114 resultados para sugar cane crops
Resumo:
Pilot and industrial scale dilute acid pretreatment data can be difficult to obtain due to the significant infrastructure investment required. Consequently, models of dilute acid pretreatment by necessity use laboratory scale data to determine kinetic parameters and make predictions about optimal pretreatment conditions at larger scales. In order for these recommendations to be meaningful, the ability of laboratory scale models to predict pilot and industrial scale yields must be investigated. A mathematical model of the dilute acid pretreatment of sugarcane bagasse has previously been developed by the authors. This model was able to successfully reproduce the experimental yields of xylose and short chain xylooligomers obtained at the laboratory scale. In this paper, the ability of the model to reproduce pilot scale yield and composition data is examined. It was found that in general the model over predicted the pilot scale reactor yields by a significant margin. Models that appear very promising at the laboratory scale may have limitations when predicting yields on a pilot or industrial scale. It is difficult to comment whether there are any consistent trends in optimal operating conditions between reactor scale and laboratory scale hydrolysis due to the limited reactor datasets available. Further investigation is needed to determine whether the model has some efficacy when the kinetic parameters are re-evaluated by parameter fitting to reactor scale data, however, this requires the compilation of larger datasets. Alternatively, laboratory scale mathematical models may have enhanced utility for predicting larger scale reactor performance if bulk mass transport and fluid flow considerations are incorporated into the fibre scale equations. This work reinforces the need for appropriate attention to be paid to pilot scale experimental development when moving from laboratory to pilot and industrial scales for new technologies.
Resumo:
This paper discusses the main milling train management tasks necessary for maintaining good extraction performance through a season. The main activities discussed are making week by week decisions about shredder and mill setting adjustments, and selecting preseason mill settings. To maintain satisfactory milling train extraction performance, the main factors affecting extraction should be examined: cane preparation with pol in open cells or shredder torque, delivery nip compaction through the load or torque controller outputs such as roll lift, feed chute flap position or pressure feeder to mill speed ratio, and added water rate. To select mill settings for the coming season, delivery nip compaction and feed chute exit compaction can be inferred from the previous seasons.
Resumo:
This paper describes recent updates to a milling train extraction model used to assess and predict the performance of a milling train. An extension was made to the milling unit model for the bagasse mills to replace the imbibition coefficient with crushing factor and mixing efficiency. New empirical relationships for reabsorption factor, imbibition coefficient, crushing factor, mixing efficiency and purity ratio were developed. The new empirical relationships were tested against factory measurements and previous model predictions. The updated model has been implemented in the SysCAD process modelling software. New additions to the model implementation include: a shredder model to assess or predict cane preparation, mill and shredder drives for power consumption and an updated imbibition control system to add allow water to be added to intermediate mills.
Resumo:
As more raw sugar factories become involved in the manufacture of by-products and cogeneration, bagasse is becoming an increasingly valuable commodity. However, in most factories, most of the bagasse produced is used to generate steam in relatively old and inefficient boilers. Efficient bagasse fired boilers are a high capital cost item and the cost of supplying the steam required to run a sugar factory by other means is prohibitive. For many factories a more realistic way to reduce bagasse consumption is to increase the efficiency of existing boilers. The Farleigh No. 3 boiler is a relatively old low efficiency boiler. Like many in the industry, the performance of this boiler has been adversely affected by uneven gas and air flow distributions and air heater leaks. The combustion performance and efficiency of this boiler have been significantly improved by making the gas and air flow distributions through the boiler more uniform and repairing the air heater. The estimated bagasse savings easily justify the cost of the boiler improvements.
Resumo:
Clarification performance and flocculant dosage is strongly linked to the mud solids loading in the feed entering the clarifier. The recycle of filtrate can represent an extra ~10-15% mud solids loading on the clarifier, thereby reducing its effective capacity. Filtrate recycling may cause significant increase in turbidity, complexed calcium ion formation, phosphate, proteins and polysaccharides in mixed juice that impact on evaporator scale formation and molasses exhaustion. The paper details the results obtained from laboratory, pilot scale and factory trials of filtrate clarification using both sedimentation and flotation methods. Clarified filtrate could be produced of similar quality to ESJ. Filtrate clarification was able to significantly remove insoluble solids, turbidity, phosphate, and polysaccharides content with slight reductions in minerals content of the filtrate. On the basis of improved filtrate quality, the clarified filtrate could be directed to ESJ, instead of the normal practice of directing the mud filtrate to mixed juice. The potential impacts of implementing filtrate clarification are discussed in respect to improved performance and throughput of the clarification station.
Resumo:
This study investigated the potential use of sugarcane bagasse as a feedstock for oil production through microbial cultivation. Bagasse was subjected to dilute acid pretreatment with 0.4 wt% H2SO4 (in liquid) at a solid/liquid ratio of 1:6 (wt/wt) at 170 °C for 15 min, followed by enzymatic hydrolysis of solid residue. The liquid fractions of the pretreatment process and the enzymatic hydrolysis process were detoxified and used as liquid hydrolysate (SCBLH) and enzymatic hydrolysate (SCBEH) for the microbial oil production by oleaginous yeast (Rhodotorula mucilaginosa) and filamentous fungi (Aspergillus oryzae and Mucor plumbeus). The results showed that all strains were able to grow and produce oil from bagasse hydrolysates. The highest oil concentrations produced from bagasse hydrolysates were by M. plumbeus at 1.59 g/L (SCBLH) and 4.74 g/L (SCBEH). The microbial oils obtained have similar fatty acid compositions to vegetable oils, indicating that the oil can be used for the production of second generation biodiesel. On the basis of oil yields obtained by M. plumbeus, from 10 million t (wet weight) of bagasse generated annually from sugar mills in Australia, it is estimated that the total biodiesel that could be produced would be equivalent to about 9% of Queensland’s diesel consumption.
Resumo:
Chloromethylfurfural (CMF), a valuable intermediate for the production of chemicals and fuel, can be derived in high yields from the cellulose component of biomass. This study examined the effect of sugar cane bagasse components and biomass architecture on CMF/bio-oil yield using a HCl/dichloroethane biphasic system. The type of pretreatment affected bio-oil yield, as the CMF yield increased with increasing glucan content. CMF yield reached 81.9% with bagasse pretreated by acidified aqueous ionic liquid, which had a glucan content of 81.6%. The lignin content of the biomass was found to significantly reduce CMF yield, which was only 62.3% with acid-catalysed steam exploded sample having a lignin content of 29.6%. The change of CMF yield may be associated with fibre surface changes as a result of pretreatment. The hemicellulose content also impacted negatively on CMF yield. Storage of the bio-oil in chlorinated solvents prevented CMF degradation.