144 resultados para LIFT-OFF
Resumo:
When a racing driver steers a car around a sharp bend, there is a trade-off between speed and accuracy, in that high speed can lead to a skid whereas a low speed increases lap time, both of which can adversely affect the driver's payoff function. While speed-accuracy trade-offs have been studied extensively, their susceptibility to risk sensitivity is much less understood, since most theories of motor control are risk neutral with respect to payoff, i.e., they only consider mean payoffs and ignore payoff variability. Here we investigate how individual risk attitudes impact a motor task that involves such a speed-accuracy trade-off. We designed an experiment where a target had to be hit and the reward (given in points) increased as a function of both subjects' endpoint accuracy and endpoint velocity. As faster movements lead to poorer endpoint accuracy, the variance of the reward increased for higher velocities. We tested subjects on two reward conditions that had the same mean reward but differed in the variance of the reward. A risk-neutral account predicts that subjects should only maximize the mean reward and hence perform identically in the two conditions. In contrast, we found that some (risk-averse) subjects chose to move with lower velocities and other (risk-seeking) subjects with higher velocities in the condition with higher reward variance (risk). This behavior is suboptimal with regard to maximizing the mean number of points but is in accordance with a risk-sensitive account of movement selection. Our study suggests that individual risk sensitivity is an important factor in motor tasks with speed-accuracy trade-offs.
Resumo:
Lateral insulated gate bipolar transistors (LIGBTs) in silicon-on-insulator (SOI) show a unique turn off characteristic when compared to junction-isolated RESURF LIGBTs or vertical IGBTs. The turn off characteristic shows an extended `terrace' where, after the initial fast transient characteristic of IGBTs due to the loss of the electron current, the current stays almost at the same value for an extended period of time, before suddenly dropping to zero. In this paper, we show that this terrace arises because there is a value of LIGBT current during switch off where the rate of expansion of the depletion region with respect to the anode current is infinite. Once this level of anode current is approached, the depletion region starts to expand very rapidly, and is only stopped when it reaches the n-type buffer layer surrounding the anode. Once this happens, the current rapidly drops to zero. A quasi-static analytic model is derived to explain this behaviour. The analytically modelled turn off characteristic agrees well with that found by numerical simulation.
Resumo:
Aircraft in high-lift configuration shed multiple vortices. These generally merge to form a downstream wake consisting of two counter-rotating vortices of equal strength. The understanding of the merger of two co-rotating trailing vortices is important in evaluating the separation criteria for different aircraft to prevent wake vortex hazards during landing and take-off. There is no existing theoretical method on the basis of which such norms can be set. The present study is aimed at gaining a better understanding of the behaviour of wake vortices behind the aircraft. Two dimensional studies are carried out using the vortex blob method and compared with Bertenyi's experiment. It is shown that inviscid two dimensional effects are insufficient to explain the observations. Three dimensional studies, using the vortex filament method, are applied to the same test case. Two Lamb-Oseen profile vortices of the same dimensions and initial separation as the experiment are allowed to evolve from a straight starting condition until a converged steady flow is achieved. The results obtained show good agreement with the experimental distance to merger. Core radius and separation behaviour is qualitatively similar to experiment, with the exception of rapid increases at first. This may be partially attributable to the choice of filament-element length, and recommended further work includes a convergence study for this parameter. Copyright © 2005 by the American Institute of Aeronautics and Astronautics, Inc. All rights reserved.
Resumo:
Comprehensive understanding of the long-term performance of cement-bentonite slurry trench cut-off walls is essential as these mixes may degrade when exposed to aggressive environments or when subjected to prolonged drying. A series of wetting-drying and immersion experiments was carried out to evaluate the durability characteristics of laboratory mixed samples and block field samples from 40 days to 11 years of age. For the wetting-drying tests, the samples buried in medium graded sand were subjected to periodical flooding and drying cycles. They were then used for permeability testing and unconfined compressive strength (UCS) testing. For the immersion tests, the samples confined in perforated molds were submerged in magnesium sulfate solution for 16 weeks and their microstructures were then analyzed using X-ray diffraction (XRD) technique. This paper identifies the effects of contaminant exposure on durability of cement-bentonite and the effects of aging by comparing 11 years old samples to younger samples. Test results showed that young or previously contaminated cement-bentonite mixes are more susceptible to sulfate attack than old or less contaminated mixes. Copyright ASCE 2008.
Resumo:
In this paper, the effects of wake/leading-edge interactions were studied at off-design conditions. Measurements were performed on the stator-blade suction surface at midspan. The leading-edge flow-field was investigated using hotwire micro-traverses, hotfilm surface shear-stress sensors and pressure micro-tappings. The trailing-edge flow-field was investigated using hotwire boundary-layer traverses. Unsteady CFD calculations were also performed to aid the interpretation of the results. At low flow coefficients, the time-averaged momentum thickness of the leading-edge boundary layer was found to rise as the flow coefficient was reduced. The time-resolved momentum-thickness rose due to the interaction of the incoming rotor wake. As the flow coefficient was reduced, the incoming wakes increased in pitch-wise extent, velocity deficit and turbulence intensity. This increased both the time-resolved rise in the momentum thickness and the turbulent spot production within the wake affected boundary-layer. Close to stall, a drop in the leading-edge momentum thickness was observed in-between wake events. This was associated with the formation of a leading-edge separation bubble in-between wake events. The wake interaction with the bubble gave rise to a shedding phenomenon, which produced large length scale disturbances in the surface shear stress. Copyright © 2008 by ASME.