as a result of surface diffusion. The surface diffusion constant is estimated to be 10(-18) cm2 s-1. The lack of light output via slow mode SPPs is an inevitable consequence of surface annealing.

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Transonic tests in linear cascade wind tunnels can suffer
from significant test section boundary interference effects in pitch. A slotted tailboard has been designed and optimised with an in-house Euler numerical method to reduce such ef- fects. Wind tunnel measurements on an overspeed Mach 1.27 discharge from a Rolls-Royce T2 cascade, featuring strong end-wall shock-induced interference, showed a 77% reduction in the flow pitchwise periodicity error with the optimised tail- board, with respect to the baseline open-jet cascade flow. Two-dimensional Euler predictions were also cross-validated against a three-dimensional Reynolds averaged computation, to explore the three-dimensionality of the discharge