54 resultados para Zero voltage switching (ZVS) converters
em Cambridge University Engineering Department Publications Database
Resumo:
A fully integrated 0.18 μm DC-DC buck converter using a low-swing "stacked driver" configuration is reported in this paper. A high switching frequency of 660 MHz reduces filter components to fit on chip, but this suffers from high switching losses. These losses are reduced using: 1) low-swing drivers; 2) supply stacking; and 3) introducing a charge transfer path to deliver excess charge from the positive metal-oxide semiconductor drive chain to the load, thereby recycling the charge. The working prototype circuit converts 2.2 to 0.75-1.0 V at 40-55 mA. Design and simulation of an improved circuit is also included that further improves the efficiency by enhancing the charge recycling path, providing automated zero voltage switching (ZVS) operation, and synchronizing the half-swing gating signals. © 2009 IEEE.
Resumo:
This paper advocates 'reduce, reuse, recycle' as a complete energy savings strategy. While reduction has been common to date, there is growing need to emphasize reuse and recycling as well. We design a DC-DC buck converter to demonstrate the 3 techniques: reduce with low-swing and zero voltage switching (ZVS), reuse with supply stacking, and recycle with regulated delivery of excess energy to the output load. The efficiency gained from these 3 techniques helps offset the loss of operating drivers at very high switching frequencies which are needed to move the output filter completely on-chip. A prototype was fabricated in 0.18μm CMOS, operates at 660MHz, and converts 2.2V to 0.75-1.0V at ∼50mA.1 © 2008 IEEE.
Resumo:
The design and manufacture of a prototype chip level power supply is described, with both simulated and experimental results. Of particular interest is the inclusion of a fully integrated on-chip LC filter. A high switching frequency of 660MHz and the design of a device drive circuit reduce losses by supply stacking, low-swing signaling and charge recycling. The paper demonstrates that a chip level converter operating at high frequency can be built and shows how this can be achieved, using zero voltage switching techniques similar to those commonly used in larger converters. Both simulations and experimental data from a fabricated circuit in 0.18μm CMOS are included. The circuit converts 2.2V to 0.75∼1.0V at ∼55mA. ©2008 IEEE.
Resumo:
Large digital chips use a significant amount of energy to broadcast a low-skew, multigigahertz clock to millions of latches located throughout the chip. Every clock cycle, the large aggregate capacitance of the clock network is charged from the supply and then discharged to ground. Instead of wasting this stored energy, it is possible to recycle the energy by controlling its delivery to another part of the chip using an on-chip dc-dc converter. The clock driver and switching converter circuits share many compatible characteristics that allow them to be merged into a single design and fully integrated on-chip. Our buck converter prototype, manufactured in 90-nm CMOS, provides a proof-of-concept that clock network energy can be recycled to other parts of the chip, thus lowering overall energy consumption. It also confirms that monolithic multigigahertz switching converters utilizing zero-voltage switching can be implemented in deep-submicrometer CMOS. With multigigahertz operation, fully integrated inductors and capacitors use a small amount of chip area with low losses. Combining the clock driver with the power converter can share the large MOSFET drivers necessary as well as being energy and space efficient. We present an analysis of the losses which we confirm by experimentally comparing the merged circuit with a conventional clock driver. © 2012 IEEE.
Resumo:
Power consumption of a multi-GHz local clock driver is reduced by returning energy stored in the clock-tree load capacitance back to the on-chip power-distribution grid. We call this type of return energy recycling. To achieve a nearly square clock waveform, the energy is transferred in a non-resonant way using an on-chip inductor in a configuration resembling a full-bridge DC-DC converter. A zero-voltage switching technique is implemented in the clock driver to reduce dynamic power loss associated with the high switching frequencies. A prototype implemented in 90 nm CMOS shows a power savings of 35% at 4 GHz. The area needed for the inductor in this new clock driver is about 6% of a local clock region. © 2006 IEEE.
Resumo:
High-power converters usually need longer dead-times than their lower-power counterparts and a lower switching frequency. Also due to the complicated assembly layout and severe variations in parasitics, in practice the conventional dead-time specific adjustment or compensation for high-power converters is less effective, and usually this process is time-consuming and bespoke. For general applications, minimising or eliminating dead-time in the gate drive technology is a desirable solution. With the growing acceptance of power electronics building blocks (PEBB) and intelligent power modules (IPM), gate drives with intelligent functions are in demand. Smart functions including dead time elimination/minimisation can improve modularity, flexibility and reliability. In this paper, a dead-time minimisation using Active Voltage Control (AVC) gate drive is presented. © 2012 IEEE.
IGBT converters conducted EMI analysis by controlled multiple-slope switching waveform approximation
Resumo:
IGBTs realise high-performance power converters. Unfortunately, with fast switching of the IGBT-free wheel diode chopper cell, such circuits are intrinsic sources of high-level EMI. Therefore, costly EMI filters or shielding are normally needed on the load and supply side. In order to design these EMI suppression components, designers need to predict the EMI level with reasonable accuracy for a given structure and operating mode. Simplifying the transient IGBT switching current and voltage into a multiple slope switching waveform approximation offers a feasible way to estimate conducted EMI with some accuracy. This method is dependent on the availability of high-fidelity measurements. Also, that multiple slope approximation needs careful and time-costly IGBT parameters optimisation process to approach the real switching waveform. In this paper, Active Voltage Control Gate Drive(AVC GD) is employed to shape IGBT switching into several defined slopes. As a result, Conducted EMI prediction by multiple slope switching approximation could be more accurate, less costly but more friendly for implementation. © 2013 IEEE.